05000313/LER-1980-034-03, /03L-0:on 800905,during Normal Operation,Small Primary to Secondary Leak Developed from Steam Generator E24A.Caused by Flow Induced Vibration Crack in Tube 74-2. Tube Was Plugged & Unit Returned to Svc

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/03L-0:on 800905,during Normal Operation,Small Primary to Secondary Leak Developed from Steam Generator E24A.Caused by Flow Induced Vibration Crack in Tube 74-2. Tube Was Plugged & Unit Returned to Svc
ML19338F163
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 10/01/1980
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19338F151 List:
References
LER-80-034-03L-01, LER-80-34-3L-1, NUDOCS 8010070582
Download: ML19338F163 (1)


LER-1980-034, /03L-0:on 800905,during Normal Operation,Small Primary to Secondary Leak Developed from Steam Generator E24A.Caused by Flow Induced Vibration Crack in Tube 74-2. Tube Was Plugged & Unit Returned to Svc
Event date:
Report date:
3131980034R03 - NRC Website

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EVENT oAfg 24 7b HE,oHT04TE to EVENT OtSCRIPTION AND PROSA8LE CONSEQUENCES h i During nonnal power operation, a s:nall primary to secondary leak developed, o,

i as indicated by an increase of the Condenser Vacuum Pump exhaust radiatiom rm i fBTil I monitor indication.

Leakage was verified to be from Steam Generator.

I i E24A, by analysis of the secondary system activity.

The RCS leak rate I

o s I limit per T.S. 3.1.6.1 and the secondary system activity limit per T.S.

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i 3.10 were not exceeded.

An orderly unit shutdown was executed.

Similar i o,

i to occurrence LER 50-313/80-026.

Reportable per T.S. 6.12.3.2.d.

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33 J4 JS 36 33 40 el 42 e3 as op CAust DESCRIPTION AND CORRECflVE ACTIONS 27 8 I Following unit shutdown. testing identified the leaker to be tube 74-2.

I ITTrl i Eddy Current (NDE) inspection was conducted of four rows on each side of i i the "open lane", a samplino of tubes around the leaker and special i

i i 3 Iinterest tubes. Cause of failure "is believed to be due to a Flow Inducedi i Vibration crack propagating from defect.. Tube 74-2 was plugged and unit i e,ggturned to service.

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