05000260/LER-1980-059-03, /03L-0:on 801230,FR-77-16 Observed Downscale During Drywell Equipment Drain Sump Pump Operation.Caused by Shift in Model 555 GE Transmitter FT77-16 Zero Adjustment. Transmitter Recalibr,Tested & Returned to Svc

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/03L-0:on 801230,FR-77-16 Observed Downscale During Drywell Equipment Drain Sump Pump Operation.Caused by Shift in Model 555 GE Transmitter FT77-16 Zero Adjustment. Transmitter Recalibr,Tested & Returned to Svc
ML19341B242
Person / Time
Site: Browns Ferry 
Issue date: 01/26/1981
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19341B231 List:
References
LER-80-059-03L-02, LER-80-59-3L-2, NUDOCS 8101300512
Download: ML19341B242 (2)


LER-1980-059, /03L-0:on 801230,FR-77-16 Observed Downscale During Drywell Equipment Drain Sump Pump Operation.Caused by Shift in Model 555 GE Transmitter FT77-16 Zero Adjustment. Transmitter Recalibr,Tested & Returned to Svc
Event date:
Report date:
2601980059R03 - NRC Website

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60 63 OOCK ET NUMBER 68 69 EVENT OATE 74 73 REPORT DATE tHe EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h lo121 lDuring normal operation, the unit operator observed FR-77-16 downscale while the g jdrywell equipment drain sump pump was operating. Flow system declared inoperable i o,4, j at 0001 (TS 3.6.c.2).

There are no redundant systems. There was no effect on the I gojsj l health or safety of the public. Previous events: 296/8019.

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Tennessee Valley Authority Form BF 17 Browns Ferry Nuclear Plant BF 15.2 1/10/79 LER SUPPLEMENTAL INFORMATION BFRO 260 / 8059 Technical Specification Involved 3.6.c.2 Reported Under Technical Specification 6.7.2.b(2)

Date of Occurrence 12/30/80 Time of Occurrence 0001 Unit.

2 Identification and Description of Occurrence:

The operator observed a downscale indication on FR 77-16 while the 'drywell equipment drain sump pump was operating.

Conditions' Prior to Occurrence:

Unit 1 at 0% power.

Unit 2 at 96% power.

' Unit 3 refueling.

Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.

None Apparent Cause of Occurrence:

The zero on the instrument loop transmitter, FT-77-16 had shifted.

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Analysis of Occurrence:

There was no danger to the health or safety of the public, no release.of activity, no damage to plant or equipment and no,resulting significant chain of events.

Corrective Action

The transmitter was recalibrated, functionally tested and returned to service.

Failure Data:

296/8019

  • Retention:

eriod - Lifetime; Responsibility - Administrative Supervisor

  • Revision:

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