05000318/LER-1980-043-03, /03L-0:on 800914,during Normal operation,22B Safety Injection Tank Level Indication Became Erratic.Cause Not Known.Bench Test Revealed No Malfunction.Level Transmitter Replaced,Recalibr & Returned to Svc

From kanterella
(Redirected from ML19338F502)
Jump to navigation Jump to search
/03L-0:on 800914,during Normal operation,22B Safety Injection Tank Level Indication Became Erratic.Cause Not Known.Bench Test Revealed No Malfunction.Level Transmitter Replaced,Recalibr & Returned to Svc
ML19338F502
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 10/14/1980
From: Lagiewski J, Rizzo P
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19338F501 List:
References
LER-80-043-03L-01, LER-80-43-3L-1, NUDOCS 8010200434
Download: ML19338F502 (2)


LER-1980-043, /03L-0:on 800914,during Normal operation,22B Safety Injection Tank Level Indication Became Erratic.Cause Not Known.Bench Test Revealed No Malfunction.Level Transmitter Replaced,Recalibr & Returned to Svc
Event date:
Report date:
3181980043R03 - NRC Website

text

nytw. n; n~K l ~

, LtdENSEE EVENT REPORT L [h hNhotstoCS ' 'l

( i - L iPLEist PRINT OQ TYPE ALL f,EEUGED INPChh4ATIOM :

I^ l LI" II

.n 4

@l'l'$7 CAT sil@

L I MI o f c i c I n1L@l o l'o l' 1 o I o I o-1 o I o'l lo' l o @l411 11 11 I l

o
- 9.

.LICEN885 CODE.. 10

.16 -

uCENSE NvwSE't.

2! >

38

. LICENSE TvPs Jo I~, con'T '. -

5'"

' Q " M' ' p; 41l Ol'5' l'010'l 0 'l'3'l 1-18 @l 019 I l'l 4-l 8 l 0 l@ll'l O'l1 l 4 l'R In l@ L

. DOCKET NUMS&M

. 81 et EVENT DATE.

74 76 -

RSPORT DATE 80 I

+

EVENT DESCRIPTION AND PROsA9LE CoNSEQUENC13 h M I<

Ourina -nomal ~ operation. 22n Safety Iitiection Tank (SIT)-level indica- -

I-

.L

r.amm al iion became erratic and increased to >199" at-0320. - The reactor was

'l

~

placed i' Hode'3'and pressure reduced <1750 osio per T.S. 3.5;1.b at I

n 4

l L

'1425. The level. transmitter was replaced and recalibrated. Estimated

~1

[ nrTTI 1 b nnT'l l ~

. tank level prio'r-to~ draining was 246". ~228 SIT was return?d to ser-

- l ITTTI-l viceat:0245on'9/15/80. The three other SIT's ' remained _ooerable dur-in9 this event. This event is similar to LER 80-50 (Docket #05000317).

1 r.wa :

['-

  1. '~

Jsgu cgu,5p,gug

,CgPg

,g (0

J1 I I E l@' lx ]@ I x l@ ~ l x I xI x I x I x I x 18 -ll J@ @* @

9 S

9

- 10 It 12..

13

- 18 19 l. '7' SEQUENTIAL OCCURRENCE REPORT REvitiON -

tg ef mo EVENT Y E AR REPORT NO.

CODE TYPE No.

'@sg 18 10 - l.

[ :,,,) -

l 0 l 41 31 Iel lOI31-L!;,j.

L, -l.

L9.J a

21 22 23 -

24-26 27 28 29 30 31

- 32

~.

K N AC P NT MET

- HOURS 22 5ei POR 5.

Su Lt MANU8 URER.

l x l@lX.]@, 3 @

LAJ@

l 01012171' LY J@

ULj@

l 4 l@ lZliI9I9l@'

J 33 34,

36 37 40 41 42 43 44 47

. CAUSE DESCRIPTIOfd AND CORRECTIVE ACTIONS h.-

li l o l:l' No cause has been deterrriined for-the erratic tank level indicatinn.

I:

p L'_1.' J l Bench tests nerfomed on the re91 aced transt.11tter have revealed nn i

i gl mal function. Neither sense line nor-isolation valve lankage was ob-1 g [,-

- served during reolacement of the transmitter und calibrations nerfo rva -

l

. LLli) !'

'in the: field.

I 80

'7 i6 g3 I ST N POWER'.--

CTHER $7ATVS 15 R

OtSCOVERY DESCRIPTION -

~ W@,l 0l 4 l-0l@l HAi l

LA_,j @l Operator Observation 1

i s I.'

8 4 ; h'h7 '
- 12!

11.

44 46 46 80 -

' RELE ASED OF RELEASE '

AMOUNT OF ACTtvlTY

~

LOCATION 07 RELEASE e tLZ j @ L Z,,j@l NA

'l l

NA

  • l o i
7

'.S.9 10 ft.

44 45 --

90 I

PER$ONNEt, EXPOSURES.

y;l0lYl*0'l@h@l "" $

l PERSONN INJV IES i*'

7.-
- S i.fi '

0,1@ DESCRIPTION NA*

I 1

NUMSER-1-

u.

20 -

.11.

12

~ D G5 0F CA OAMAGE 70 PActLlTY TYPE @[ DESCRIPTION U 17

'NA l

1 9 80~

]

i - t 7 u.

?SE9.-

~

10

. NR.C USE ONLY Ls g ',.

1.. Pustic Tv :,

~

< ts

' Os5CRiPTdON

'HAL I.'l 1 1 l l l'lLI I l 'l I I i~

, n ;

l n

68,6,91

,80 7j L 17.3

-; 3 ; 9 }

10.,

y C

q*

cy,y, a),,,, A,,,-: 4.s!"L'acisuski/P.G. Rizzo

,, Ways;- (301)~259 a747/4706

.Y ~

l L :.

v

~.-

<\\

..' m.

m 4

a-

'LLER NO 43/3L

DOCKET NO.-

50-318~-

EVEilT DATE. _09/14/80-REPORT DATE D10/14/80 cATTACHMENT CAUSE DESCRIPTION AND CORRECTIVE ACTIONS:

b

~

.During the' next. Unit 2 Refueling 0utage_ additional work is to be i

performed on the process sensing lines _ to the transmitter.

Connecting fittings will be replaced and additional testing for leaks will be perfomed under Main +enance-Request 0-80-2940.

l l

l l

l

'. i l

I i

l' I

I

- 4 1.

<s 4

- 4

+

J r-