05000366/LER-1980-054-03, /03L-0:on 800524,while Performing Calibr of Both Primary Containment Purge Vacuum Breaker Pressure Switches, 2T48-N211 Found Inoperable.Caused by Personnel Error.Stuck Switch Removed & Repaired.Switch Wiring Corrected

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/03L-0:on 800524,while Performing Calibr of Both Primary Containment Purge Vacuum Breaker Pressure Switches, 2T48-N211 Found Inoperable.Caused by Personnel Error.Stuck Switch Removed & Repaired.Switch Wiring Corrected
ML19318A959
Person / Time
Site: Hatch 
Issue date: 06/17/1980
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19318A956 List:
References
LER-80-054-03L, LER-80-54-3L, NUDOCS 8006240436
Download: ML19318A959 (2)


LER-1980-054, /03L-0:on 800524,while Performing Calibr of Both Primary Containment Purge Vacuum Breaker Pressure Switches, 2T48-N211 Found Inoperable.Caused by Personnel Error.Stuck Switch Removed & Repaired.Switch Wiring Corrected
Event date:
Report date:
3661980054R03 - NRC Website

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EVENT DATE 74 7b REPORT DATE 80 EVENT DESCRIPTION AND PROBAOLE CONSEQUENCES h o 2 l With the mode switch in run while perforninn calibration of both Primarv l

l o l31 l Containment Purge Vacuum Breaker Pressure Switches, 2T48-N211 was found l

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inoperable.

The remaining instrument, 2T48-N210, was operable.

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o s I was no ef fect upon public health and safety, nor was safe plant operation i

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affected.

This is a repetitive event as last reported on Reportable i

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Occurrence Report No. 50-366/1978-016.

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40 41 42 43 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIC,NS 27 lilo] l The cause of the occurrence was personnel error.

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NARRATIVE

REPORT Ceorgia Power Company-Plant E. I. Hatch Baxicy, Georgia 31513 e

Reportabic Occurrence Report No. 50-366/1980-054.

I On May 24, 1980, with the mode switch in run, while performing calibration on both Primary Containment Purge Vacuum Breaker Pressure Switches, 2T48-N211 was found inoperable. The remaining instrument, 2T48-N210, was operabic.

Both instruments are Static-0-Ring Pressure Switches.

There were no ef fects upon public health and safety, nor was safe plant operation affccted. :This is a repetitive event as last reported on Reportable Occurrence Report No. 50-366/1978-016.

l The cause of the occurrence was personnel error.

The initial diagnosis was a stuck switch.

It was removed and repaired. After installation it was determined that the switch was wired incorrectly. The wiring was corrected,

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the switch successfully retested and returned to service.

A review of all previous Maintenance Requests revealed no generic problems.

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