LER-1978-028, /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed |
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LICENSEE CODE 14 10i'I so$,RCE l L l@l 0 l 510 l-l013 l 4 IJ}@ldl311l8l718]@l0l4lll31.7l8l@
CO.T 68 69 EVENT QATE 74 75 REPORT DATE 80 3~
60 61 OQCK ET *.U*.t3 E R EVENT OESCRIPTION AND PROS A8LE CONSEQUENCES h lo 2; l At 0950 hours0.011 days <br />0.264 hours <br />0.00157 weeks <br />3.61475e-4 months <br /> on March 18, 1978, Steam and Feedwater Rupture Control System (SFRCS)
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Channel 1 Steam Ce *erator (SG) 1-1 level input was declared inoperable. This placed l lo ial l the unit in the Ac: ion Statement 13 of Technical Specification 3.3.2.2, which requireq g o,., ; ;
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all eight SG 1evel inputs to be operable while in Modes 1, 2 or 3.
g a ; 3, danger to the health and safety of the public or unit personnel.
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47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h A small steam 1
Iilo1] Water was found in the connection box of level transmitter SP09B8.
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[ the connection box, surveillance testin;; was performed to verify operability. A l
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TOLEDO EDISON COMPANY N
DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION j
SUPPLEMENTAL INFORMATION FOR LER NP-33-78-32 DATE OF EVENT: March 18, 1978 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:
Steam and Feedwater Rupture Control System (SFRCS)
Channel 1, Steam Generator 1-1 level indication (Level Transmitter LT-SP0938) in-operable.
Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MRT) = 2107,
, and Load (MWE) = 725.
4 Description of Occurrence: On March 18,1978 at 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> during the performance of Surveillance Test ST 5099.01, " Miscellaneous Instru=ent Shif t Checks", an opera-tor noticed that level indication for SFRCS Channel 1 Steam Generator (SG) 1-1 level was reading higher than the other channels (but not at its maximum level).
At 0950 hours0.011 days <br />0.264 hours <br />0.00157 weeks <br />3.61475e-4 months <br />, Channel 1 SG l-1 level input was declared inoperable. This occur-rence placed the unit in Action Statement 13 of Technical Specification 3.3.2.2,.
which requires all eight SG 1evel inputs to be operable in Modes 1, 2 or 3.
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The Action Statement specifies that operation may proceed,until performance of the next required channel functional test, provided the inoperable section of the i
channel is placed in the tripped condition within one hour. Channel 1 SG l-1 level input was tripped at 1037 hours0.012 days <br />0.288 hours <br />0.00171 weeks <br />3.945785e-4 months <br />.
Because of high radiation levels inside Containment during power operation, reac-tor power was reduced at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on March 18,1978, from 76% to 25% of full power to allow personnel access to ineestigate and repair the problem.
Reactor power was returned to 75% of full power after LT-SP09B8 was declared operable at
.2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br /> on March 18, 1978.
Designation of Apoarent Cause of Occurrence: Maintenance Work Order I&C 255-78 was issued to investigate the cause of this occurrence'.
Instrument and Control personnel found water in the connection box of level transmitter LT-SP0938, and also in the conduit leading to the transmitter. The transmitter and leads were
' cleaned and dried.
A small steam leak in the vicinity is ' believed to have been the source of the water in the conduit. The water traveled through the conduit to the transmitter.
LER #78-028 G
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TOLEDO EDISON COMPANY N
DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION PAGE 2 SUPPLEMENTAL INFORMATION FOR LER NP-33-78-32 Analysis of Occurrence: There was no danger to the health and safety of the public or unit personnel. During the period that Channel 1 SG 1evel-was in-operable, three remaining SFRCS Channels were operable. The inoperable channel was placed in the tripped (safe) condition. The steam generator level signal is not used to detect a steam line break inside the containment vessel.
Corrective Action
Af ter cleaning and drying the connection box for level trans-mitter LT-SP09B8, Surveillance Test ST 5030.14, "SFRCS Monthly Test" and ST 5099.01, " Miscellaneous Instrument Shif t Checks" were performed. LT-SP09B8 was declared operable at 2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br /> on March 18, 1978. This re=oved the unit from Action Statement 13 of Technical Specification 3.3.2.2.
To prevent permeation of water into these transmitters, a waterproof fitting will be installed on each steam generator level transmitter which inputs to the SFRCS, per Facility Change Request 77-433. Installation of these fittings will ec=mence Failure Data: There have been no previously reportable occurrences of water leakage as the cause of transmitter inoperability.
LER #78-028 9
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| 05000346/LER-1978-002-03, /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | | | 05000346/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000346/LER-1978-003-03, /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | | | 05000346/LER-1978-003, Forwards LER 78-003/03L-0 | Forwards LER 78-003/03L-0 | | | 05000346/LER-1978-004, Forwards LER 78-004/03L-0 | Forwards LER 78-004/03L-0 | | | 05000346/LER-1978-004-03, /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | | | 05000346/LER-1978-005-03, /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | | | 05000346/LER-1978-005, Forwards LER 78-005/03L-0 | Forwards LER 78-005/03L-0 | | | 05000346/LER-1978-006-03, /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | | | 05000346/LER-1978-006, Forwards LER 78-006/03L-0 | Forwards LER 78-006/03L-0 | | | 05000346/LER-1978-007-03, /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | | | 05000346/LER-1978-007, Forwards LER 78-007/03L-0 | Forwards LER 78-007/03L-0 | | | 05000346/LER-1978-008-03, /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | | | 05000346/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000346/LER-1978-009-03, /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | | | 05000346/LER-1978-009, Forwards LER 78-009/03L-0 | Forwards LER 78-009/03L-0 | | | 05000346/LER-1978-010-03, /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | | | 05000346/LER-1978-010, Forwards LER 78-010/O3L-0 | Forwards LER 78-010/O3L-0 | | | 05000346/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000346/LER-1978-011-03, /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | | | 05000346/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000346/LER-1978-012-03, /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | | | 05000346/LER-1978-013-03, /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | | | 05000346/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000346/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000346/LER-1978-014-03, /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | | | 05000346/LER-1978-015, Forwards LER 78-015/03L-0 | Forwards LER 78-015/03L-0 | | | 05000346/LER-1978-015-03, /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | | | 05000346/LER-1978-016-03, /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | | | 05000346/LER-1978-016, Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | | | 05000346/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000346/LER-1978-017-03, /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | | | 05000346/LER-1978-018-03, /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | | | 05000346/LER-1978-018, Forwards LER 78-018/03L-0 | Forwards LER 78-018/03L-0 | | | 05000346/LER-1978-019-03, /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | | | 05000346/LER-1978-020, Forwards LER 78-020/03L-0 | Forwards LER 78-020/03L-0 | | | 05000346/LER-1978-020-03, /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | | | 05000346/LER-1978-021-03, /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | | | 05000346/LER-1978-022-03, /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | | | 05000346/LER-1978-022, Forwards LER 78-022/03L-0 | Forwards LER 78-022/03L-0 | | | 05000346/LER-1978-023-03, /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | | | 05000346/LER-1978-023, Forwards LER 78-023/03L-0 | Forwards LER 78-023/03L-0 | | | 05000346/LER-1978-024-03, /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | | | 05000346/LER-1978-025-03, /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | | | 05000346/LER-1978-025, Forwards LER 78-025/03L-0 | Forwards LER 78-025/03L-0 | | | 05000346/LER-1978-026, Forwards LER 78-026/03L-0 | Forwards LER 78-026/03L-0 | | | 05000346/LER-1978-026-03, /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | | | 05000346/LER-1978-027, Forwards LER 78-027/03L-0 | Forwards LER 78-027/03L-0 | | | 05000346/LER-1978-027-03, /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque | /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque Out | | | 05000346/LER-1978-028-03, /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | |
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