05000366/LER-1980-131-03, /03L-0:on 800909,reactor Pressure Switch 2B31-N018A Actuated at 162 Psig Rather than 135 Psig.Caused by Setpoint Drift.Switch Recalibr & Tested Successfully

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/03L-0:on 800909,reactor Pressure Switch 2B31-N018A Actuated at 162 Psig Rather than 135 Psig.Caused by Setpoint Drift.Switch Recalibr & Tested Successfully
ML19338E881
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 09/30/1980
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19338E877 List:
References
LER-80-131-03L, LER-80-131-3L, NUDOCS 8010060259
Download: ML19338E881 (2)


LER-1980-131, /03L-0:on 800909,reactor Pressure Switch 2B31-N018A Actuated at 162 Psig Rather than 135 Psig.Caused by Setpoint Drift.Switch Recalibr & Tested Successfully
Event date:
Report date:
3661980131R03 - NRC Website

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LICENSEE EVENT REPORT coNTnoL CLOCK:

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60 69 DOCK ET NU'/D ER 6tl 63 EVENT DATE 14 7h REPOHT DAT E 80 EVENT DESCRIPTION AND PROBAOLE CoNSEoVENCES h 10121 l With the unit in start-up and hot standby at 0 Mut, while performing HNP i ioi3i l 3102, Reactor Pressure Shutdown Cooling Mode FT & C, reactor pressure switch l

l r, 14 l l 2D31-N018A actuated at 162 psig increasing. Tech Specs, Section 3.3.2-2, I

l,Isl I item 6b, requires actuation at $135 +25 psig head correction. Redundant l

l 21 r,1 l switch 2B31-N0188 was within tolerance. Safe plant operation nor the health I

lo lil I and safety of the public was not affected by this event. This is a repetitive l

i;is j l event as last reported on Reportable Occurrence No. '50-366/1980-121.

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40 41 42 43 44 4f CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11 1011 The cause of this event has been attributed to setpoint drift.

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[. ii j l was recalibrated and functionally tested successfully.

Unit I uses the I

iiigi l same type switch, Barksdale Model B2T, for this application.

A generic l

l 1.13 ] l review revealed no inherent problems.

The unit is now in full compliance.

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LER. fi.50-366/1980-131 1

Licensee:. Georgia Power Company Facility Name:- Edwin I. Hatch Docket #: ~50-366

Narrative

Report for ' LER 50-366/1980-131.

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On September 9,1980, while -the reactor was; starting up'following anLunplanned

. shutdown, 2B31-N018A, switch #2, Reactor Shutdown Cooling Mode Instrument, was

. found to actuate at 162 psig increasing while performing HNP-2-3102, Reactor

- High Pressure Shutdown Cooling Mode Instrument Functional Test and Calibration.
- Tech Specs Section 3.3.2-2, item 6b', requires actuation.at 5135 +25 psig head -

correction.

Switch #1 actuated in tolerance and redundant switch 2831-N018B actuated in' tolerance.

Plant operation was not affected and the.public health I

and safety was not affected.

ThisLis a repetitive event as last reported on

~ Reportable Occurrence Report No. ' 50-366/1980-121.

The cause o'f this event was attributed to setpoint drift.

The switch was immediately recalibrated and functionally tested successfully.

Unit I uses the same. type of' switch, a Barksdale Model B2T, for this operation.

A generic review revealedjno inherent problems.

The~ unit is now in full-

- compliance and no further reporting is required.

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