05000277/LER-1980-014-04, /04T-0:on 800808,oil Sheen Observed on Conowingo Pond,Near Berm That Separates Pond from Cooling Towers. Caused by Oil Overflow Due to Incorrect Level Gauge Reading in Diesel Storage Tank a During Oil Delivery.Gauge Recalibr

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/04T-0:on 800808,oil Sheen Observed on Conowingo Pond,Near Berm That Separates Pond from Cooling Towers. Caused by Oil Overflow Due to Incorrect Level Gauge Reading in Diesel Storage Tank a During Oil Delivery.Gauge Recalibr
ML19331D213
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 08/18/1980
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19331D210 List:
References
LER-80-014-04T, LER-80-14-4T, NUDOCS 8008270524
Download: ML19331D213 (1)


LER-1980-014, /04T-0:on 800808,oil Sheen Observed on Conowingo Pond,Near Berm That Separates Pond from Cooling Towers. Caused by Oil Overflow Due to Incorrect Level Gauge Reading in Diesel Storage Tank a During Oil Delivery.Gauge Recalibr
Event date:
Report date:
2771980014R04 - NRC Website

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