ML19323A027

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Forwards IE Bulletin 80-07, BWR Jet Pump Assembly Failure. Written Response Required
ML19323A027
Person / Time
Site: FitzPatrick 
Issue date: 04/04/1980
From: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Leonard J
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
References
NUDOCS 8004110061
Download: ML19323A027 (1)


Text

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6' 9g UNITED STATES 8

NUCLEAR REGULATORY COMMISSION o

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REGION I GG1 PARK AVENUE

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KING OF PRUSSIA, PENNSYLVANIA 19406 April 4, 1980 Docket No. 50-333 Power Authority of the State of New York James A. Fitzfatrick Nuclear Power Plant ATTN:

Mr. J. D. Leonard, Jr.

Resident Manager P. O. Box 41 Lycoming, New York 13093 Gentlemen:

The enclosed IE Bulletin No. 80-07, "BWR Jet Pump Assembly Failure," is for-warded to you for action. A written response is required.

If you desire additional information regarding this matter, please contact this office.

Sincerely,

/

/

f Boyce H. Grier Director

Enclosures:

1.

IE Bulletin No. 80-07 with Attachments 2.

List of Recently Issued IE Bulletins CONTACT:

D. L. Caphton (215-337-5254) cc w/encls:

George T. Berry, Executive Director P. W. Lyon, Manager - Nuclear Operations A. Klausmann, Director, Quality Assurance M. C. Cosgrove, Quality Assurance Supervisor J. F. Davis, Chairman, Safety Review Committee C. M. Pratt, Assistant General Counsel M. Wilverding, Licensing Supervisor i

8004110o6(

SSINS No.:

6820 Accession No.:

UNITED STATES 8002280648 NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.

20555 IE Bulletin No. 80-01 Date: April 4, 1980 Page 1 of 4 BWR JET PUMP ASSEMBLY FAILURE Description of Circumstances:

On February 2, 1980, Commonwealth Edison Company (CECO) reported that a jet pump failed in Dresden Unit 3 while operating at about 67 percent of full power in a coastdown mode to a refueling shutdown.

Observed changes in plant parameters during the event indicated an individual jet pump failure had occurred.

In accordance with T.S., an orderly plant shutdown was begun to bring the unit to cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

I The plant parameter changes reported by the licensee were (1) generator l

electrical output decreased from 539 to 511 MW electrical, (2) core thermal power decreased as indicated by decreased APRM readings and steam flow tg the turbine, (3) indicated total core flow increased from 97.6 to 104.7 x 10 Ib./hr., (4)coreplatedifferentialpressuredecreasedfrom16.1to33.8 psid.,and(5)Brecirculationloopflowincreasedfrom49to54x10 gpm while A recirculation loop flow remained at 49 x 10 gpm.

These changes were readily observed by the operator in the control room and it was postulated that a jet pump had failed.

Individual jet pump readings were taken, the jet pump operability surveillance was performed, and an apparent failure of jet i

j pump No. 13 was determined.

Following vessel head removal and defueling, TV camera and visual inspections of the jet pumps and vessel annulus revealed the hold-down beam assembly of the suspect jet pump had broken across its ligament sections at the mean diameter of the bolt thread area. Failure of the beam assembly resulted in

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pump decoupling at the diffuser connection.

Subsequent insitu ultrasonic examination of all other jet pump hold-down beams, using a special UT technique developed by General Electric (GE), revealed ultrasonic indications of cracking at the same location in 6 of the remaining 19 beams examined.

Initial estimates of crack depth ranged from 6 to 20 mils.

A sketch of the typical jet pump assembly is shown in Figures 1 and 2.

On March 15-16, 1980, insitu ultrasonic jet pump hold-down beam assemblies at Qu refueling). One beam was found to contai in excess of 100 mils depth in the same 1 DUPl.ICATE DOCUMENT

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Dresden.

Entire document Previous 1y entered into system under On March 28, 1980, Boston Edison reported m ea ed crack indicationa in three (3) h p

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