ML19323A025

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Forwards IE Bulletin 80-07, BWR Jet Pump Assembly Failure. No Written Response Required
ML19323A025
Person / Time
Site: Shoreham File:Long Island Lighting Company icon.png
Issue date: 04/04/1980
From: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Wofford A
LONG ISLAND LIGHTING CO.
References
NUDOCS 8004110053
Download: ML19323A025 (1)


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NUCLEAR REGULATORY COMMISSION o

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REGION I S

631 PARK AVENUE 4, * * * = *,&,&

KING oF PRUSSIA, PENNSYLVANIA 194M Docket No. 50-322 April 4,1980 Long Island Lighting Company ATTN:

Mr. Andrew W. Wofford i

Vice President 175 East Old Country Road Hicksville, New York 11801 L

Gentlemen:

The enclosed IE Bulletin No. 80-07, " SWR Jet Pump Assembly Failure," is forwarded to you for information.

No written response is required.

If you desire additional information regarding this matter, please contact this office.

l Sincerely, AH W

Boyce H. Grier

" Director

Enclosures:

1.

IE Bulletin No. 80-07 with Attachments 2.

List of Recently Issued IE Bulletins CCNTACT:

D. L. Caphton (215-337-5254) l cc w/encls:

J. P. Novarro, Project Manager Edward M. Barrett, Esquire Edward J. Walsh, Esquire T. F. Gerecke, Manager, Engineering QA Department i

8 0 04ti o g Q

4 SSINS No.:

6820 Accession No.:

UNITED STATES 8002280648 NUCLEAR REGULATORY COMMISSION l

OFFICE OF INSPECTION AND ENFORCEMENT

~

WASHINGTON, D.C.

20555 i

IE Bulletin No. 80-07 Date: April 4, 1980 Page 1 of 4 i

BWR JET PUMP ASSEMBLY FAILURE l

Description of Circumstances:

On February 2, 1980, Commonwealth Edison Company (CECO) reported that a jet pump failed in Dresden Unit 3 while operating at about 67 percent of full power in a coastdown mode to a refueling shutdown.

Observed changes in plant parameters during the event indicated an individual jet pump failure had t

occurred.

In accordance with T.S.,

an orderly plant shutdown was begun to bring the unit to cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

i The plant parameter changes reported by the licensee were (1) generator l

electrical output decreased from 539 to 511 MW electrical, (2) core thermal i

power decreased as indicated by decreased APRM readings and steam flow tg the turbine, (3) indicated total core flow increased from 97.6 to 104.7 x 10 lb./hr., (4)coreplatedifferentialpressuredecreasedfrom16.1 tog 3.8 psid.,and(5)Brecirculationloopflowincreasedfrom49to54x10 gpm j

while A recirculation loop flow remained at 49 x 10 gpm.

These changes were readily observed by the operator in the control room and it was postulated j

that a jet pump had failed.

Individual jet pung readings were taken, the jet pump operability surveillance was performe.1, and an apparent failure of jet i

pump No. 13 was determined.

l Following vessel head removal and defueling, TV camera and visual inspections of the jet pumps and vessel annulus revealed the hold-down beam assembly of the suspect jet pump had broken across its ligament sections at the mean i

diameter of the bolt thread area. Failure of the beam assembly resulted in pump decoupling at the diffuser connection.

Subsequent insitu ultrasonic i

examination of all other jet pump hold-down beams, using a special UT technique developed by General Electric (GE), revealed ultrasonic indications of cracking at the same 2) cation in 6 of the remaining 19 beams examined.

Initial estimates of crack depth ranged from 6 to 20 mils. A sketch of the typical jet pump assembly is shown in Figures 1 and 2.

t On March 15-16, 1980, insitu ultrasonic jet pump hold-down beam assemblies at Qua i

refueling).

One beam was found to contai i

in excess of 100 mils depth in the same 1 DUPLICATE DOCUMENT

[

l Entire document Previously entered into system under.

On March 28, 1980, Boston Edison reported revealed crack indications in three (3) h p

h No.

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