LER-1978-065, /03L-0:on 780607,six Containment Isolation Check Valves Found Inoperable During Local Leak Rate Test.Caused by Improper Seating of Valves Due to Dirt or Wear.Discs & Seats Cleaned,Valves Lapped & Valves Retested |
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4 EVENT CESCRIPT!CN AND PACBA8LE CONSECUENCES h isolation check valves were found inoperable ;
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The check valve
- during the perfor=ance of the Contain=ent Local Leak Rate
- g;3; go;,,,l leakage in each case was deter =f.ned to be in excess of the local leak race test re-There was no danger to the health and safety of the public or unit per-io,3; ; quire =ents.
isolation was maintained by existing redundant isolation valves I o is j i sonnel. Containment (NF-33-78-79)
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The valves were success-l Iii21 Ivalves were cleaned of dirt and all the valves were lacoed.
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TOLEDO EDISON COMPANY
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DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION
~M SUPPLEMENTAL INFORMATION FOR LER NP-33-78-79 DATE OF EVENT: June 7, 1978 through June 11, 1978 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Six Containment Isolation Check Valves were found inoperable by the Local Leak Rate Test.
Conditions Prior to Occurrence:
The unit was in Mode 6, with Power (MWT) = 0, and Load (MRE) = 0.
Description of Occurrence:
On June 7, 1978 through June 11, 1978, the Containment Isolation Check Valves listed below were found inoperable during the perfor=ance of the " Containment Local Leak Rate Test", ST 5061.02:
1.
Containment Vessel Air Sample Isolation Check Valve, CV125 2.
Hydrogen Dilution System 1-1 Containment Isolation Check Valve, CV210 3.
Hydrogen Dilution System 1-2 Containment Isolation Check Valve, CV209
<s 4.
Instrument Air System Containment Isolation Check Valve, IA501 5.
Station Air System Containment Isolation Check Valve, SA502 g
N-6.
100 PSI Nitrogen Header Containment Isolation Check Valve, NN58 The check valve leakage in each case was determined to be in excess of the local leak rate test requirements.
The unit was in Mode 6 and thus did not enter the Action Statement of Technical Specification 3.6.3.1, which requires the containment isolation "al ras to be operable in Modes 1, 2, 3 and 4.
These incidents are being repot : (d ac component failures.
Designation of Acoarent Cause of Occurrence:
The cause of these inoperabilities was component failure. Some of the check valve internals contained particles of dirt which prevented proper seating of the valves while performing the local leak rate test.
The valves also had indications of wear and pitting which prevented proper seat.ng.
Analvsis of Occurrence: There was no danger to the hea2th and safety of the public or unit personnel.
Containment isolation was maintained by existing redundant isolation valves in series with the valves that were found inoperable.
The redundant isolation valves were tested per the Local Leak Rate Test and de-termined to be satisfactory.
[
) LER #78-065 V
TOLEDO EDISON COMPANY DAVIS-BESSE CTIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORE\\ TION FOR LER NP-33-78-79 PAGE 2
Corrective Action
The discs and seats of valves IA501, SA502 and Cv125 were cleaned of dirt and all the valves were lapped per Maintenance Work Orders 78-1354 (IA501),
78-1358 (CV125), 78-1359 (,Cv210), 78-1360 (CV209), 78-1362 (NN58), and 78-1379 (SA502). The valves were retested per the Local Leak Rate Test, ST 5061.02 on June 9, 1978 through June 18, 1978. All of the valves passed the test and were declared operable. The Toledo Edison Power Engineering and Construction Depart-ment is presently evaluating the application of these check valves.
Failure Data: There have been no previous similar occurrences.
LER #78-065 s
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| 05000346/LER-1978-002-03, /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | /03L-0:on 780103,control Rod Group 5 Rod 12 Absolute Position Indication Declared Inoperable.Caused by Component Failure of Absolute Position Indicator Reed Switch.Switch Replaced | | | 05000346/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000346/LER-1978-003-03, /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | /03L-0:on 780103,unidentified RCS Leakage Greater than 1,66 Gallon Per Minute.Caused by Loose Packing on Valve DH2735.Valve Repacked & Stroked | | | 05000346/LER-1978-003, Forwards LER 78-003/03L-0 | Forwards LER 78-003/03L-0 | | | 05000346/LER-1978-004, Forwards LER 78-004/03L-0 | Forwards LER 78-004/03L-0 | | | 05000346/LER-1978-004-03, /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | /03L-0:on 780105,inlet Balancing Dampers to Emergency Ventilation Sys Fans 1-1 & 1-2 Found Closed.Cause Unknown.Dampers Returned to Balance Position & Locknut Tightened | | | 05000346/LER-1978-005-03, /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | /03L-0:on 780106,auxiliary Feed Pump Turbine 1-1 Speed Control Lost & Declared Inoperable.Caused by Short Circuits & Blown Fuses Due to Design Deficiency.Higher Current Rated Relays Installed & Circuit Modified | | | 05000346/LER-1978-005, Forwards LER 78-005/03L-0 | Forwards LER 78-005/03L-0 | | | 05000346/LER-1978-006-03, /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | /03L-0:on 780107,computer Alarm Indicated That Steam & Feedwater Rupture Control Sys Steam Generator to Feedwater Differential Pressure Channel 1 Had Tripped.Caused by Component Failure.Input Buffer 1-3 in Channel 1 Replaced | | | 05000346/LER-1978-006, Forwards LER 78-006/03L-0 | Forwards LER 78-006/03L-0 | | | 05000346/LER-1978-007-03, /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | /03L-0:on 780109,during Monthly Surveillance Test ST 5081.01,diesel Generator 1-1 Tripped on High Crankcase Pressure.Caused by Dirty Crankcase Vent Oil Collector.Vent Oil Collector Disassembled & Cleaned | | | 05000346/LER-1978-007, Forwards LER 78-007/03L-0 | Forwards LER 78-007/03L-0 | | | 05000346/LER-1978-008-03, /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | /03L-0:on 780112,both Containment Spray Pumps Found Inoperable.Caused by Personnel Error.Spray Pump Circuit Breakers re-energized | | | 05000346/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000346/LER-1978-009-03, /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | /03L-0:on 780112,component Cooling Water Heat Exchanger 1-1 Outlet Isolation Valve SW 1424 Declared Inoperable.Caused by Component Failure.Solenoid Valve in Control Scheme Found Burned Out.Unit Removed | | | 05000346/LER-1978-009, Forwards LER 78-009/03L-0 | Forwards LER 78-009/03L-0 | | | 05000346/LER-1978-010-03, /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | /03L-0:on 780115, Reactor Coolant Pump Monitor on Channel 1 Found Out of Tolerance & Reactor Protection Sys Declared Inoperable.Caused by Defective Module.New Module Calibr & Installed | | | 05000346/LER-1978-010, Forwards LER 78-010/O3L-0 | Forwards LER 78-010/O3L-0 | | | 05000346/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000346/LER-1978-011-03, /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | /03L-0:on 780116,during Surveillance Test,Decay Heat Pump 1-1 Failed to Start.Caused by Fuses in Breaker for Decay Heat Motor Failing to Make Proper Contact.Control Power Fuese Pulled & Reinserted.Pump Returned to Svc | | | 05000346/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000346/LER-1978-012-03, /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | /03L-0:on 780124,personnel Airlock Failed Leak Rate Test.Caused by Loose Shaft Seal Due to Routine Use of Personnel & Escape Lock (Exit/Entry to Containment).Shaft Seals Tightened to Prevent Excessive Leakage | | | 05000346/LER-1978-013-03, /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | /03L-0:780119,Cell 32 in Station Battery 1N Electrolyte Specific Gravity Decreased 0.003 Greater than Allowed by Tech Spec 3.8.2.3.Caused by Electrolyte Stratification Due to Low Battery Loading | | | 05000346/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000346/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000346/LER-1978-014-03, /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | /03L-0:on 780123,quandrant Power Tilt in Excess of Steady State & Transient Limits Indicated by Unit Process Computer.Caused by Detector Inadvertently Left Off Scan After Testing.Test Procedure Being Modified | | | 05000346/LER-1978-015, Forwards LER 78-015/03L-0 | Forwards LER 78-015/03L-0 | | | 05000346/LER-1978-015-03, /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | /03L-0:on 780131,feedwater Steam Generator 1 Channel 2 Pressure Differential Switch Did Not Actuate at Desired Setpoint During Surveillance Test.Caused by Pressure Differential Switch Out of Tolerance | | | 05000346/LER-1978-016-03, /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | /03L-1:on 780202,absolute Position Indicator for Group 5,Rod 12,declared Inoperable.Caused by Component Failure in Penetration Area.Containment Conductors Connected to Spare Penetration Connector | | | 05000346/LER-1978-016, Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | Forwards LER 78-016/03L-1,LER 78-021/03L-1,LER 78-100/03L-1, LER 78-034-03L-1 & LER 78-024/03L-1 | | | 05000346/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000346/LER-1978-017-03, /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | /03L-0:on 780126,all Meteorological Channels Became Inoperable During Blizzard.Caused by Instrumentation Power Loss Due to Tripped Breaker at Meteorological Tower. Breaker Reset on 780128 | | | 05000346/LER-1978-018-03, /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | /03L-0:on 780208,diesel Generator 1-1 Making Unusual Noises During Monthly Test.Unusual Noise Traced to Turbocharger.Exact Cause Undetermined.Turbocharger Replaced & Diesel Generator Monthly Test Completed | | | 05000346/LER-1978-018, Forwards LER 78-018/03L-0 | Forwards LER 78-018/03L-0 | | | 05000346/LER-1978-019-03, /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | /03L-1:on 780210,decay Heat Cooler Outlet Valve DH14A & DH14B Mechanical Stops Found Incorrectly Opened. Caused by Personnel Incorrectly Resetting Stops After Previous Work Completion.Stops Tagged & Records Marked | | | 05000346/LER-1978-020, Forwards LER 78-020/03L-0 | Forwards LER 78-020/03L-0 | | | 05000346/LER-1978-020-03, /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | /03L-0:on 780210,reactor Protection Sys Channel 3 Hot Leg Temp String TI-RC3B4 Declared Inoperable.Caused by Loose Wire Connection.Loose Terminal at Temp Element Tightened,Rendering TI-RC3B4 Operable | | | 05000346/LER-1978-021-03, /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | /03L-1:on 780220,absolute Position Indicator for Control Rod 12 of Group 5 Declared Inoperable.Caused by Component Failure in Penetration Area.Conductors Connected W/Spare Penetration Connectors | | | 05000346/LER-1978-022-03, /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | /03L-0:on 780223,flow Transmitter FTRC1A3 Found Inoperable.Caused by Defective Flow Transmitter Amplifier. Amplifier Replaced & Flow Transmitter FTRC1A3 Returned to Svc on 780226 | | | 05000346/LER-1978-022, Forwards LER 78-022/03L-0 | Forwards LER 78-022/03L-0 | | | 05000346/LER-1978-023-03, /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | /03L-0:on 780224,temp Indication for Reactor Protection Sys Channel 2 Spiked Tripping Channel & Shut Down Reactor.Caused by Faulty Connector Due to Dirt on Contacts. Channel 2 Temp String Modules Removed & Connectors Cleaned | | | 05000346/LER-1978-023, Forwards LER 78-023/03L-0 | Forwards LER 78-023/03L-0 | | | 05000346/LER-1978-024-03, /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | /03L-1:on 780228,MSIV MS-101 Rendered Inoperable to Allow Maint Personnel to Remove Raised Metal on Two of Four Spring Guide Tubes.Cause of Raised Metal Unknown.Metal Filed Down,Valve Closing Time Adjusted & Valve Tested | | | 05000346/LER-1978-025-03, /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | /03L-0:on 780304,RCS Leakage Found Greater than 1 Gallon Per Minute.Leakage Cause Undetermined.Leakages Processed Through Normal Containment Sump.Unidentified RCS Leakage Reduced Below 1 Gallon Per Minute in 5.5-h | | | 05000346/LER-1978-025, Forwards LER 78-025/03L-0 | Forwards LER 78-025/03L-0 | | | 05000346/LER-1978-026, Forwards LER 78-026/03L-0 | Forwards LER 78-026/03L-0 | | | 05000346/LER-1978-026-03, /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | /03L-0:on 780309,radiation Monitor Re 5029 Found Inoperable Due to Low Sample flow.12 Previous Radiation Monitor Inoperabilities Not Reported.Caused by Pump Motor Bearing Seizure Due to High Ambient Temp | | | 05000346/LER-1978-027, Forwards LER 78-027/03L-0 | Forwards LER 78-027/03L-0 | | | 05000346/LER-1978-027-03, /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque | /03L-0:on 780316,stop Valve AF3870 Failed to Open During Testing.Caused by High Differential Pressure Due to Check Valve AF39 & AF72 Leakage.Motor Operator Initially Not Adjusted for This Pressure,Causing Operator to Torque Out | | | 05000346/LER-1978-028-03, /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | /03L-0:on 780318,channel 1 Steam Generator 1-1 Declared Inoperable.Caused by Water in Level Transmitter SP09B8 Connecting Box Due to Steam Leak.Connection Box Cleaned & Dried.Waterproof Fitting Will Be Installed | |
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