ML19323E906
| ML19323E906 | |
| Person / Time | |
|---|---|
| Site: | Quad Cities |
| Issue date: | 05/12/1980 |
| From: | Peoples D COMMONWEALTH EDISON CO. |
| To: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| Shared Package | |
| ML19323E805 | List: |
| References | |
| NUDOCS 8005270389 | |
| Download: ML19323E906 (2) | |
Text
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/yb C:mmrnwacith Edisin 3..e Or One First National Plaza. Chicago Illinois N.x C Address Reply to: Post Office Box 767
)
%gi.,
Chicago, Illinois 60690 May 12, 1980 Mr. James G. Keppler, Director Directorate of Inspection and Enforcement - Recion III U.S. Nuclear Reguliitory Commission 799 Roosevelt Road Glen Ellyn, IL 60137
Subject:
Quad Cities Units 1 and 2 Response to IE Insepction Report Nos. 50-254/80-08 and 50-265/80-01 NRC Docket Nos. 50-254265 Reference (a):
R. F. Heishman letter to C.
Reed dated April 21, 1980
Dear Mr. Keppler:
Reference (a) transmitted the report of an inspection conducted by Mr. E. Chow, J.
Hopkins, and J.
Streeter of your office on January 4, March 6-7, 9-11, 1980, of activities at the i
Quad Cities Nuclear Power Station, Units 1 and 2.
This report and App
!x A to Reference (a), Notice of Violation, indicated that one 4cem of noncompliance (deficiency) was identified during the inspection.
Pursuant to 10 CFR Part 2, Section 2.201, Attachment A contains our response to the item of noncompliance, which provides the corrective actions taken and indicates that full compliance is achieved at this time.
Please address any questions you may have concerning this matter to this office.
Very truly yours, ff Me" L
D.
L. Peoples Director of Nuclear Licensing Attachment 3728A 8 0 05 27 0M a-
p Attachment A g
NRC Docket No. 50-265 The i tem of non-compliance identified in Appendix A to the NRC letter dated April 21, 1980, is responded to in the following paragraphs.
Contrary to Technical Speci fication 6.2. A. procedure QTS 1 E0-S7, Revision 6, was not adhered to in that valve posi tion veri fication was not carried out on March 8,1980, to veri fy that test valves 2-1402-33A and 2-1402-33B were locked closed as requi red.
Corrective Action Taken and Results Achieved Drawing Change Requests were initiated for the Core Spray Piping Diagrams for both Units 1 and 2, to show the inboard locked 3/4-inch test valves as 1402-33A and 1402-338. Valve tags and valve checklists were updated to show this configuration, which is in accordance wi th QTS 150-S7 Prior to unit s tartup valves 2-1402-33A and 2-1402-33B were veri fied to be locked closed.
Outboard valves 2-1402-32A and 2-1402-32B were veri fied c1 sed. The corresponding 9
valves for Unit 1 were also verified to be in their proper positions.
Correc tive Action to Avoid Further Non-Comoliance The valve check lists for both Units 1 and 2 IPCLRT (QTS 150-S5 and QTS 150-S 7, respectively) were reviewed to assure correctness.
Procedure revisions have been submi tted, and will be implemented prior to the next IPCLRT.
Date Uhen Full Comoiiance will be Achieved Full compliance is achieved at this time.
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