ML19326B853

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RO 50-313/76-25:on 760831,leak Found in Decay Heat Discharge Line B.Probably Caused by Excessive Vibration.Schedule 10 Piping Replaced W/New Section
ML19326B853
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 09/27/1976
From: David Williams
ARKANSAS POWER & LIGHT CO.
To:
Shared Package
ML19326B844 List:
References
NUDOCS 8004180590
Download: ML19326B853 (4)


Text

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('O 1-Reportabic Occurrence Report No. 50-313/76-25 2.

Report Date: 9/27/76 3.

Occurrence Date: 8/31/76 4

Facility:

Arkansa? Nuclear One-Unit 1 Rursellv11.a, Arkansas 5.

Identification of Occurrence:

Leak in "B" decay heat discharge line.

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Conditions Prior to Occurrence:

Steady-State Power Reactor Power 0

MWth llot Standby Not Output 0

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Cold Shutdown X

Percent of Full Power 0

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Refueling Shutdown Load Changes During Routine Power Operation i

Routine Startup i.

Operation Routine Shutdown

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Operation

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Other (specify) 7.

Description of Occurrence:

At 0420 hours0.00486 days <br />0.117 hours <br />6.944444e-4 weeks <br />1.5981e-4 months <br /> on 8/31/76, an approximate 2 gpm leak was discovered in the heat affected zone of the boss to line weld for DH-1019.

The crack was in the 10" discharge line downstream of decay heat.

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Attachuent "C" l

!! arch 23,1976 NSP-10, Rev. 4 Page 2 of 4 1

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Reportable Occurrence Report No.

50-313/76-25

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Designation of Apparent Cause ol' Occurrence:

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Design Procedurc Manufacture Unusual Service Condition including Environmental Installation /

Construction Component Failure Operator Other (specify)

X The probable cause of the crack was excessive vibration.

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Analysis of Occurrence:

The leak was confined to the Reactor Auxiliary Building; hence, there wa._no hazard to the health and safety of the public.

Attachment "C" March 23, 1976 NSP-10, Rev. 4 Page 3Of4 l

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Reportable Occurrence Report iio.

50-313/70-25 10.

Corrective Action:

The repair was made by removing r. 2 ft. section of the schedule 10.p.iping and replacing with new section.

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11.

Failure Data:

Cracked welds reported in Reportable Occurrence Report 50-313/74-2, 76-10, and 76-24.

Section of pipe had same heat number of 800201.

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