ML19317F225
| ML19317F225 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 04/11/1975 |
| From: | DUKE POWER CO. |
| To: | |
| Shared Package | |
| ML19317F221 | List: |
| References | |
| NUDOCS 8001080935 | |
| Download: ML19317F225 (1) | |
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DUKE POWER COMPANY
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OCONEE UNIT 3
(-II *T Report No.:
A0-287/75-6 Report Date: April 11, 1975 Occurrence Date: March 27, 1975 Facility: Oconee Unit 3, Seneca, South Carolina Identification of Occurrence:
Inadvertent isolation of Keowee underground feeder Conditions Prior to Occurrence:
Power operation Description of Occurrence:
on March 27, 1975, the Keowee Emergency Start Test was performed from the Oconee Unit 3 control room. The test is performed by isolating the Keowee overhead transmission line from the 230 kv switchyard, inhibiting one Keowee unit, and starting the remaining Keowee unit with the emergency start circuits. The first portion of the test, with Unit 2 inhibited, satis-factor 11y resulted in Keowee Unit 1 charging the underground feeder.
When the inhibit was removed from Keowee Unit 2 and Unit 1 was inhibited, ACB3 (breaker from Unit 1 to underground feeder) opened resulting in both Keowee units being isolated from the underground feeder and overhead transmission j
lines for a period of five minutes.
Designation of Apparent Cause of Occurrencel The apparent cause of this occurrence was a deficiency in the procedure in that it did not caution that a Keowee unit inhibit results in the opening of the associated breaker to the underground feeder.
The Test Cecrdinator performing the test did not realize the existence of this interlock.
I Analysis of Occurrence:
The Keowee Hydro Station supplies emergency power to the Oconee Nuclear Station through the underground feeder in the event of a system blackout and the loss of the Oconee units. This incident resulted in the Keowee Hydro Station being separated from Oconee for a period of five minutes.
Should emergency power have been required, ACB-4 could have been closed by j
operator action to connect Keowee Unit 2 to the underground feeder.
It is j
concluded that the health and safety of the public was not affected by l
this incident.
Corrective Action:
The Keowee Emergency Start Test procedure has been changed to assure that either ACB3 or ACB4 is closed at all times during the test.
This will result in one Keowee unit being connected to the underground feeder circuit at all times.
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NRC DILNjfp 'lON FOR PART SO DOCKET MATERIAL
- TEMPORARY FORM)
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CONTROL NO:
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FILE: INCIDEITT REPORT FII.Z FROM: Duke Power-Company DATE OF DOC D ATE R E O LTR TWX RPT OTHER Charlotte, N.C.
4-11-75 4-16-75 XXX ORIG CC OTHER SENT AEC PDR XXX TO'.
XXX Norman C. Moseley 1 Signed SENT LOCAL PDR CLASS UNCLASS PROPINFO INPUT NO CYS REC'D DOCKET NO:
XXX 1
50-287 ENCLOSURES:
DESCRIPTION:
Letter trans the following,.....
Abnorm. Occurr. # 75-6, on 3-27-75, concern-ing Inadvertent isolation of Keowee under-ground feeder....
( 1 cy. Encl. rec'd)
Oconee #3 PLANT NAME:
FOR ACTION /INFORMATION vcn 4_17 75 BUTLER (L)
SCHWENCER (L) ZIEMANN (L)
REGAN (E)
W/ Ccpie:
W/ Copies W/ Copies W/ Copies CLARK (L)
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DICKER (E)
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VASSAL.LO (L)
KNIGHTON (E)
SPE l.S W/ Copies W/ Copies W/ Copies W/ Copies KNIEL (L)
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'Y'OUNGtstOOD (E)
W/ Copics W/3 Copies W/ Copies W/ Copies INTERNAL DISTRIBUTION BEG F TECH REVIEW DENTON LIC ASST A/T IND.
jNRC PDR pSCHROEDER yGRIMES R. DIGGS (L)
BRAITMAN OGC, ROOM P 506A MACCARY GAMMILL H. GEARIN (L)
SALTZMAN GOSSICK/ STAFF KNIGH' KASTNER E. GOULBOURNE (L)
MELTZ CASE PAWL Al BALLARD P. KREUTZER (E)
GIAMBUSSO SHAO SPANG LER J. LEE (L)
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MCDONALD S. REED (E)
CHAPMAN MOORE (L)
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DUBE (Ltr)
DEYOUNG (L)
,NOVAK MULLER S
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SKOVHOLT (L)
ROSS DICKER GOLLER (L) (Ltr) lPPOLITO KNIGHTON M. SLATER (E)
PETERSON P. CO LLINS TEDESCO YOUNG BLOOD H. SMITH (L)
HARTFIELD (2) f DENISE LONG REGAN S. TEETS (L)
KLECKER R E G O P R_
LAINAS PROJECT LDR G. WILLI AMS (E)
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WIGGINTON f "IPC/PE (3)
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DUKE POWER COMPANY PowzR Buscrwo 4aa SouTu CHURcu SrazzT, CuAaroTTE, N. C. asaci A. C. THICS P. o. Box as7e StmaOm Vict PettiOENT PWODUCfiON ANO TRANSedeSSION April 11, 1975
..s.
f Mr. Norman C. Moseley, Director ~
U. S. Nuclear Regulatory Coramission Suite 818 230 Peachtree Street, Northwest Atlanta, Georgia 30303 Re:
Oconce Unit 3 Docket No. 50-287
Dear Mr. Moseley:
Pursuant to Sections 6.2 and 6.6.2 of the Oconee Nuclear Station
~ Technical Specifications, please find attached Abnormal Occurrence Report A0-287/75-6%
1 Very truly yours, S
l A. C. Thies ACT:vr Attachment cc:
Mr. Angelo Giambusso W
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- N DUKE POWER COMPANY OCONEE UNIT 3 Report No.:
A0-287/75-6 Report Date: April 11, 1975 Occurrence Date:
March 27, 1975 Facility: Oconee Unit 3, Seneca, South Carolina
. Identification of Occurrence:
Inadvertent isolation of Keowee underground feeder Conditions Prior to Occurrence: Power operation Description of Occurrence:
On March 27, 1975, the Keowee Emergency Start Test was performed from the Oconee Unit 3 control room. The test is performed by isolating the Keowee overhead trcnsmission line from the 230 kv switchyard, inhibiting one Keowee unit,-and starting the remaining Keowee unit with the emergency start circuits. The first portion of the test, with Unit 2 inhibited, satis-factorily resulted in Keowee Unit 1 charging the underground feeder.
When the inhibit was removed from Keowee Unit 2 and Unit 1 was inhibited, ACB3 (breaker from Unit 1 to underground feeder) opened resulting in both Keowee units being isolated from~the underground feeder and overhead transmission lines for a period of five minutes.
Designation of Apparent Cause of Occurrence:
The apparent cause of this occurrence was a deficiency in the procedure in that it did ncc caution that a Keowee unit inhibit results in the opening of the associated breaker to the underground feeder.
The Test Coordinator performing the test did not realize the existence of this interlock.
Analysis of Occurrence:
The Keovee Hydro Station supplies emergency power to the Oconee Nuclear Station through the underground feeder in the event of a system blackout and the loss of the Oconee units. This incident resulted in the Keowee Hydro Station being separated from Oconee for a period of five minutes.
Should emergency power have been required, ACB-4 could have been closed by operator action to connect Keowee Unit 2 to the underground feeder.
It is concluded that the health and safety of the public was not affected by this incident.
Corrective Action:
The Keowee Emergency Start Test. procedure has been changed.co assure that either ACB3 or ACB4 is closed at all times during the test.
This will result in one Keowee unit being connected to the underground feeder circuit at all times.