ML19332E394

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Forwards Maint Team Insp Repts 50-254/89-17 & 50-265/89-17 on 890918-22,1002-06 & 18 & Notice of Violation.Executive Summary Also Encl.Specific Strengths & Significant Weaknesses Listed
ML19332E394
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 11/28/1989
From: Miller H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Reed C
COMMONWEALTH EDISON CO.
Shared Package
ML19332E395 List:
References
NUDOCS 8912070170
Download: ML19332E394 (4)


See also: IR 05000254/1989017

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NOV 2 81989

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Docket No. 50-254

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Docket No. 50-265

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Commonwealth' Edison Company

ATTH:' Mr. Corde n Reed

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rienior Vice President

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- Post Office Box 767-

' Chicago, IL 60690

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Gentlemen:

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' This reftra to toe Special Haintenance Team Inspection perfcrmed by

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Mr. J. rl. Heisler and others of this office on September 18-22, October 2-6,

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.and 18,~1989.- This inspection covered activities at the Quad Cities Nuc1 car

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Generat'.ng Station, Un3ts 1 and 2, as authorited by NRC Operating Licenses

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No. DPR-09 and DPR-30, and-the inspection findings that were discussed with

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Mr. D. Galle and others of your staff at the conclurion of the inspection.

The inspection was conducted during an outage to assess and evaluate your

support and implementation-of maintenance to assure that plant structures,

systems, and components reliably perform on demand. Various activities were.

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evaluated to determine if maintenance was accomplished, effective, and

' adequately assessed by your own quality verification process.

The enclosed copy of our inspection report identifies specific areas examined

during.the' inspection. Within these areas, the inspection consisted of a

selective examination of procedures and representative records, observations,

and interviews with personnel.

In an attempt to focus on those activities

that are most risk significant, insight from a Quad Cities Probabilistic Risk

Assessment Study performed by the NRC was used to select systems and

components important to safety.

The inspection team concluded that maintenance at Quad Cities Nuclear Generating

Station was, in general, satisfactorily performed, effective, and well managed.

-The team identified strengths as well as weaknesses in the maintenance program.

The Executive Summary highlights our inspection findings, and Section 4.0 of the

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inspection report provides a synopsis of your maintenance program.

Some of the specific strengths noted by the inspection team were:

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Management comitment to improve station maintenance through reliability

centered maintenance based on System Unavailability Monitoring Studies

(SUMS), and Component Failure Analysis Reports (CFAR) Program, and the

introduction of new maintenance techniques such as laser alignment, new

diagnostic testing methods for MOVs, and vibration analysis of station

equipment.

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Commonwealth Edison Company

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An excellent load monitoring program to track load changes on power sources.

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Good communications program for informing the plant staff of management

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goals and objtctives and industry initiatives.

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Some of the mere significant weaknesses were:

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Deficiencies in procedural compliance und content that resulted 4n

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failure to follow acceptance criteria for establishing cable pull

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tension, undocumented lifted leads during maintenance and no acceptance

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' criteria in procedures for diesel and HPCJ overspeed tests.

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Inadequate engineering support of mt.intenance as indicated by inadequate

seismic evaluation of the replacement impeller for the HPCI booster

pump, inadequate vendor manual review that omitted some vendor

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recommendations from the preventive maintenance program, cod minimal

system eagineering involvement in root cause analysis and trending.

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Inadequate corrective action that resulted in improper fuse replacement,

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one-third of the indicating lights being out on the control rod position

indicating panel in Unit 2, and lack of periodic testing and inspection of

the RCIC turbine overspeed trip linkage despite an LER being issued in

1986.

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Control of contractors as evidenced by a contractor using a MOV as a

work bench for cutting conduit, a contractor QC inspector not observing a

QC hold point during maintenance, and a contractor employee lying on bags

in a radiation controlled area.

During this inspection, certain of your activities appeared to be in violation

of NRC requirements as specified in the enclosed Notice. A written response

is required.

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In accordance with 10 CFR 2.790 of the Comission's regulations, a copy of-

this letter, the enclosures, and your response to this letter will be placed in

the NRC Public Document Room.

The responses directed by this letter and the accompanying Notice are not

subject to the clearance procedures of the Office of Management and Budget as

required by the Paperwork Reduction Act of 1980, PL 96-511.

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NOV 2 81989

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Comonwealth Edison Company

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We iv111 gladly discuss any questions you have concerning this inspection.

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Sincerely,

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Origim) nirgned by T. O. Martin (for)

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'h.. J. Miller. Direcht

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DhiLion of Reactor Laf ety

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Enciosures:

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Hotice of Violation

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Inspection Report

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No. 50-254/89017(DRS);

No. 50-265/89017(DRS)

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cc w/rnelosures:

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T. Kovach, Nuc* ear

Licensing Manager

R. L. Bax, Station Manager

DCD/DCB (RIDS)

Licensing Fee Management Branch

Resident Inspector, Rill

Richard Hubbard

J. W. McCaffrey, Chief, Public

Utilities Division

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Comissioner Curtiss, OCM/JC

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K. Hart, NRR/LPED

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Division Directors. DRS

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RI, RII, RIV, and RV

T. Marsh, NRR/MEB

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EXECUTIVE SUMMARY

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An announced NkC team inspection was performed at Quad Cities Nuclear Station

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during the period September 18-22, October 2-6 and 18, 1989. The inspection

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was performed to evaluate the exte..t that a maintenance program had been

establi Aed and implemented at Quad Cities to assure the preservation or

restoration of the availability and reliability of plant structures, systems,

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and components to operate on demand. Three major areas were assessed,

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Aneluding ovoroll plast performance ss affected by maintenance, management

support of maintenance, and implementatiorn

Tc accomplish this task, several

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maintenance related 9etivities were-evaluated to determine if maintenance was

accomplished, effective, and self-assessed.

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The inspection tearc noted specific strcngths in it'e areas of management viger

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in introducing nee maintenance techniques such as laser alignment of rotating

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equipment and adranced testing for MOVs; reliability centered maintenance

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program based on System Unavai' ability Monitoring Studies (SUMS); Component

Failure Analysis Report (CFAR) program based on industry experience; ciectrical

load monitoring program *, ALARA su) port for major maintenance; unique color

coding to clearly differentiate tie units; and communications to staff on

industry initiatives, management goals and objectives with regard to maintenance.

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Ueaknesses

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Poor _ technical support in the development of procedures resulted in a lack of

acceptance criteria for the overspeed trip settings in test procedures for

overspeed trip tests for emergency diesels-and HPCI turbines. Additionally,

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the PM procedures did not include the vendor recommendations for seriodic

linkage tests of HPCI and RCIC turbines, in spite of previous pro)1 ems with the

RCIC turbine overspeed linkage. Weaknesses were noted with the level of system

awareness and technical knowledge of system engineers and their lack of

involvement in failure and root cause analysis. The amount of quality control

coverage of electrical and I&C maintenance work was weak.

Instances of poor

contractor control were noted, in that no work packages were noticed near a job

site with work in progress, misuse of plant equipment by a contractor occurred,

and a contractor was noticed to be inattentive in a radiation area. A weakness

was also observed in the uskeep of control rod position indication status in

-the control room in that a>out one-third of the CRD position indications on

Unit 2 were blank due to burned out light bulbs.

Conclusion

Results of this inspection showed the maintenance program at Quad Cities to be

generally well managed and effectively implemented. Based on the review of past

work activities, observations of ongoing work activities, work controls, and

attempts at self-assessment, the inspectors determined that overall electrical,

mechanical, and I&C maintenance and support activities were adequately performed

to maintain operability of components at a level commensurate with the

components' function.

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