05000366/LER-1980-088-03, /03L-0:on 800529,while Performing HNP-2-3154, Reactor Pressure Vessel Level Instrument (LPCI) Ft&C, Switch 2 on 2B21-NO31A Failed.Caused by Switch Being Out of Adjustment Due to Loose Screw.Switch Readjusted

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/03L-0:on 800529,while Performing HNP-2-3154, Reactor Pressure Vessel Level Instrument (LPCI) Ft&C, Switch 2 on 2B21-NO31A Failed.Caused by Switch Being Out of Adjustment Due to Loose Screw.Switch Readjusted
ML19318A972
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 06/19/1980
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19318A963 List:
References
LER-80-088-03L, LER-80-88-3L, NUDOCS 8006240455
Download: ML19318A972 (2)


LER-1980-088, /03L-0:on 800529,while Performing HNP-2-3154, Reactor Pressure Vessel Level Instrument (LPCI) Ft&C, Switch 2 on 2B21-NO31A Failed.Caused by Switch Being Out of Adjustment Due to Loose Screw.Switch Readjusted
Event date:
Report date:
3661980088R03 - NRC Website

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8 LO G1 DOCKET NUYBER 68 69 EVENT DATE 14 7S REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Ol2ll With the reactor in the run mode and while performing IINP-2-3154, RPV Level l

,; j a ; l Instrument (LPCI) FT6C, switch no. 2 on 2B21-N031A failed to operate. There l

o l4 l l were no probable consequences and no effect on safe plant operation because l

O 15 I l Redundant Switch 2B21-N031C was operabic. This is a repetitive event as l

o 16 l l last reported on Reportable Occurrence Report No. 50-366/1980-087. The l

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' Georgia Power Company Plant ::. I.. llatch Baxicy, Georgia.31513 l

Reportabic Occurrence Report No. 50-366/1980-088.

With the reactor in the run mode and while performing IINP-2-315'4, RPV Level

~ Instrument (LPCI) FT&C, switch no. 2 on 2B21-N031A failed to operate. There were no probable consequences and no ef fect on safe plant operation because redundant cwitch 2B21-N031C was operabic.

This is a repetitive event as last reported on Reportable Occurrence Report No. 50-366/1980-87. The health and safety of the public was not affected.

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The cause for the switch f ailing to operate was due to the switch being out of adjustment. The screw holding the mechanical arm on the switch plate was slightly. loose causing the switch to drif t out of adjustment. The switch was recalibrated and surveillance was performed with satisfactory results.

All screws holding mechanical arms on switch plates were checked to ensure they were tight.

Surveillance on Unit I instruments had been performed earlier

= with satisfactory results. Calibration procedures for both units were revised I

to verify that all screws were tight before returning instruments to service.

All Yarways on both units were inspected to ensure no other problems existed.

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