05000318/LER-1980-052-03, /03L-0:on 801103,CTMT Penetration Room Exhaust Fan Discharge Damper 22 Linkage Was Found Broken.Caused by Excessive Wear on Clevis Pin Due to Inadequate Lubrication. Linkage Repaired & Restored to Svc on 801104

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/03L-0:on 801103,CTMT Penetration Room Exhaust Fan Discharge Damper 22 Linkage Was Found Broken.Caused by Excessive Wear on Clevis Pin Due to Inadequate Lubrication. Linkage Repaired & Restored to Svc on 801104
ML19341A211
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 01/08/1981
From: Pence W, Wenderlich R
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19341A210 List:
References
LER-80-052-03L-01, LER-80-52-3L-1, NUDOCS 8101220390
Download: ML19341A211 (1)


LER-1980-052, /03L-0:on 801103,CTMT Penetration Room Exhaust Fan Discharge Damper 22 Linkage Was Found Broken.Caused by Excessive Wear on Clevis Pin Due to Inadequate Lubrication. Linkage Repaired & Restored to Svc on 801104
Event date:
Report date:
3181980052R03 - NRC Website

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8 80 81 DOCKET NUM8ER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROSABLE CONFEQUENCES h F5Til I During nonnal operation at 0645, the linkaoe was found to be broken for i

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  1. 22 CTMT penetration room exhaust fan discharge damoer, a dearadation of I

LO_L_1I the requirements of T.S. 3.6.6.1.

The linkaae was repaired and restored I

iO isI I to service at 1345 on 11-4-80. The other CTNT penetration room exhaust i

LO_L8_I I air filter train remained operable. This event had no impact upon the 1

lOi>i i public health or safety.

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gi existing preventive maintenance orocedure for insoection of the linkaoe I

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