ML19312C813
| ML19312C813 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 03/23/1978 |
| From: | Parker W DUKE POWER CO. |
| To: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| References | |
| NUDOCS 8001100723 | |
| Download: ML19312C813 (2) | |
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LYSTEM tRIDS) s INF0FMATICN DISTPIEUTION 50-26'.2gj. 7 FE0liLATORY DI I.TRIE.UTION FOR INC0NING MATERIAL DOCDATE- 03/23/7?
ORG: PARPER W 0 DATE RCVD: 03/23/79
?. ' OREILLY J P DUKE PWR L.R C COPIES RECEIVED C T'r PE: LETTER NOTARIZED: NO LTR 1 EflCL 1 ON 02/22/78 CONCERNING ATTEMPT TO BvECT:
(R0 50-269/78-003) SOURCE OF AUXILIARY PWR FOR SUGJECT FACIL CENSEE EVENT REPT N
PRT FE0 WEE H'fDF0 UNIT 2, BREAKER.
W/ATT LER 78-003,
)ILIED DUE TO AN INOFERABLE FIELD FLASHING
>-029 6 7G-001.
REVIEWER INITIAL:
XJN 1
DISTRIBUTER INITIAL; LANT NAME: OCONEE - UNIT OCONEE - UNIT 2 OCONEE - UNIT 3 IS AS FOLLOWS **************4,*++
DISTRIBUTION OF THIS MATERIAL o**+44***********
CUNNINGHAM - ALL AMENDMENTS TO FSAR AND CHANG 10TES:
M.
INCIDENT REPORTS tDI3TRIEUTIGN CODE A002) 4 ENCL BR CHIEF PCT +
FOR ACTION:
7 NRC PDR**W/ ENCL nEG FILE 4*W/ ENC MIPC**W/3 ENCL INTERNAL:
--b-E* +W a
-E-HOUSTON **W/ ENCL SCHROEDER/IPPOLIT0**W/ ENCL GRIMES **W/ ENCL NOVAK/ CHECK **W/ ENCL BUTLER **W/ ENCL KNIGHT **W/ ENCL TEDESCO**W/ ENCL HANAUER**W/ ENCL BAER**W/ ENCL EISENHUT**W/ ENCL VOLLMER/ BUNCH **W/ ENCL SHAG **W/ ENCL ROSA **W/ ENCL KREGER/J. COLLINS **W/ ENCL K SEYFRIT/IE**W/ ENCL LPDR'S EXTERNAL:
WALHALLA. SC+4W/ ENCL TIC **W/ ENCL 3 gyr SU39.ITTED PER NSIC+*W/ ENCL GUI.ATORY GUIDE 10.1 ACRS CAT B**W/16 ENCL 6
NN r"om LTR 45 ENCL 45 lDISTRIEUTION:
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- +**++***********************G 1
THE END soo1 a 0 o723 o.ok,
DUKE POWI.N COSUMNY Pow en Di it :u o Sotr a C u r uc a S r n t.c r. C naut.oT T E. N C,,2e e w,
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.J Mr. James P. O'Reilly, Director U. S. Nuclear Regulatory Commission Suite 1217 230 Peachtree Street, Northwest Atlanta, Georgia 30303 RE: Oconee Units 1, 2, and 3 Docket No. 50-269, -270, and -237
Dear Mr. O'Reilly:
Pursuant to Sections 6.2 and 6.6.2 of the Oconee Nuclear Station Technical Specifications, please find attached Reportable Occurrence Report R0-269/78-3.
Also attached are revised Licensee Event Reports submitted on two similar occurrences reported in Reportable Occurrence Reports RC-269/B-29 and R0-269/78-1, originally transmitted by my letters of January IS, and February 3,1978, respectively.
Ver/trulyyours,
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'Jilliam O. Parker Jr./t w i;
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DL*KE PC'iER CC"PANY l
OCONEE UNIT '
Report Number:
R0-269/78-3 i
Report Date:
P. arch 23, 1978 Occurrence Date:
February 22, 1978 Facility: Oconee Nuclear Station, Seneca, South Carolina i
Identification of Occurrence:
Keovee Hydro Unit 2, Field Flashing 3reaker Inoperable i
l Conditions Prior to Occurrence: Unit 1 1007. FP l
Unit 2 1007. FP i
Unit 3 1007.,FP Description of Occurrence:
I At 1750, on February 22, 1978, when an attempt was made to start Keowee Hydro Unit 2, the unit's field flashing breaker failed to close.
The unit was there-f are inoperable, contrary to the requirements of Oconee Nuclear Station Techni-cal Specification 3.7.1.
The unit was started and successrully operated at i
i 1752.
The breaker and controls, wires and contacts within the breaker were in-spected with no abnormalities discovered.
The unit has successfully started on several subsequent occasions.
i d
This type of incident has occurred on two previous occasions, which were reported in Reportable Occurrence Reports R0-269/77-29, and R0 269/73-1, transmitted by my letters of January 18, and February 3, 1978 respectively.
l Apparent Cause of Occurrence:
The apparent cause of the incident was. initially identified as a faulty relay 1
within the field flashing breaker control syste=.
The apparently faulty relay was replaced, along with another relay that had been arcing.
After relay re-placement, and during the investigation of this report, the breaker failed to 4
operate again.
Therefore, the exact cause of the breaker =alfunction has not yet been determined.
The breaker system is continuing to be observed to deter-mine the cause of the incident.
J Analysis of Occurrence:
The failure of the breaker to close caused Keowee Unit 2 to become temporarily i
Two minutes after the initial unsuccessful attempt, the field flashing breaker successfully operated making Keowee Unit 2 fully operable.
Throughout this period, the second Keowee Hydro unit was fully operable and available to supply emergency power to the station if required.
The health and i
safety of the public were not endangered.
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. Corrective Action 1
3 Initially an inspection of the breaker and its controls was made with no j
def ective components disco.ered.
During the investigation of this report two relays in the field flashing bre.aker control circuit were replaced.
An extensive investigation is i
continuing in this area of concern to correct the breaker control system faults.
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[TTil 1 At 1750 on February 22, 1978, during normal operation, Oconee attempted to La 2] 1 start cowee Hydro Unit 2 which is a source of auxillary power for the Oconee ;
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During subsequent investigations the 3,i;31 breaker failed on three other occasions.
Faulty relays were at first suspect; t,,,jt but the third failure occurred after two relays were replaced.
The apparent
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EV F.NT OE SC AIPTICN ANO **3C'5 A 4L1 CONS ECUENCES h to 121 Louring normal operation Keowee avdro Unit 2 failed to start on initiation i
[21211from Oconee control room.
Since Keovee 2 is a source of auxiliary power l
Iol41ifor the Oconee station (Units 1, 2, and 3) this is reportable under I
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ti!ali The Field Flashing Breaker on the generator failed to close on first attempt.,
,,,,,,The breaker was verified as operable by subsequent operation and visual g,,;,texamination.
Nor.al inspection and servicing resulted in no further correc-ti!3l [ tive action.
Extensive investigation is continuing as of March 23, 1978.
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s loIjl_DuringnormaloperationKeowceH@ydroUnit EvtNr :tscmencN ANo eacsants ccNstoutNcts 2 failed to start on initiation l
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Since Keowee 2 is a source of auxiliary power I 3 L. j l for the Oconee station (Units 1, 2, and 3) this is reportable under 2is l T. S. 6.6.2.1.b.(2).
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li)o]1 The Field Flashing 3reaker (DB-26) on the generator failed to close on first i
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The breaker was verified as operable by subsequent operation and
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Inspection and servicing resulted in no further correc 3 tive action.
Extensive investigation is continuing as of March 23, 1973.
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