05000277/LER-1980-020-01, /01T-0:on 800926,breaker Which Supplies Power to B Standby Liquid Control Sys Pump & B Squib Valve Found Open. Caused by Accidental Tripping of Pump Breaker.Breaker Switches of All Sblc Pumps Locked

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/01T-0:on 800926,breaker Which Supplies Power to B Standby Liquid Control Sys Pump & B Squib Valve Found Open. Caused by Accidental Tripping of Pump Breaker.Breaker Switches of All Sblc Pumps Locked
ML19340B282
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 10/10/1980
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19340B277 List:
References
LER-80-020-01T, LER-80-20-1T, NUDOCS 8010210735
Download: ML19340B282 (1)


LER-1980-020, /01T-0:on 800926,breaker Which Supplies Power to B Standby Liquid Control Sys Pump & B Squib Valve Found Open. Caused by Accidental Tripping of Pump Breaker.Breaker Switches of All Sblc Pumps Locked
Event date:
Report date:
2771980020R01 - NRC Website

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!Ml With unit at full power, the "SBLC Loss of Continuity" alarm was I

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' the step-off pad has been removed.

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