ML19341C635

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LER 81-006/03L-0:on 810127,ATWS/recirculation Pump Trip High Pressure Trip Points from PT-2-3-56Bm,56Cm & 56Dm Tripped Above Tech Spec Level During Surveillance Testing Per Operation Procedure 4342.Caused by Instrument Drift
ML19341C635
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 02/25/1981
From: Murphy W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19341C631 List:
References
LER-81-006-03L, LER-81-6-3L, NUDOCS 8103030856
Download: ML19341C635 (1)


Text

NSC FCIM 384 U. S. NUCLEAR REGULATORY COMMISSION

, LICENSEE EVENT REPORT LER 81-06/3L CONTROL BLOCK: l l l l l l lh (PLEASE PRINT OR TYPE ALL REQUIREO INFORMATION) lo lil8l9VI TlLICENSEE 7

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, t o is l l health or safety. This event is r.ot repetative. I l017l l ,

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l i l o l l The instruments invclved are all master trip units associated with a Rosemount modell ,

m I510 DU Trip /Calibra: ion System which was installed during the past refueling outage. I l i 121 I The cause for the out-of-specification cot:dition is instrument drif t. The instru- I lil3l lments were immediately adjusted to the required setpoints. I tilai I l 7 8 9 80 ST  % POWER OTH ER STATUS is RY DISCOVERY DESCRIPTION I1 l5 l W@ l 1 l 0 l 0 l@l NA l lBl@l Surveillance Testing l ACTtvlTV CO TENT RELEASE AMOUNT 08 ACTIVITY LOCATION OP RELEASE fits 819L7J @D 08 RELEASEL7J@l 7 10 11 NA 44 I I 45 NA 80 l

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