05000346/LER-1977-092-03, /03L-0:on 771101,facility Review Board Meeting Revealed That Surveillance Requirement of Venting Hpis Valve HP 72 Not Performed.Caused by Personnel Error.High Point Valve Vented & Modified

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/03L-0:on 771101,facility Review Board Meeting Revealed That Surveillance Requirement of Venting Hpis Valve HP 72 Not Performed.Caused by Personnel Error.High Point Valve Vented & Modified
ML19326A554
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 11/29/1977
From: Batch S
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19326A516 List:
References
LER-77-092-03L, LER-77-92-3L, NUDOCS 8002040720
Download: ML19326A554 (2)


LER-1977-092, /03L-0:on 771101,facility Review Board Meeting Revealed That Surveillance Requirement of Venting Hpis Valve HP 72 Not Performed.Caused by Personnel Error.High Point Valve Vented & Modified
Event date:
Report date:
3461977092R03 - NRC Website

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GCKET.MSER 6d ti3 EVENT DATE 74 75 REPORT DATE 83 EVENT DESCRIPTION ANO P90313LE COP 1200ENCES h i

I o t 2 g l During a Station Reviav Bo.rd meeting on November 1,1977, it was recognized that a

i One of I g g surveillance requirement of Technical Specification 4.5.2 was not. completed.

l l the four High Pressure Injection Lines (1-2) had not been vented per Surveillance _

lo 94; Io isi I Test, ST 5051.01, "ECCS Monthly" at vent valve HP 72 since August 1, 1977. The I

j o is i l Surveillance Tast.had been completed with the exceotion of HP 72 which was removed I

lol7l l from the procedure by modi! cation T-2232 on August 31, 1977. There was no danger i

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CAUSE DESCRIPTION AND CCRRECTIVE ACTIONS ii ;oll Personnel error is.the cause of this occurrence.

Vent Valve -HP 72 was incorrectiv I

g l removed from the Surveillance Test by operations personnel due to the near inacces _ _f _

,,,,; ; sib.:lity of'the valve.

- Th.a high coint at HP 72 was. vented on November 1, 1977, and.

L q, ; 3 g l the modification T-2232-was, voided.

Facility Change Request 77-428 was written on gii4; l November 2 ~1977 to request an improvement in the accessibility of vent valve HP 72.

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SUPPLEMENTAL INFORMATION FOR LER NP-33-77-92

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4 DATE OF EVENT: November 1, 1977

' FACILITY:

Davis-Besse Unit 1 l

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IDENTIFICATION OF OCCURRENCE: Failure to perform the surveillance requirement of t

venting High Pressure Injection Valve HP 72.

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Conditions Prior to Occurrencep The plant was.in Mode 1, with Power (MWT) = 693,.

.and Load (MWE) = 235.

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Description of Occurrence: During a Station Rt.lew Board meeting on November 1, i

1997, it was recognized that 4. surveillance requirement of Technical Specification l

(TS) 4.5.2 was not completed. -one of the four High Pressure Injection Lines (1-2) had not been vented per Surveillance Test, ST 5051.01, "ECCS Monthly" at vent valve HP 72 since August 1, 1977. The Surveillance Test had been completed with the ex-caption of HP 72 which was removed from the procedure by modification-T-2232 on _ -

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l August 31, 1977.

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' Designation of Apparent Cause of' Occurrence: ' Personnel error is the cause of this Vent Valve. HP 72 was incorrectly _ removed from the Surveillance Test occurrence.

f, by operations personne. due to-the near inaccessibility of the valve.

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Analysis of Occurrence: There was no danger to the health and safety of the public t

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or to station personnel. Only one of the-four High Pressure Injection (HPI) Lines-..~

was not ventied.

Also, once that.HPI Lines are filled, they. remain f411ed with the.

j pressure supplied from the Boratea Water-Storage. Tank.

Corrective Action

The higir point-at HP 72 was vented on November 1,1977 and..the.

modification T-2232 was veided.

Pipe hangers were verified to be in operable con-j dition on HPI Line 1-2 on November 8,1977 to verify no excessive pipe movements i

had occurred.

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Facility Change Request 77-428 was writren on November 2, 1977 to request an improve-i ment.in the accessibility of vent valve HP 72.

l The deletion of a surveillance requirement will be discussed with the operations personnel involved.

~ Failure Data: No previous occurrences 6f a temporary modification to a procedure causing a missed surveillance test or action have occurred.

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