ML19327A896

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Monthly Operating Rept for Sept 1989 for Callaway Unit 1. W/891006 Ltr
ML19327A896
Person / Time
Site: Callaway Ameren icon.png
Issue date: 09/30/1989
From: Blosser J, Mccann R
UNION ELECTRIC CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
ULNRC-2089, NUDOCS 8910190080
Download: ML19327A896 (6)


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Nuclear Regulatory Commission Document Control Desk Washington, DO 20555 ULNRC-2089 near Sir:

DOCKET NUMBER 50-483 CALLAWAY PLANT UNIT 1 FACILITY OPERATING LICENSE NPF-30 MONTHLY OPERATING REPORT--

SEPTEMBER 1989 The enclosed Monthly Operating Report for September, 1989 is submitted pursuant to section 6.9.1.8 of the Callaway Unit 1 Technical Specifications.

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. D. Blosser Manager, Callaway Plant V

DLHtt1 w tak JDB/ BEY /RDA/ TAM /RJM/ crc Enclosure cc: Distribution attached 8910190080 890930 PCR- ADOCK 05000483 R PDC NN mmno w en en uoen

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'cc!_ distribution for'ULNRC-2089

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-Mr. Robert DeFayette, Chief- '

Project Section-1A- .;

- U. S.-NuclearLRegulatory Commission-

' Region-III y 799' Roosevelt Road d

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M.T.' Thomas Alexion (2 copies)  ;

g ._ , Office of Ncclear. Reactor Regulation

'l ' - U.: S. Nuclear Regulatory Consission -

, :Q > Mail Stop P-316 7920 Norfolk Avenue i Bethesda, MD- 20014 ei

'NRC Resident Inspector '

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. Manager Electric Department

. Missouri!Puolic Service Commission 1

Pt O. Box 360 y ,

Jefferson. City, MO ;65102 g ':

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N , , ,, J DOCKET No., '50-483 >

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[ UNIT NAMEl- . CALLAW/,Y UNM 1

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?CH - CCOMPLETED BY'- -Ri J..McCann a?  ? :a;'

't- ' " TELEPHON~ I314/676-8243'-

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%" " , PART -A1 . . , OPERATIONS. SUMARY a:

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'J_ ;The plant.oyerated at approximately 1004 power with the following exceptions, p . ,

s .Fowet had,been reduced to.90% on 8/24/89 in order to overhaul circulating water pump A. Full power e ,

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.(operation resumed onl9/2/89. >

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  • 2. The unit was removed from service on 9/6/89 in' order to; restore S/C chemistry to within 1 specifications.following an inadverter : ' Auxiliary Feedwater Actuation Signal which caused ESW water

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to be injected 'into S/G's A' and D'(LER r/ 010). :. Full power operation resumed on 9/8/89. .

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AVERACE DAILY UNIT POWER LEV::L '
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,.-5 UNIT NAME' CALLAWAY UNIT 1 ..

W DCE- :10-06-89 1

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COMPLETED BY R. J. McCarn

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.. MONTH

, -LSEPTEMBER 1989 1AVERACE DAILY POWER LEVEL. AVERACE DAILY POWER LEVEL

~ DAY:- (MWe-Net) DAY (MWe-Net)

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Six , ,1032 17 1173-s s .2 ' -1088 18 11172

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, ;3 :1163' 19 '1173 4? I1163 20 1171 4

! :5: 1135 21 1171 m

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OPERATINC DATA REPORT i

tr sti DOCKET NO.- 50-483- i 1

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UNIT HAMEi .CALLAWAY UNIT 1 S

D Qi DATE. 10-06-89 *

  • $p COMPLETED BY- . R. J. McCann -

'IILEPHONE 314/676-8243

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a m, OPERATING ETATUS:

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b' p, + ' 1. . REPORTING PERIOD: SEPTEMBER 1989 CROSS Il0URS IN REPORTING PERIOD: 720 6,551 41,892.5.

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2. CURRENTLY AUT110RIZED POWER LEVEL (MWt): 3565 MAX. DEPEND. CAPACITY (MWe-Net): 1118 ,

' DESIGN ELECTRICAL RATING (HWe-Net): 1171 .;

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if, 3. . POWER LEVEL TO WHICll. RESTRICTED (IF ANY) (HWe Net): i fD ..

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f 4','- REASONS FOR RESTRICTION (IF ANY):

TilIS MONTH YP. TO DATE -CUMULATIVE L 5. NUMBER OF HOURS REACTOR WAS CRITICAL . . . . . . . . . . . . . . . 720 5,272.6 35,771.4-s s

6. ' REACIOR RESERVE SIIUTDOWN 110URS . . . . . . . . . . . . . . . . . . . . .

O. 0 0 1 --  : 7. 110URS GENERATOR ON LINE. . . . . . . . . . . . . . . . . . . . . . . . . . . . 673 5,160.9 34,745.4.

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.  ; 8. - UNIT RESFRVE SIfuTDOWN 110URS . . . . . . . . . . . . . . . . . . . . . . . . 0- 0 0

9. CROSS . TiiEPHAL ENERGY CENERATED (HWil) . . . . . . . . . . . . . . . 2,346,488 17,765,517 113,652,1281 f l0. CROSS ELECTRICAL ENERGY CENERATED (MW
!) ............ 807,037 6,058,155 :38,491,705 '

'11.--NET ELECTRICAL

  • CY GENERATED (MWH) .............. 768,524 5,765,138 36,509,339 12 REACTOR SERVI CE FACTok . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 100 . 80. 5 - 85.4

.13. LREACTOR AVAILABILITY FACTOR .....................~... 100 80.5 85.4:

14 UNITS 'ERVICE FACTOR ............................'.... 93.5 78.8- 82.9:

15. ' UNIT AVAILABILITY FACIOR ........................... 93.5 78.'8 82.9 +

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,g 16. : UNIT CAPACITY FACTOR (Using HDC) ...................

95.5 78.7 ' 71< . 0 l.

175 . UNIT CAPY ITY FACTOR (Using Desien HWe) ............ 91.2 ,75.2 74.4-t

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18.' UNIT FORCED OUTAGE RATE ............................ ,

6.5 1.5 3.7 19.' SHUTDOWNS SCHEDULED OVER NEXT 6 MONTilS (TYPE, DATE, AND DURATION OF EACil):

29. IF SHUT DOWN AT END OF REPORTING PERIOD, ESTIhATED DATE OF ETARTUP:

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. UNIT SHL N AND POWER REDUCTIONS

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DOCKET NO.-

UNIT NAME^

.50-483 CALIAWAY UNIT l' s

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DAIE. 10-06 COMPLMTD BY./ R; J. McCann' TELEPHONE 314/676-8243' REPORI MONTH:' SEPIDEER 1989 METHOD OF-TYPE SHUITING DOWN

' IIIE REACTOR OR 1 DURATION 1 F: 70RCED '

NO. DATE S: SCHEDULED (HOURS) REASON REDUCING POWER CORRECTIVE ACTIONS / COP 9EENTS 4

10 ' 8/24/89 F 0 B- 4 Reduced power to'approximately 90% in order to overhaul circulating water pump A. Full powe.r operation resumed on 9/02/89.' -

.11 9/06/89 F .47.0 G 1 The unit was removed from service in order to restore S/C chepiistry to within , specifications following an inadvertent- Auxiliary Feedwater '

./ctuation Signal which caused ESW water to be injected into'S/G's A!

and J (LER 89-010). Full power operation resumed on'9/08/89.-

SUMMARY

REASON METHOD A: EQUIPMENT FAILURE (EXPIAIN) 1: MANUAL B: MAINT. OR TEST ~2: MA'fUAL SCRAM C: REFUEIING 3: AUTOMATIC SCRAM D: REGULATORY. RESTRICTION' 4: OTHER-(EIPLAIN)

' F: OPERATOR TRAINING AND

. LICENSE EXAMINATION-F: ADMINISTRATIVE G: OPERATIONAL ERROR (EXPLAIN)

H: 'OTHER (EIPLAIN)

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