ML19327A623

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Forwards IE Bulletin 80-17, Failure of 76 of 185 Control Rods to Fully Insert During Scram at Bwr. No Written Response Required
ML19327A623
Person / Time
Site: Clinton  
Issue date: 07/03/1980
From: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Gerstner W
ILLINOIS POWER CO.
References
NUDOCS 8008060508
Download: ML19327A623 (1)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION Ik

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799 ROOSEVELT ROAD GLEN ELLYN. BLLINOls 60137 o

JUL' 3 880 Docket No. 50-461 Docket No. 50-462 Illinois Power Company ATTN:

Mr. W. C. Gerstner Executive Vice President 500 South 27th Street Decatur, IL 62525 Gentlemen:

This enclosed IE Bulletin No. 80-17, is forwarded to you for informa-tion. No written response is required.

If you desire additional information regarding this matter, please centact this office.

Sincerely, g4nxb JamesG.Kepp1Nr Director

Enclosure:

IE Bulletin No. 80-17 cc w/ encl:

Central Files Director, NRR/DPM Director, NRR/ DOR PDR Local PDR NSIC TIC Mr. Dean Hansell, Office of Assistant Attorney General Mr. Gary N. Wright, Chief Division of Nuclear Safety l

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O SSINS No.:

6820 Accession No.:

8005050076 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT JULY 3, 1980 IE BULLETIN NO. 80-17 FAILURE OF 76 0F 185 CONTROL RODS TO FULLY INSERT DURING A SCRAM AT A BWR Description of C':rcumstances:

On June 28, 1980, 76 of the 185 control rods failed to fully insert during a routine shutdown at TVA's Browns Ferry Unit No. 3 located at Athens, Alabama.

The reactor was manually scrammed from about 30 percent power in accordance with routine shutdown procedures.

The shutdown was initiated to repair the feedwater system.

The 76 control rods that failed to fully insert were all on the east side of the core.

Following scram' discharge volume (SDV) high level bypass and a short drain period of the SDV, a second manual scram was initiated and all partially inserted rods were observed to drive inward, but 59 remained partially withdrawn.

A third manual scram was made, again following high level in the SDV and bypassing for another short drain of the SDV, with the result that 47 rods remained partially withdrawn.

Following a longer drain of the SDV, an automatic scram occurred that was initiated by a scram discharge volume tank high water level signal when the scram reset switch was placed in " Normal"; with this scram all remaining rods fully inserted.

The total time elapse from the initial scram to the time that all rods were inserted was approximately 15 minutes.

Core coolant flow, temperature and pressure remained normal for plant conditions. The unit is now shutdown and additional testing indicates that a possible cause of the malfunction was the retention of a significant amount of water in the east bank scram discharge volume.

In view of these interim findings and pending results of continued investigation, the following actions are to be taken.

Actions To Be Taken By Licensees:

All General Electric Boiling Water Reactors with operating licenses which are operating at any power on the date of this Bulletin shall perform the following steps in the time stated...s - ' m.

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perform the following steps prior t j j

DUPLICATE DOCUMENT j

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Within 3 days from the date 01 i tests to verify that there is 1 Entire document previously DischargeVolume(SDV)andassj entered into system under-are operable and vent system i,1 Soo6c6co76 xNo No. of pages:

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