ML19330B326

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IE Insp Rept 50-461/80-10 on 800501-30.Noncompliance Noted: Control Rod Drive Penetration Rework Activity Performed W/O Written Approved Instructions or Approved Design Change
ML19330B326
Person / Time
Site: Clinton Constellation icon.png
Issue date: 06/19/1980
From: Knop R, Livemore H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19330B323 List:
References
50-461-80-10, NUDOCS 8007310367
Download: ML19330B326 (4)


See also: IR 05000461/1980010

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U.S. NUCLEAR REGULATORY COMMISSION

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0FFICE OF INSPECTION AND ENFORCEMENT

REGION III

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Report No. 50-461/80-10

Docket No. 50-461

License No. CPPR-137

Licensee:

Illinois Power Company

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500 27th Street

Decatur,-IL 62525

Facility Name:

Clinton Power Station, Unit 1

-Inspection At:

Clinton Site, Clinton, IL

Inspection Con eted: May 1-30, 1980

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Inspector:

H. H. Liveritore

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Approved By:

R. C. Knop, Chie

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Projects Section 1

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Inspection Summary

Inspection on May 1-30, 1980 (Report No. 50-461/80-10)

Areas Inspected: Routine inspection by the IE Regional Resident Inspector

(SRI) of safety related construction activities including concrete place-

ment, inaterial laydown and storage areas. This inspection involved 85

inspector-hours by one NRC inspector.

Results: Of the areas inspected, one item of noncompliance was identified.

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DETAILS

Persons Contacted

Principal Licensee Employees

  • G. M. Brashear, Site Manager, Clinton

R. J. Canfield, Director-Construction

  • A. J. Budnick, Director-QA
  • E.

E. Connou, Assistant Director-Construction

L. W. Dozier, Assistant Director-Construction

D. E. Korneman, Supervisor-Construction

  • J. F. Hampton, Supervisor-QA
  • R. W. Folck, QA Specialist
  • J.

S. Spencer, Director-Engineering

R. Backen, QA Specialist

R. Weber, QA Engineer

R. Becker, QA Consultant

  • J.

M. King, Electrical Supervisor

Baldwin Associates

  • J. R. Hilding, QA Manager
  • R.

Selva, Manager Quality and Technical Services

  • J. Linehan, QC Manager
  • W.

H. Harrington, Project Manager

  • J.

E. Findley, Project Engineer

M. Merritt, Quality Control

  • T.

F. Walker, Senior Quality Control

  • R.

D. Bennett, Manager, Technical Services

General Electric Company

  • S.

G. Hall, Quality Control

Other staff and personnel were contacted during the reporting period.

  • Denotes those attending at least one of the exit meetings.

Functional or Program Areas Inspected

1.

Plant Toars

One or more plant areas were toured several times each week during

the reporting period to obset te general construction practices, area

cleanliness, and storage / maintenance of material and equipment.

Item of noncompliance is discussed in parceraph five (5).

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Concrete Placement

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The inspector performed a surveillance of concrete pours of reactor

building (outside CTW-20, Traveler 1246) and diesel generator build-

ing roof and 737 level equipment pads (1.raveler 1197).

The following conditions were noted:

(1) The forms were secure and leak tight prior to the placement.

(2) The preplacement inspection had been completed and was in order

for pour CTW 20.

The inspector noted that the traveler 1197 for

the 737' level equipment pad pour was not completely signed off

and concrete placement was in progress.

Investigation revealed

that the situation was one of Quality Control oversight and was

not typical of normal operation. The inspector will follow this

area and has no more questions at this time.

(3) Quality Control inspectors were assigned to perform periodic

concrete testing. Numbers were adequate.

(4) Concrete testing was performed at the required frequencies.

(5) Adequate numbers of crews and personnel were assigned to make

the placement.

(6) Surrounding equipment was protected from any concrete spill

during placement.

-(7) Delivery and placement were satisfactory.

Concrete was pumped

to the placement area and deposited via a flexible boot which

adequately confined the concrete to a minimum fall to prevent

segregation.

(8) Concrete was observed to be properly consolidated using internal

concrete vibrators. The vibrators were randomly checked while

operating in the concrete. Vibrator technique was satisfactory.

No items of noncompliance or deviations were identified.

3.

Inspection of Material / Component Laydown Areas

The resident inspector performed a followup surveillance of pipe,

electrical, and reb.r laydown outside storage areas. The inspec-

tion was in relation'to the requ'.rements of ANSI N45.2.2: material

protected and stored off the ground, caps on pipe ends, and segrega-

tion of safety and non-safety material. Much improvemt.nt had been

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made since the April report. The electrical laydown area had been

cleaned up and was satisfactory.

Pipe laydown was improvdi with ail

caps on, and ends protected. The rebar area showed marked improvement

with scrap removed and rebar moved off the ground and separated.

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No items of noncompliance or deviations were identified.

4.

Inspection of Power Block Areas

The inspector performed numerous inspection tours of the Reactor Fuel

and Auxiliary Buildings.

Inspection was for housekeeping, fire

hazard, and protection of safety related materials. The below ground

floors of the Auxiliary and Fuel Buildings had numerous examples of

safety related pipe laying on the floor, some in water, and examples

of trash and wood piled in arets conductive to fueling a fire. These

two areas were the greatest offenders. Management was notified and

took prompt action. The resident inspector performed followup in-

spections and noted that the area is in satisfactory condition at

this time. Future followups will be performed.

No items of noncompliance or deviations were identified.

5.

CRD Penetration Work Activity

The inspector performed a surveillance of the Reactor Building con-

trol rod drive (CRD) penetration rework activity. Due to some past

inferior welds, the constructor has been attempting to remove some

35 control rod drive tubes installed in the concrete drywell wall.

Existing job instructions covered specific numbered tubes to be

stress relieved and removed by pipe drilling. Adjacent to the CRD

tubes, a 3" exploratory hole was drilled through the exterior wall

plate, parallel to the tubes, cutting through rebar, and jamming

three feet into the concrete drywell wall. This operation was per-

formed without written approved instructions or an approved design

change.

This item is considered in noncompliance with the requirements of

Criterion V of 10 CFR 50, Appendix B (461/80-10-01).

Unresolved Matters

Unresolved n.atters are items about which more information is required in

order to ascertain whether they are acceptable items, items of noncom-

pliance, or deviations. There are no unresolved items.

Exit Meetings

The resident inspector attended an exit meeting conducted by the RIII

Inspectors Gallagher and Wescott on May 23, 1980. The inspector met

with the licensee representatives (denoted under Persons Contacted) on

May 9, 15, 27, and 30, 1980. The inspector summarized the scope and

findings of the inspections performed. The licensee representatives

acknowledged the findings reported in previous paragraphs.

Attachments:

Preliminary

Inspection Findings

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