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LER-1980-093, /03L-0:on 800612,during Steady State Power, HNP-2-1050 Rounds Procedure Readings Showed Drywell Average Temp High.Caused by High Ambient Temp & Inadequate Cooling. Chilled Water Flow Increased |
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During: steady-ntate' power operation. readinos beinq taken per IINP-2-1050, I
l Rounds ~ Procedure, showed the drywell average temperature to be above the m'[
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'145 degree F limit of Tech Spec 3.6.1.7.
There were no offects upon pub-l lic health or safety due to this event.
This is a repetitive occurr-l lTTsl: 1 l
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NARRATIVE
REPORT Georgia Power Company Plant E.
I. Hatch Baxicy, Georgia 31513 Reportable Occurrence Report No. 50-366/1980-093.
On June 12, 1980, during steady state power operation, readings being taken per UNP-2-1050, Rounds Procedure, indicated that the average drywell temper-ature was greater than the 145 degrees F limit of Tech Specs Section 3.6.1.7, (145 degrees F at 0177 CDT and 145.5 degrees F at 1610 CDT).
This event, high drywell temperature,-was due to both high ambient temeprature and in-sufficient drywell cooling capability.
The insufficient drywell cooling capability was due to the fact that two reactor building chillers are used to provide chilled water to not only the drywell, but also to the reactor and radwaste buildings.
Corrective action
consisted of throttling the chilled water going to the reactor and radwaste building coolers and thereby.ncreasing the amount of chilled water being supplied to the drywell coolers.
Also, water to coolers in room with chillers was throttled inadvertently causing chiller trip.
Chillers were i
then restarted.and water flow to room coolers increased.
.On July 2,1980, during steady state power operation, work had been completed on the reactor building 2A chiller, and the 2B chiller was taken out of service to run the 2A chiller for a check out as required following mainte-nance. During this swapping of the chillers, the average drywell temperature went above the 145 degree F limit (146.5 degrees F at 1235 CDT).
The temper-tature was back within limits af ter allowing A chiller to run following the 2
swap. -
On July 3,1980, during steady state power operation, the average drywell temperature was observed to be close to (but not above) the 145 degrees F limit. At this time, the A.E. and members of the site maintenance and engineering departments tried reducing total chilled water flow in an attempt'to gain better cooling by decreasing velocity of the coolers.
This attempt, however, proved to be unsuccessful and the average drywell temper-
.ature rose to 145.7 degrees F at 0020 CDT on July 4, 1980.
The flow was then returned to_ its original setting and the temperature dropped to below 145 degrees F.
On July 4,'1980, during steady state power operation, the average drywell temperature was observed to be 145.6 degrees F at 0900 CDT and 145.7 degrecs F at'1405 CDT.
AfterLthe high temperature at 0900 CDT, attempts were made to lower it by. running all'four sets of fan coil units in the drywell; however,
.this was' unsuccessful.
Shift-finally succeeded in lowering temperature by-throttling back on flow of chilled water to the reactor building (from 170 gpm.
to 130 gpm) and-running only 2 sets of the drywell fan coll' units.
Later temperature ; recorder 2T47-R626 was recalibrated and when readings.wcre taken
,at 1405 CDT the temperature was indicated as being high.
Investigation showed that' the ~ recorder had been incorrectly calibrated.
A' correct cali-
.bration of the recorder _showed-the temperature to be within the limits.
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. Narrative Foport Reportablo Occurrence' Report No. 50-366/1980-093 page 2-On July 7, '1980,"during steady stato power operation, the average drywell ~
temperature was observed to be 145.7 degrecs F at 1752 CDT. This high temperature was due to high. ambient temperature and it dropped back within specs as the-temperature outside; dropped.
J Onl July 8,1980, during steady stato power operation, the average drywell temperature was' observed to be 145.96 degrees F at 0845 CDT.
At that time, both of the reactor building chillers were placed into service and were paralleled.
This action corrected the temperature problem, but at 1900 CDT, the A chiller tripped and the temperature went from 140 to 147.1 degrees F.
The chiller was restarted and the temperature dropped back within specs.
~
At present both reactor chillers are being run in parallel and the temper-ature is being maintained below the 145, degrees F limit of Tech Spec 3.6.1.7.
I Future.correctivo action is to consist of adding additional water chillors.
The new chillers are to be used to handle the reactor building and radwaste bulla..ng leads and the present chillers are - to be used for the drywell only.
l Completion of the chiller addition is expected prior to Cycle II operations.
There were no effects upon public health or safety due to this event.
This is.a repetitive occurrence, see LER 50-366/1980-086.
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| 05000321/LER-1980-001-01, /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | | | 05000366/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000366/LER-1980-001-03, /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | | | 05000321/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000321/LER-1980-002-03, /03L-0:on 800112,while Performing HNP-1-3655,fan lT46-C001B Would Not Meet Flow Requirements Per Tech Specs. Ten Days Later,While Venting Drywell Per HNP-1-1500,flow Did Not Meet Tech Specs.Equipment Recalibr | /03L-0:on 800112,while Performing HNP-1-3655,fan lT46-C001B Would Not Meet Flow Requirements Per Tech Specs. Ten Days Later,While Venting Drywell Per HNP-1-1500,flow Did Not Meet Tech Specs.Equipment Recalibr | | | 05000321/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000366/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000366/LER-1980-002-01, /01T-0:on 800128,during Cold Shutdown,Ae Notified Util That Single Mode Failure Existed for Torus Gravity Fill Isolation Valve 2G51-F013.Caused by Design Deficiency. Standing Order Issued | /01T-0:on 800128,during Cold Shutdown,Ae Notified Util That Single Mode Failure Existed for Torus Gravity Fill Isolation Valve 2G51-F013.Caused by Design Deficiency. Standing Order Issued | | | 05000366/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000366/LER-1980-003-03, /03L-0:on 800117,while Applying Equalizing Charge to 125/250-volt Dc Station Svc Batteries,Hpci Automatic Flow Control Power Inverter Tripped.Caused by Instrument Drift. Instrument Recalibr Satisfactorily | /03L-0:on 800117,while Applying Equalizing Charge to 125/250-volt Dc Station Svc Batteries,Hpci Automatic Flow Control Power Inverter Tripped.Caused by Instrument Drift. Instrument Recalibr Satisfactorily | | | 05000321/LER-1980-003-03, While Performing RHR Valve Operability Procedure,Outboard Shutdown Cooling Isolation Valve F008 Opened in 25.8-S.Caused by Normal Wear & Human Reaction Time.Valve Operator Adjusted | While Performing RHR Valve Operability Procedure,Outboard Shutdown Cooling Isolation Valve F008 Opened in 25.8-S.Caused by Normal Wear & Human Reaction Time.Valve Operator Adjusted | | | 05000321/LER-1980-003, Forwards Revised LER 80-003/03X-1 | Forwards Revised LER 80-003/03X-1 | | | 05000321/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000321/LER-1980-004-03, /03L-0:on 800106,during Startup Mode,Main Steam Line Inboard Isolation Drain Valve Failed in mid-position. Caused by Failure of Valve Motor Winding.Motor Replaced & Valve Returned to Operable Status | /03L-0:on 800106,during Startup Mode,Main Steam Line Inboard Isolation Drain Valve Failed in mid-position. Caused by Failure of Valve Motor Winding.Motor Replaced & Valve Returned to Operable Status | | | 05000366/LER-1980-004-03, /03L-0:on 800118,during Steady State Power Operation Hydrogen Recombiner Inlet Valve 2T49-F003A Did Not Open.Caused by a Failed Torque Switch.Sys Returned to Operation After Switch Was Replaced | /03L-0:on 800118,during Steady State Power Operation Hydrogen Recombiner Inlet Valve 2T49-F003A Did Not Open.Caused by a Failed Torque Switch.Sys Returned to Operation After Switch Was Replaced | | | 05000366/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000321/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000321/LER-1980-005-03, /03L-0:on 800109,w/reactor Mode Switch in Run Mode,Discovered That Surveillance Procedure HNP-1-3007, Turbine Control Valve Fast Closure,Was Not Performed in Grace Period.Caused by Personnel Error | /03L-0:on 800109,w/reactor Mode Switch in Run Mode,Discovered That Surveillance Procedure HNP-1-3007, Turbine Control Valve Fast Closure,Was Not Performed in Grace Period.Caused by Personnel Error | | | 05000366/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000366/LER-1980-005-03, /03L-0:on 800119,during Power Operation,Tech Specs 4.8.1.1.1.a & 4.8.1.1.2a4 for Electrical Power Sources Were Not Performed within 1-h.Caused by Personnel Misinterpretation of Tech Spec Requirements | /03L-0:on 800119,during Power Operation,Tech Specs 4.8.1.1.1.a & 4.8.1.1.2a4 for Electrical Power Sources Were Not Performed within 1-h.Caused by Personnel Misinterpretation of Tech Spec Requirements | | | 05000321/LER-1980-006-03, /03L-0:on 800113,one Standby Gas Treatment Sys Rendered Inoperable W/Both Units in Power Operation.Unit Not Proven Operable within Required 4-h.Caused by Inability to Prove Filter Train Operable within 4-h | /03L-0:on 800113,one Standby Gas Treatment Sys Rendered Inoperable W/Both Units in Power Operation.Unit Not Proven Operable within Required 4-h.Caused by Inability to Prove Filter Train Operable within 4-h | | | 05000321/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000321/LER-1980-007-03, /03L-0:on 800114,while Testing Standby Svc Water Pump,Pump Would Not Meet Criteria.Caused by Disengagement of Pump First Stage Impeller Lock Collet.Lock Collet Replaced & Pump Reinstalled | /03L-0:on 800114,while Testing Standby Svc Water Pump,Pump Would Not Meet Criteria.Caused by Disengagement of Pump First Stage Impeller Lock Collet.Lock Collet Replaced & Pump Reinstalled | | | 05000321/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000366/LER-1980-007-01, /01T-0:on 800130,while Performing High Drywell Pressure Instrument (Reactor Protection Sys) Functional Test & Calibr,Instruments 2C71-N002A,B & D Exceeded Tech Specs.Caused by Instrument Drift | /01T-0:on 800130,while Performing High Drywell Pressure Instrument (Reactor Protection Sys) Functional Test & Calibr,Instruments 2C71-N002A,B & D Exceeded Tech Specs.Caused by Instrument Drift | | | 05000366/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000366/LER-1980-008-03, While Increasing Reactor Power by Rod Withdrawal,Operator Noticed Rod Select Matrix Backlighted & Rod Sequence Control Sys Not Initiating Rod Blocks Properly.Caused by Design Change | While Increasing Reactor Power by Rod Withdrawal,Operator Noticed Rod Select Matrix Backlighted & Rod Sequence Control Sys Not Initiating Rod Blocks Properly.Caused by Design Change | | | 05000366/LER-1980-008, Forwards LER 80-008/03L-1 | Forwards LER 80-008/03L-1 | | | 05000321/LER-1980-008-03, /03L-0:on 800115,during Steady State Power Operation,Secondary Containment Integrity Violated When Personnel Opened 164-ft Elevation Reactor Bldg & Turbine Bldg Airlock Doors Simultaneously.Procedure Revised | /03L-0:on 800115,during Steady State Power Operation,Secondary Containment Integrity Violated When Personnel Opened 164-ft Elevation Reactor Bldg & Turbine Bldg Airlock Doors Simultaneously.Procedure Revised | | | 05000321/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000366/LER-1980-009-03, /03L-0:on 800130,while Performing Procedure HNP-2-33-3,HPCI Min Flow Valve 2E41-F012 Failed to Close. Caused by Sticking Switch Contacts on Flow Switch 2E41-N006. Switch Contacts Cleaned & Procedure HNP-2-3303 Performed | /03L-0:on 800130,while Performing Procedure HNP-2-33-3,HPCI Min Flow Valve 2E41-F012 Failed to Close. Caused by Sticking Switch Contacts on Flow Switch 2E41-N006. Switch Contacts Cleaned & Procedure HNP-2-3303 Performed | | | 05000321/LER-1980-009-03, /03L-0:on 800118,during Normal Operation,Drywell/ Torus Temp Recorder 1T47-R611 Found Stamping Erratically, Making Drywall & Torus Air Temps & Water Temp Difficult to Ascertain.Caused by Failure of Microswitch.Switch Replace | /03L-0:on 800118,during Normal Operation,Drywell/ Torus Temp Recorder 1T47-R611 Found Stamping Erratically, Making Drywall & Torus Air Temps & Water Temp Difficult to Ascertain.Caused by Failure of Microswitch.Switch Replaced | | | 05000366/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000321/LER-1980-010-03, /03L-0:on 800118,during Normal Operation While Performing Standby Liquid Control Pump Operability Test & Relief Valve Test,Pump a Discharge Relief Valve 1C41-F029A Operated at 1,225 Psig.Caused by Setpoint Drift.Valve Reset | /03L-0:on 800118,during Normal Operation While Performing Standby Liquid Control Pump Operability Test & Relief Valve Test,Pump a Discharge Relief Valve 1C41-F029A Operated at 1,225 Psig.Caused by Setpoint Drift.Valve Reset | | | 05000321/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000366/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000366/LER-1980-010-03, /03L-0:on 800131,during Reactor Startup,At 58% Power,Max Total Peaking Factor Was Calculated at 3.0 Compared to Design Value of 2.38.Caused by Lower than Normal Xenon Distribution During Startup | /03L-0:on 800131,during Reactor Startup,At 58% Power,Max Total Peaking Factor Was Calculated at 3.0 Compared to Design Value of 2.38.Caused by Lower than Normal Xenon Distribution During Startup | | | 05000321/LER-1980-011-03, /03L-0:on 800120,while at Steady State Power, torus-to-drywell Differential Pressure recorder,LT48-R631B Had Low Reading.Cause Not Stated | /03L-0:on 800120,while at Steady State Power, torus-to-drywell Differential Pressure recorder,LT48-R631B Had Low Reading.Cause Not Stated | | | 05000366/LER-1980-011-03, /03L-0:on 800202,while Performing Reactor Core Isolation Cooling Shutdown Flow Test,Power Inverter for Remote Flow Control Loop Found to Be Tripped.Caused by Defective Input Filter Capacitors | /03L-0:on 800202,while Performing Reactor Core Isolation Cooling Shutdown Flow Test,Power Inverter for Remote Flow Control Loop Found to Be Tripped.Caused by Defective Input Filter Capacitors | | | 05000321/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000366/LER-1980-012-03, /03L-0:on 800214,while at Full Power,Rhr & Plant Svc Water Min Flow Line Found to Be Inadequately Supported. Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | /03L-0:on 800214,while at Full Power,Rhr & Plant Svc Water Min Flow Line Found to Be Inadequately Supported. Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | | | 05000321/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000366/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000321/LER-1980-012-03, /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | | | 05000321/LER-1980-013, Forwards Updated LER 80-013/03X-1 | Forwards Updated LER 80-013/03X-1 | | | 05000321/LER-1980-013-03, Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | | | 05000366/LER-1980-013-03, /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | | | 05000366/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000366/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000366/LER-1980-014-03, /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | |
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