LER-1978-006, /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced |
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| 3461978006R03 - NRC Website |
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l a 121 l At 1145 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.356725e-4 months <br /> on 1/7/78. nersonnel received a computer alarri l
g o # 3 r l Feedwater Ruoture Control System Steam Cencrator to Feeduster Dif ferentici Pressure ITT7] } Trip for Channel 1.
This placed the unit in Action Statement 13 o# Tech Snec 3.3.2.2 l
I E"T1 Iwhich requires all Steam Generator to Fetdwater Differential Pressure Switches in l o is j l Modes 1. 2 and 3.
The unit entered Mode 4 to perfo-m outane maintenance at 2100 hour0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />sf l
[oliJ-Qhich renovcd the unit frort the Action Statement.of Tech Soc.c 3.3.2.2.
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The No. 2 circuit on Inntit Buffer I s i g o l lThe cause of this occurrence is component On 1/7/78, ocrsonnel reoineed Inn,it 9._, F e -i g 11-3 in C5762A had failed to the trip state.
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DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMEMTAL INFORMATION FOR LER NP-33-78-07 v
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f DATE OF EVENT:
January 7, 1978 a
a FACILITY: Davis-Besse Unit 1 1
IDENTIFICATION OF OCCURRENCE: Failure of Input Buffer 1-3 for Steam and Feedvater Rupture Control System Channel 1.
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I Conditions Prior to Occurrence: The unit was in Mode 3, with Power (MWT) = 0, i
and Load (MWE) = 0.
j Description of Occurrence: At 1145 hours0.0133 days <br />0.318 hours <br />0.00189 weeks <br />4.356725e-4 months <br /> on January 7,1978, Operations personnel received a computer alarm indicating a Steam and Feedwater Rupture Control System (SFRCS) Steam Cenerator to Feedwater Differential Pressure Trip for Channel 1.
The resulting investigation indicated a single failure in the input circuit from pressure dif ferential indication switch 2686A.
No other pressure differential j
indicating suitch.es monitoring the Steam Cenerator to Feedwater Differential 4
Pressure were'in the tripped state. This placed the unit in Action Statement 13 of Technical Specification 3.3.2,2 which requires all Steam Generator to Feedwater Differential Pressure Switches in Modes 1, 2 and 3.
Since the input was placed
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and lef t in the tripped condition since the time of the. trip, the Action Statement
" required action was fulfilled.
The unit entered Mode 4 to perform outage main-tenance at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br />, which removed the unit from the Action Statement of Tech-nical Specification 3.3.2.2.
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i Designation of Apparent Cause of Occurrence: The cause of this. occurrence is component failure. The No. 2 circuit on Input Buffer 1-3 in C5762A had failed to the trip state.
The input buffer assembly was returned to the manufacturer
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who discovered a diode had failed causing the input buf fer failure..
4 Analysis of Occurrence: There was no danger to the health 'and safety of the public or to unit personnel.
The failure of Input Buffer 1-3 in C5762A immediately put the channel in the tripped state. Redundant Steam Cenerator to Feedwater Differ-ential Pressure inputs w'ere also available.
.C$rrective Action: Cn January 7,1973, Instrument and Control personnel replaced j,
., Input Buffer 1-3 in SFRCS Channel-1. On January 10, 1978, all. functional testing (ST 5031.14) and' response time testing (ST 5031.09) was completed on the new input--
l buffer and the channel was declared operable, i Failure Data: One pievious failure has occurred on these input buffers as dis,
NP-32-77-16.
v / cussed in-Licensee Event Report 4
'LF.R 473-006 O
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| 05000346/LER-1978-002-03, /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | | | 05000346/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000346/LER-1978-003-03, /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | | | 05000346/LER-1978-003, Forwards LER 78-003/03L-0 | Forwards LER 78-003/03L-0 | | | 05000346/LER-1978-004, Forwards LER 78-004/03L-0 | Forwards LER 78-004/03L-0 | | | 05000346/LER-1978-004-03, /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | | | 05000346/LER-1978-005-03, /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | | | 05000346/LER-1978-005, Forwards LER 78-005/03L-0 | Forwards LER 78-005/03L-0 | | | 05000346/LER-1978-006-03, /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | | | 05000346/LER-1978-006, Forwards LER 78-006/03L-0 | Forwards LER 78-006/03L-0 | | | 05000346/LER-1978-007-03, /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | | | 05000346/LER-1978-007, Forwards LER 78-007/03L-0 | Forwards LER 78-007/03L-0 | | | 05000346/LER-1978-008-03, /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | | | 05000346/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000346/LER-1978-009-03, /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | | | 05000346/LER-1978-009, Forwards LER 78-009/03L-0 | Forwards LER 78-009/03L-0 | | | 05000346/LER-1978-010-03, /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | | | 05000346/LER-1978-010, Forwards LER 78-010/O3L-0 | Forwards LER 78-010/O3L-0 | | | 05000346/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000346/LER-1978-011-03, /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | | | 05000346/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000346/LER-1978-012-03, /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | | | 05000346/LER-1978-013-03, /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | | | 05000346/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000346/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000346/LER-1978-014-03, /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | | | 05000346/LER-1978-015, Forwards LER 78-015/03L-0 | Forwards LER 78-015/03L-0 | | | 05000346/LER-1978-015-03, /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | | | 05000346/LER-1978-016-03, /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | | | 05000346/LER-1978-016, Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | | | 05000346/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000346/LER-1978-017-03, /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | | | 05000346/LER-1978-018-03, /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | | | 05000346/LER-1978-018, Forwards LER 78-018/03L-0 | Forwards LER 78-018/03L-0 | | | 05000346/LER-1978-019-03, /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | | | 05000346/LER-1978-020, Forwards LER 78-020/03L-0 | Forwards LER 78-020/03L-0 | | | 05000346/LER-1978-020-03, /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | | | 05000346/LER-1978-021-03, /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | | | 05000346/LER-1978-022-03, /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | | | 05000346/LER-1978-022, Forwards LER 78-022/03L-0 | Forwards LER 78-022/03L-0 | | | 05000346/LER-1978-023-03, /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | | | 05000346/LER-1978-023, Forwards LER 78-023/03L-0 | Forwards LER 78-023/03L-0 | | | 05000346/LER-1978-024-03, /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | | | 05000346/LER-1978-025-03, /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | | | 05000346/LER-1978-025, Forwards LER 78-025/03L-0 | Forwards LER 78-025/03L-0 | | | 05000346/LER-1978-026, Forwards LER 78-026/03L-0 | Forwards LER 78-026/03L-0 | | | 05000346/LER-1978-026-03, /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | | | 05000346/LER-1978-027, Forwards LER 78-027/03L-0 | Forwards LER 78-027/03L-0 | | | 05000346/LER-1978-027-03, /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque | /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque Out | | | 05000346/LER-1978-028-03, /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | |
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