05000346/LER-1978-065-03, /03L-0:on 780607,six Containment Isolation Check Valves Found Inoperable During Local Leak Rate Test.Caused by Improper Seating of Valves Due to Dirt or Wear.Discs & Seats Cleaned,Valves Lapped & Valves Retested

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/03L-0:on 780607,six Containment Isolation Check Valves Found Inoperable During Local Leak Rate Test.Caused by Improper Seating of Valves Due to Dirt or Wear.Discs & Seats Cleaned,Valves Lapped & Valves Retested
ML19319C007
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 07/05/1978
From: David Brown, Cedoz R
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19319C006 List:
References
LER-78-065-03L, LER-78-65-3L, NUDOCS 8001290732
Download: ML19319C007 (3)


LER-1978-065, /03L-0:on 780607,six Containment Isolation Check Valves Found Inoperable During Local Leak Rate Test.Caused by Improper Seating of Valves Due to Dirt or Wear.Discs & Seats Cleaned,Valves Lapped & Valves Retested
Event date:
Report date:
3461978065R03 - NRC Website

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DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION

~M SUPPLEMENTAL INFORMATION FOR LER NP-33-78-79 DATE OF EVENT: June 7, 1978 through June 11, 1978 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Six Containment Isolation Check Valves were found inoperable by the Local Leak Rate Test.

Conditions Prior to Occurrence:

The unit was in Mode 6, with Power (MWT) = 0, and Load (MRE) = 0.

Description of Occurrence:

On June 7, 1978 through June 11, 1978, the Containment Isolation Check Valves listed below were found inoperable during the perfor=ance of the " Containment Local Leak Rate Test", ST 5061.02:

1.

Containment Vessel Air Sample Isolation Check Valve, CV125 2.

Hydrogen Dilution System 1-1 Containment Isolation Check Valve, CV210 3.

Hydrogen Dilution System 1-2 Containment Isolation Check Valve, CV209

<s 4.

Instrument Air System Containment Isolation Check Valve, IA501 5.

Station Air System Containment Isolation Check Valve, SA502 g

N-6.

100 PSI Nitrogen Header Containment Isolation Check Valve, NN58 The check valve leakage in each case was determined to be in excess of the local leak rate test requirements.

The unit was in Mode 6 and thus did not enter the Action Statement of Technical Specification 3.6.3.1, which requires the containment isolation "al ras to be operable in Modes 1, 2, 3 and 4.

These incidents are being repot : (d ac component failures.

Designation of Acoarent Cause of Occurrence:

The cause of these inoperabilities was component failure. Some of the check valve internals contained particles of dirt which prevented proper seating of the valves while performing the local leak rate test.

The valves also had indications of wear and pitting which prevented proper seat.ng.

Analvsis of Occurrence: There was no danger to the hea2th and safety of the public or unit personnel.

Containment isolation was maintained by existing redundant isolation valves in series with the valves that were found inoperable.

The redundant isolation valves were tested per the Local Leak Rate Test and de-termined to be satisfactory.

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) LER #78-065 V

TOLEDO EDISON COMPANY DAVIS-BESSE CTIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORE\\ TION FOR LER NP-33-78-79 PAGE 2

Corrective Action

The discs and seats of valves IA501, SA502 and Cv125 were cleaned of dirt and all the valves were lapped per Maintenance Work Orders 78-1354 (IA501),

78-1358 (CV125), 78-1359 (,Cv210), 78-1360 (CV209), 78-1362 (NN58), and 78-1379 (SA502). The valves were retested per the Local Leak Rate Test, ST 5061.02 on June 9, 1978 through June 18, 1978. All of the valves passed the test and were declared operable. The Toledo Edison Power Engineering and Construction Depart-ment is presently evaluating the application of these check valves.

Failure Data: There have been no previous similar occurrences.

LER #78-065 s

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