ML19320C438

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Forwards IE Circular 80-14, Radioactive Contamination of Plant Demineralized Water Sys & Resultant Internal Contamination of Personnel. No Written Response Required
ML19320C438
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 06/24/1980
From: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Daltroff S
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
References
NUDOCS 8007160836
Download: ML19320C438 (1)


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$31 PARK AVENUE Kina or Paussia. PENNSYLVANi A 19404 Docket Nos. 50-277 50-278 Philadelphia Electric Company ATTN: Mr. S. L. Daltroff Vice President Electric Production 2301 Market Street Philadelphia, Pennsylvania 19101 Gentlemen:

The enclosed IE Circular No. 80-14, " Radioactive Contamination of Plant Demin-eralized Water System and Resultant Internal Contamination of Personnel," is forwarded to you for information.

No written response is required.

If you desire additional information regarding this matter, please contact this office.

Sincerely, y e H. Grier Director

Enclosures:

1.

IE Circular No. 80-14 2.

List of Recently Issued IE Circulars CONTACT:

P. J. Knapp (215-337-5291) l cc w/encls:

W. T. Ullrich, Station Superintendent Troy B. Conner, Jr., Esquire Eugene J. Bradley, Esquire j

Ra niond L. Hovis, Esquire Mi hael J. Scibinico, II, Assistant Attorney General 8007160#36

ENCLOSURE 1 SSINS.: 6830 UNITED STATES Accession No.:

NUCLEAR REGULATORY COMMISSION 2505 g n

0FFICE OF INSPECTION AND ENFORCEMENT I

i WASHINGTON, D. C.

20555 oo

.2J IE Circular No. 80-14 Date:

June 24, 1980 Page 1 of 2 RADIOACTIVE CONTAMINATION OF PLANT DEMINERALIZED WATER SYSTEM AND RESULTANT i

INTERNAL CONTAMINATION OF PERSONNEL This circular describes an event which occurred at a nuclear power facility; the generic im I

however,le facilities. plications may be applicable to research reactors, and fuel cyc On March 17, 1980, a licensee informed the NRC resident ins)ector that portions of the plant demineralized water (DW) system were found to )e radioactively contaminated.

A temporary hose used to add demineralized water to the spent fuel pool was the pathway for the cross-contamination.

After this fuel pool makeus was completed on March 14, the temporary DW line (still connected to the Dd header) was inadvertently left submerged in the fuel pool.

Since the DW header pressure at the point of supply was relatively low (a DW booster pump had been secured), a siphoning action occurred, resulting in radioactive contamination of portions of the DW header.

On March 17, 1980, while performi'ng routine secondary system chemical analyses, the licensee discovered that the demineralized water tap in_

containedhighlevelsofboronandhadactivityof1.5x10}hechemistrylab uCi/ml (mainly Cs-134,Cs-137,Co-58,Co-60andMn-54).

It was subsequently discovered that demineralized water from the chemistry laboratory supply tap had been used to make five (5)(pots of coffee.23) individuals who had consumed this coffee were The remaining coffee was confiscated and the l

twenty-three counted.

All involved individuals showed no intake greater than an equivalent 0.01 MPC-HRS. Analysis performed by the licensee's radiation consultant, based on the maximum concentration of radioactivity found in the coffee, indicated i

that the resultant 50 year dose commitment to an individi.a1 drinking eight ounces of this coffee would be less than 1 millirem.

Further-licensee investigation revealed that the non-radiological chemistry DW supply tap was the only DW sup 1 point outside the Auxiliary Building controlled area.

This DW supp tap was tagged prohibiting human consumption to prevent a similar event in e future.

It is recommended that you review your facilities use of demineralized water (DW) via temporary connections and give attention to the following:

1.

Provisions should be made to assure that radioactive materials are not inadvertently introduced into use of temporary connections. your facility's DW system via the improper A temporary cross connection between contaminated systems and the DW system without adequate physical controls to pr6 vent cross-contamination should-be prohibited.

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IE Circular No. 80-14 June 24, 1980 Page 2 of 2 2.

In addition to some physical means of preventing backflow into the DW system, appropriate administrative controls should be established to ensure that the DW supply valve is secured and temporary hosing is disconnected from the DW supply header after use.

3.

Use of plant-supplied DW for human consumption should be prohibited.

The potable water system should be the only authorized source of water for human consumption.

4.

Examine potable and demineralized water systems to determine if pathways exist allowing or having the potential to allow contamination of these systems including temporary connections whereby siphons could cause situations described above.

No written response to this Circular is reguired.

Your review of this matter to determine its applicability to your facility and any corrective and preven-tive actions taken or planned, as appropriate will be reviewed during a subsequent NRC inspection.

If you desire additional information regarding this matter, contact the Director of the appropriate NRC Regional Office.

i

IE Circular No. 80-14 June 24, 1980 PECENTLY ISSUED IE CIRCULARS Circular Subject Date of Issued to No.

Issue 80-13 Grid Strap Damage in 5/28/80 All holders of a Westinghouse Fuel Assemblies Power Reactor Operating License (OL) or Construction Permit (CP) 80-12 Valve-Shaft-To-Actuator Key 5/14/80 All holders of a May Fall Out of Place When Power Reactor Mounted Below Horizontal Axis OL or CP 80-11 Emergerycy Diesel Generator 5/13/80 All holders of a Power Lube 011 Cooler Failures Reactor OL or CP 80-10 Failure to Maintain 4/29/80 All holders of a Environmental Qualification Power Reactor of Equipment OL or CP 80-09 Problems With Plant Internal 4/28/80 All holders of a Power Communications Systems Reactor OL or CP 80-08 BWR Technical Specification 4/18/80 All holders of a Power Inconsistency - RPS Response Reactor OL for a General Time Electric BWR 80-07 Problu; with HPCI Turbine 4/3/80 All holders of a Power Oil System Reactor OL or CP 80-06 Control and Accountability 4/14/80 Medical licensees in Systems for Implant Therapy Categories G and G1 Sources 80-05 Emergency Diesel-Generator 4/1/80 All holders of a Power Lubricating Oil Addition and Reactor OL or CP Onsite Supply 80-04 Securing of Threaded Locking 3/14/80 All holders of a Power Devices on Safety-Related Reactor OL or CP Equipment 80-03 Protection from Toxic Gas 3/6/80 All holders of a Hazards Power Reactor OL 80-02 Nuclear Power Plant Staff 2/1/80 All holders of a Work Hours Raactor OL, including research and test reactors, or CP

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