ML19340B282

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LER 80-020/01T-0:on 800926,breaker Which Supplies Power to B Standby Liquid Control Sys Pump & B Squib Valve Found Open. Caused by Accidental Tripping of Pump Breaker.Breaker Switches of All Sblc Pumps Locked
ML19340B282
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 10/10/1980
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19340B277 List:
References
LER-80-020-01T, LER-80-20-1T, NUDOCS 8010210735
Download: ML19340B282 (1)


Text

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j gt .2 uCENSEE EVENT REPORT deport No. 2-80 -20/1T-0 cc,.muL utuco i I

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hvENT DESCRIPTION AND PROGAOLE CONSEQUENCES h

!Ml T With unit at full power, the "SBLC Loss of Continuity" alarm was I

. (~m l received. Immediate investigation revealed that the breaker which l

, oitI supplies power to the 'B' SBLC pump and 'B' Squib valve was open. I l gM i The breaker was immediately closed restoring the SBLC system to full ,_

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ngl operability. Continued operation was permitted by Tech Spec 3.h.B.1. I

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$YSTE M CAUSE CAUSE COMP. VALVE CODE CoOE SUSCODE COMPONENT CODE SU8 CODE SUSCODE lM

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10 11 12 83 tu 19 SEQUENTI A L OCCURRENCE REPORT HEVI$lON

, gg R EVENT YEAR R EPORT NO. CODE i i.* E N O.

@ aseo,Ro ar I8101 1-1 101210I l-l I0111 i Tl 1-1 1 01

_,, 21 22 23 24 2G 27 18 29 30 31 32 Af:1 tofs itittne6 CFFECT SiH J100WN A IT ACHMEN T Neitu d PRIMf COMP 8'f MPf)NL N 1 IAKLN AC Iluf4 UN e'LAN T MkTHUO HOUHh sutsMit'f Lu FOHM buts buPPLil H MAffuf AGIUI4 Lit lXI@lXl@ lZl@ W@ l 0 l0 l0 l0 l lYl@ W@ l Nl@ lCl7l710l@

J3 34 J3  % 3/ 40 48 42 43 44 4s CAUSC GCSCH1PTioN ANo CORRECTIVE ACTIONS IT A I Cause of event is believed to be an accidental tripping of the pump I t.!il l breaker by someone bumping the switch which was at knee level and was I

- 1 i i ,1 ! - adjacent to a step-off pad. The breaker switches of all EBLC pumps l

1i ; ij l have been locked, the contaminated area has been decontaminated, and l l

. i s .. l l ' the step-off pad has been removed. I i 4 3 oc <

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Yv'OEs* secWER oTHER STATUS @ 45 ll RY 04SCOVERY DESCFetPTION 1iEl@ l0l9-l9l@l N/A l [_A_j@l Control Room Alarm l A TivtTY . CO TENT nELE AsEn oF RELEASE AMOUNTCF ACTivlTY LOCATION OF RELEASE 3, A Z l @ -li uZI@l N/A o

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