|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M3371999-10-20020 October 1999 Forwards Notice of Docketing of License SNM-2506 Amend Application.Notice Has Been Forwarded to Ofc of Fr for Publication ML20217M1111999-10-19019 October 1999 Forwards Insp Repts 50-282/99-14 & 50-306/99-14 on 990920- 22.One Violation Noted & Being Treated as Ncv.Insp Focused on Testing & Maint of Heat Exchangers in High Risk Sys ML20217F4331999-10-15015 October 1999 Forwards Rev 39 to Security Plan.Changes Do Not Decrease Effectiveness of Security Plan.Rev Withheld,Per 10CFR73.21 ML20217C2351999-10-0606 October 1999 Forwards Insp Repts 50-282/99-12 & 50-306/99-12 on 990823-0917.No Violations Noted.Insp Consisted of Selected Exam of Procedures & Representative Records,Observation of Activities & Interviews with Personnel ML20212J8811999-09-28028 September 1999 Forwards Preliminary Accident Sequence Precurson Analysis of Operational Event That Occurred at Plant,Unit 1 on 990105, for Review & Comment.Comment Requested within 30 Days of Receipt of Ltr IR 05000272/19990071999-09-28028 September 1999 Forwards Insp Repts 50-272/99-07 & 50-306/99-07 on 990721- 0831.One Potentially Safety Significant Issue Identified Dealing with Control Room Special Ventilation System.Four Addl Issues of Low Safety Significance Identified ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212G9801999-09-23023 September 1999 Refers to Resolution of Unresolved Items Identified Re Security Alarm Station Operations at Both Monitcello & Prairie Island ML20212F5121999-09-20020 September 1999 Forwards Response to NRC , Preparation & Scheduling of Operator Licensing Examinations ML20212D8401999-09-16016 September 1999 Discusses 990902 Telcon Between D Wesphal & R Bailey Re Administeration of Retake Exam at Prairie Island During Wk of 991206.NRC May Make Exam Validation Visit to Facility During Wk of 991116 ML20217H2331999-09-10010 September 1999 Forwards Security Insp Repts 50-282/99-10 & 50-306/99-10 on 990809-12.Two Findings,Each of Low Risk Significance Identified & Being Treated as non-cited Violations Consistent with App C of Enforcement Policy ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20212A9241999-09-0909 September 1999 Discusses Plans Made During 990902 Telephone Conversation to Inspect Licensed Operator Requalification Program at Prairie Island During Weeks of 991101 & 991108.Requests That Written Exams & Operating Tests Be Submitted by 991022 ML20212B0511999-09-0909 September 1999 Forwards Insp Repts 50-282/99-11 & 50-306/99-11 on 990816-20.One Issue of Low Safety Significance Was Identified & Being Treated as Ncb ML20211Q7641999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Plant Operator License Applicants During Wk of 000515,in Response to D Westphal ML20211N8631999-09-0707 September 1999 Withdraws 970814 Request for Exemption from 10CFR50,App R, Section III.G.2, Fire Protection of Safe Shutdown Capabilities ML20211K5911999-09-0101 September 1999 Informs That Util Reviewed Rvid Data Base,As Requested in NRC .Summary of Proposed Changes & Observed Differences Are Included in Encl Tables ML20211L0211999-09-0101 September 1999 Provides Notification That License Amends 141 & 132 & Associated License Conditions 6 & 7 Have Been Fully Implemented ML20211K5931999-08-31031 August 1999 Forwards License Amend Request for License SNM-2506, Proposing Change to License Conditions 6,7 & 8 & TSs App a of License by Permitting Inclusion of Bpras & Thimble Plug Devices in Sf Assemblies Stored in TN-40 Casks ML20211Q6041999-08-31031 August 1999 Forwards Rev 19 to USAR for Pingp,Per 10CFR50.71(e).Rev Brings USAR up-to-date as of 990228,though Some Info Is More Recent.Attachment 1 Contains Descriptions & Summaries of SE for Changes,Tests & Experiments,Per 10CFR50.59 ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211D3541999-08-24024 August 1999 Discusses GL 95-07 Re Pressure Locking & Thermal Binding of safety-related Power Operated Gate Valves.Forwards SE Re Response to GL 95-07 ML20211C7601999-08-19019 August 1999 Confirms NRC Intent to Meet with NSP & Ceco on 990807 in Lisle,Il to Discuss with Region III Pilot Plants,Any Observations,Feedback,Lessons Learned & Recommendations Relative to Implementation of Pilot Program ML20211B8311999-08-19019 August 1999 Forwards Request for Relief 8 Re Limited Exams Associated with Unit 1 Third ten-year Interval Inservice Insp Program. Licensee Requests Relief Due to Impractibility of Obtaining 100% Exam Coverage for Affected Items ML20211B5711999-08-19019 August 1999 Forwards Second 90-day Rept for Implementation of Voltage Based Repair Criteria at Prairie Island Unit 1.Rept Fulfills Requirements of Section 6.b of Attachment 1 to GL 95-05 ML20211C2311999-08-19019 August 1999 Forwards Unit 1 ISI Summary Rept,Interval 3,Period 2 Refueling Outage Dates 990425-0526,Cycle 19 971212-990526. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarizes Results ML20211B0561999-08-18018 August 1999 Provides Addl Info on Proposed Rev to Main Steam Line Break Methodology ,in Response to NRC Staff Request Made in 990416 Telcon.Nuclear Svcs Corp Rept PIO-01-06, Analysis Rept Structural Analyses of Main Steam Check... Encl ML20211B2621999-08-17017 August 1999 Forwards Insp Repts 50-282/99-09 & 50-306/99-09 on 990719-22.No Violations Noted.Insp Included Review & Evaluation of Current Emergency Preparedness Performance Indicators ML20211C7371999-08-17017 August 1999 Discusses Closure of Staff Review Re Generic Implication of Part Length Control Rod Drive Mechanism Housing Leak on 980123.Enclosed NRC 980811 & 1223 Ltrs Responded to WOG Positions Re Corrective Actions ML20210T5661999-08-12012 August 1999 Forwards RAI Re & Suppl ,which Requested Exemptions from TSs of Section III.G.2 of 10CFR50 App R,To Extent That Specifies Separation of Certain Redundant Safe Shutdown Circuits with fire-related Barriers ML20210R7021999-08-12012 August 1999 Forwards Insp Repts 50-282/99-06 & 50-306/99-06 on 990601- 0720.One NCV Occurred,Consistent with App C of Enforcement Policy ML20210P5191999-08-11011 August 1999 Discusses GL 92-01,Rev 1,Supp 1, Rv Integrity, Issued by NRC on 950519 & NSP Responses for PINGP & 951117. Staff Reviewed Info in Rvid & Released Info as Rvid Version 2.Requests Submittal of Comments Re Revised Rvid by 990901 ML20210G5061999-07-30030 July 1999 Responds to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates 05000282/LER-1999-007, Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics1999-07-23023 July 1999 Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics ML20210J4991999-07-22022 July 1999 Forwards Rev 18 to USAR for Pingp,Bringing USAR up-to-date as of 990228,though Some Info More Recent.Safety Evaluation Summaries Also Encl ML20209J0941999-07-15015 July 1999 Forwards SER Finding Rev 7 to Topical Rept NSPNAD-8102, Reload Safety Evaluation Methods for Application to PI Units, Acceptable for Ref in Plant Licensing Actions ML20209H8051999-07-14014 July 1999 Forwards Summary of non-modification Safety Evaluation Number 515 Re Storage of Fuel Inserts,Per Insp Rept 72-0010/99-201 ML20209D4181999-07-0707 July 1999 Informs That Util Has Changed Listed TS Bases Pages Attached for NRC Use.Util Made No New Commitments in Ltr ML20209H8361999-07-0202 July 1999 Forwards Operator Licensing Exam Repts 50-282/99-301(OL) & 50-306/99-301(OL) for Tests Administered During Week of 990517-21.Two Applicants Passed All Sections of Exam & Issued Reactor Operator Licenses to Operate Pings ML20196J9681999-07-0101 July 1999 Informs That in Sept 1998,Region III Received Rev 20 to Portions of Util Emergency Plan Under 10CFR50.54(q).Based on Determination That Changes Do Not Decrease Effectiveness of Licensee Emergency Plan,No NRC Approval Required ML20209C3951999-07-0101 July 1999 Forwards Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20209B7541999-07-0101 July 1999 Final Response to GL 98-01,Suppl 1 Re Y2K Readiness of Computer Sys.Sys Remediated as Required for Plant Operation. Contingency Plans Developed to Mitigate Impact of Y2K-induced Events at Key Rollover Dates ML20196J8941999-06-30030 June 1999 Transmits Util Comments on Draft Regulatory Guide DG-1074, Steam Generator Tube Integrity. Licensee Recommends That NRC Focus on Several Important Listed Areas Considered Principal Concerns & Contentions ML20209F0391999-06-30030 June 1999 Forwards Insp Repts 50-282/99-04 & 50-306/99-04 on 990407-0531.Violation Noted.Notice of Violation or Civil Penalty Will Not Be Issued,Based on NRC Listed Decision to Exercise Discretion ML20209C3011999-06-29029 June 1999 Forwards Annual Rept of Corrections to NSP ECCS Evaluation Models,Iaw 10CFR50.46.Since All Analyses Remain in Compliance,No Reanalysis Is Required or Planned ML20209B5751999-06-24024 June 1999 Submits Revised Relief Request for Limited Examinations Associated with Third 10-yr ISI Examination Plan.Attached Is Unit 1 Relief Request 7,rev 1 Which Addresses Limited Examinations ML20196F3871999-06-23023 June 1999 Forwards Revised Pages 71,72 & 298 of Rev 7 to NSPNAD-8102, Prairie Island Nuclear Power Plant Reload Safety Evaluation Methods for Application to PI Units, Per Discussions with Nrc.Approved Version of Rept Will Be Issued 05000282/LER-1999-006, Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics1999-06-18018 June 1999 Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics ML20196D5501999-06-18018 June 1999 Forwards Individual Exam Results for Licensee Applicants Who Took May 1999 Initial License Exam.In Accordance with 10CFR2.790,info Considered, Proprietary. Without Encls ML20196A6741999-06-17017 June 1999 Refers to 990517-20 Meeting with Util in Welch,Minnesota Re Licensee Initiatives in Risk Area & to Establish Dialog Between SRAs & Licensee PRA Staff 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217F4331999-10-15015 October 1999 Forwards Rev 39 to Security Plan.Changes Do Not Decrease Effectiveness of Security Plan.Rev Withheld,Per 10CFR73.21 ML20212G7171999-09-24024 September 1999 Submits Semiannual Status Update on Project Plans for USAR Review Project & Conversion to Its.Conversion Package Submittal Continues to Be Targeted for Aug of 2000 ML20212F5121999-09-20020 September 1999 Forwards Response to NRC , Preparation & Scheduling of Operator Licensing Examinations ML20211N8631999-09-0707 September 1999 Withdraws 970814 Request for Exemption from 10CFR50,App R, Section III.G.2, Fire Protection of Safe Shutdown Capabilities ML20211K5911999-09-0101 September 1999 Informs That Util Reviewed Rvid Data Base,As Requested in NRC .Summary of Proposed Changes & Observed Differences Are Included in Encl Tables ML20211L0211999-09-0101 September 1999 Provides Notification That License Amends 141 & 132 & Associated License Conditions 6 & 7 Have Been Fully Implemented ML20211Q6041999-08-31031 August 1999 Forwards Rev 19 to USAR for Pingp,Per 10CFR50.71(e).Rev Brings USAR up-to-date as of 990228,though Some Info Is More Recent.Attachment 1 Contains Descriptions & Summaries of SE for Changes,Tests & Experiments,Per 10CFR50.59 ML20211K5931999-08-31031 August 1999 Forwards License Amend Request for License SNM-2506, Proposing Change to License Conditions 6,7 & 8 & TSs App a of License by Permitting Inclusion of Bpras & Thimble Plug Devices in Sf Assemblies Stored in TN-40 Casks ML20211K2591999-08-27027 August 1999 Forwards NSP Co Fitness for Duty Program Performance Data for Six Month Period Ending 990630 ML20211C2311999-08-19019 August 1999 Forwards Unit 1 ISI Summary Rept,Interval 3,Period 2 Refueling Outage Dates 990425-0526,Cycle 19 971212-990526. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarizes Results ML20211B8311999-08-19019 August 1999 Forwards Request for Relief 8 Re Limited Exams Associated with Unit 1 Third ten-year Interval Inservice Insp Program. Licensee Requests Relief Due to Impractibility of Obtaining 100% Exam Coverage for Affected Items ML20211B5711999-08-19019 August 1999 Forwards Second 90-day Rept for Implementation of Voltage Based Repair Criteria at Prairie Island Unit 1.Rept Fulfills Requirements of Section 6.b of Attachment 1 to GL 95-05 ML20211B0561999-08-18018 August 1999 Provides Addl Info on Proposed Rev to Main Steam Line Break Methodology ,in Response to NRC Staff Request Made in 990416 Telcon.Nuclear Svcs Corp Rept PIO-01-06, Analysis Rept Structural Analyses of Main Steam Check... Encl ML20210G5061999-07-30030 July 1999 Responds to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates 05000282/LER-1999-007, Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics1999-07-23023 July 1999 Forwards LER 99-007-00,re Loss of CR Special Ventilation Function.One New Commitment Was Made in Rept as Indicated in Corrective Action Section Statement in Bold Italics ML20210J4991999-07-22022 July 1999 Forwards Rev 18 to USAR for Pingp,Bringing USAR up-to-date as of 990228,though Some Info More Recent.Safety Evaluation Summaries Also Encl ML20209H8051999-07-14014 July 1999 Forwards Summary of non-modification Safety Evaluation Number 515 Re Storage of Fuel Inserts,Per Insp Rept 72-0010/99-201 ML20209D4181999-07-0707 July 1999 Informs That Util Has Changed Listed TS Bases Pages Attached for NRC Use.Util Made No New Commitments in Ltr ML20209C3951999-07-0101 July 1999 Forwards Supplemental Response to GL 95-07, Pressure Locking & Thermal Binding of SR Power-Operated Gate Valves ML20209B7541999-07-0101 July 1999 Final Response to GL 98-01,Suppl 1 Re Y2K Readiness of Computer Sys.Sys Remediated as Required for Plant Operation. Contingency Plans Developed to Mitigate Impact of Y2K-induced Events at Key Rollover Dates ML20196J8941999-06-30030 June 1999 Transmits Util Comments on Draft Regulatory Guide DG-1074, Steam Generator Tube Integrity. Licensee Recommends That NRC Focus on Several Important Listed Areas Considered Principal Concerns & Contentions ML20209C3011999-06-29029 June 1999 Forwards Annual Rept of Corrections to NSP ECCS Evaluation Models,Iaw 10CFR50.46.Since All Analyses Remain in Compliance,No Reanalysis Is Required or Planned ML20209B5751999-06-24024 June 1999 Submits Revised Relief Request for Limited Examinations Associated with Third 10-yr ISI Examination Plan.Attached Is Unit 1 Relief Request 7,rev 1 Which Addresses Limited Examinations ML20196F3871999-06-23023 June 1999 Forwards Revised Pages 71,72 & 298 of Rev 7 to NSPNAD-8102, Prairie Island Nuclear Power Plant Reload Safety Evaluation Methods for Application to PI Units, Per Discussions with Nrc.Approved Version of Rept Will Be Issued 05000282/LER-1999-006, Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics1999-06-18018 June 1999 Forwards LER 99-006-00 Re Discovery That Manual SI Actuation Switch Had Not Been Tested on Staggered Basis During Integrated SI Test.Two New Commitments Are Indicated in Corrective Action Section Statement in Bold Italics ML20195G4281999-06-0909 June 1999 Notifies That Amsac/Dss Mods Completed & TS 138/129 Has Been Fully Implemented 05000282/LER-1999-005, Forwards LER 99-005-00 Re Containment Inservice Purge Sys Not Isolated During Heavy Load Movement Over Fuel.Event Has Indicated That Level of Performance Expected by Mgt Has Not Yet Been Achieved1999-06-0707 June 1999 Forwards LER 99-005-00 Re Containment Inservice Purge Sys Not Isolated During Heavy Load Movement Over Fuel.Event Has Indicated That Level of Performance Expected by Mgt Has Not Yet Been Achieved ML20207F4301999-06-0101 June 1999 Forwards 1999 Unit 1 SG Insp Results,Per TS 4.12.E.1. Following Insp 84 Tubes Were Plugged for First Time ML20196L2461999-05-21021 May 1999 Forwards Rev 0 to COLR for Pingp,Unit 1 Cycle 20, IAW TS Section 6.7.A.6 ML20195C6861999-05-21021 May 1999 Forwards Rev 17 to USAR for Prairie Island Nuclear Generating Plant.Attachment 1 Contains Descriptions & Summaries of SEs for Changes,Tests & Experiments Made Under Provisions of 10CFR50.59 During Period Since Last Update ML20206U6781999-05-17017 May 1999 Forwards Revised Emergency Response Plan Implementing Procedures,Including Rev 15 to F3-3,rev 15 to F3-16,rev 14 to F3-22 & Table of Contents ML20206U7131999-05-17017 May 1999 Forwards Revised EOF Emergency Plan Implementing Procedures, Including Table of Contents & Rev 2 to F8-10, Record Keeping in Eof. with Updating Instructions ML20206T2461999-05-17017 May 1999 Forwards Off-Site Radiation Dose Assessment for Jan-Dec 1998, Rev 0 to Annual Radiactive Effluent Rept for 980105- 990103 & Effluent & Waste Disposal Annual Rept Solid Waste & Irradiated Fuel Shipments,Jan-Dec 1998 ML20206R0401999-05-13013 May 1999 Forwards Application for Amends to Licenses DPR-42 & DPR-60, Removing Plant Organization Requirement,Imposed in Amend 141/132 That Plant Manager,Who Has Responsibility for Overall Safe Operation of Plant,Report to Corporate Officer ML20206Q0871999-05-13013 May 1999 Forwards Result of Evaluation Re Ultrasonic Exams of SG Number 22 Performed in Accordance with ASME Boiler & Pressure Vessel Code Section Xi.Procedure Used for Evaluation Contained in WCAP-14166,submitted for Review ML20206F9381999-05-0303 May 1999 Forwards Response to NRC 990304 RAI Re GL 96-05 Program at Pingp.Licensee Commitments Are Identified in Encl as Statements in Italics ML20206J3851999-05-0303 May 1999 Forwards 1998 Annual Radiological Environmental Monitoring Rept 05000282/LER-1999-004, Forwards LER 99-004-00 Re Discovery of Inadequate Sp That Demonstrates Operability of SFP Special Ventilation Sys.Two New NRC Commitments Are Contained in Corrective Action Section of Rept in Bold Italics1999-05-0303 May 1999 Forwards LER 99-004-00 Re Discovery of Inadequate Sp That Demonstrates Operability of SFP Special Ventilation Sys.Two New NRC Commitments Are Contained in Corrective Action Section of Rept in Bold Italics ML20206E1761999-04-28028 April 1999 Forwards Revised TS Pages for Amends 144 & 135 to Licenses DPR-42 & DPR-60,respectively,to Update Controlled Manual or File ML20205S3221999-04-20020 April 1999 Forwards Application for Amends to Licenses DPR-42 & DPR-60, Changing Implementation Date for Relocation from TS to UFSAR of Requirements in TS 3.1.E & Flooding Shutdown Requirements of TS 5.1 ML20205P9891999-04-12012 April 1999 Requests Approval for Proposed Alternatives to Liquid Penetrant Requirements of N-518.4 of 1968 ASME Boiler & Pressure Vessel Code.Results of Analysis & Summary of Tests Performed & Tests Results Are Encl ML20205Q0191999-04-12012 April 1999 Forwards Application for Amend to License DPR-42 & DPR-60, Relocating Shutdown Margin Requirements from TS to COLR 05000282/LER-1998-010, Forwards LER 98-010-01 Re Discovery That 32 App R Related MOVs Are Susceptible to Physical Damage by Fire Induced Hot Shorts.Rept Provides Addl Details on Current Plans for Completing C/As Committed to in Original LER1999-04-0808 April 1999 Forwards LER 98-010-01 Re Discovery That 32 App R Related MOVs Are Susceptible to Physical Damage by Fire Induced Hot Shorts.Rept Provides Addl Details on Current Plans for Completing C/As Committed to in Original LER ML20205P9221999-04-0101 April 1999 Submits Relief Request 8,rev 0 Which Addresses Limited Exams Associated with Unit 2 Third ten-year Interval Inservice Insp Program.Util Requests Relief Per 10CFR50.55a(q)(5)(iii) Due to Impracticality of Obtaining 100% Exam Coverage ML20205E8371999-03-31031 March 1999 Submits Four Copies of Rev 38 to Prairie Island Security Plan,Per 10CFR50.54(p).Changes Do Not Decrease Effectiveness of Security Plan.Encl Withheld,Per 10CFR73.21 ML20196K7831999-03-31031 March 1999 Forwards Decommissioning Funding Status Rept for Monticello & Prairie Island Nuclear Generating Plants,Per Requirements of 10CFR50.75(f)(1) ML20205Q5051999-03-30030 March 1999 Forwards Inservice Insp Summary Rept Interval 3,Period 1 & 2 Refueling Outage Dates 981109-1229 Cycle 19,970327- 981229. Rept Identifies Components Examined,Exam Methods Used,Exam Number & Summarized Results ML20205H5731999-03-29029 March 1999 Submits Required 1998 Actual & 1999 Projected Cash Flow Statements for Monticello Nuclear Generating Plant & PINGP, Units 1 & 2.Encl Contains Proprietary Info.Proprietary Info Withheld,Per 10CFR2.790(b)(1) ML20205C6561999-03-26026 March 1999 Submits Semiannual Update on Project Plans for USAR Review Project & Conversion to ITS ML20204H3371999-03-19019 March 1999 Forwards Application for Amend to Licenses DPR-42 & DPR-60, Removing Dates of Two NRC SERs & Correcting Date of One SER Listed in Section 2.C.4, Fire Protection 1999-09-07
[Table view] Category:UTILITY TO NRC
MONTHYEARML20065D5821990-09-19019 September 1990 Forwards Rev 25 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20059L3431990-09-13013 September 1990 Forwards Application for Amends to Licenses DPR-42 & DPR-60, Revising Tech Spec Section 6.7.A.6.b ML20064A6411990-09-0606 September 1990 Amends 900724 Certification for Financial Assurance for Decommissioning Plant,Per Reg Guide 1.159.Util Intends to Seek Rate Relief by Pursuing Rehearing & Appeal of Rate Order by Initiating New Rate Proceeding ML20059E8671990-09-0606 September 1990 Forwards Rev 24 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20028G8401990-08-29029 August 1990 Forwards Effluent & Waste Disposal Semiannual Rept for Jan- June 1990 & Revised Effluent & Waste Disposal Semiannual Rept for Second Half of 1989,which Includes Previously Omitted Fourth Quarter Analyses Results of Sr-89 & Sr-90 ML20058Q4021990-08-0202 August 1990 Informs NRC of Potentially Generic Problem Experienced W/Westinghouse DB-50 Reactor Trip Breaker.Info Being Provided Due to Potential Generic Implications of Deficiencies in Westinghouse Torquing Procedues ML20056A3371990-07-31031 July 1990 Forwards Rev 2 to, ASME Code Section XI Inservice Insp & Testing Program,Second 10-Yr Insp Interval of Operation ML20055J4441990-07-26026 July 1990 Submits Supplemental Info to Violations Noted in Insp Repts 50-282/89-26 & 50-306/89-26.Training of Supervisory Personnel Not Completed Until 900719 Due to Time Constraints Encountered During Feb 1990 Unit 1 Refueling Outage ML20055G3981990-06-28028 June 1990 Forwards Annual Rept of Changes,Tests & Experiments for 1989 & Rev 8 to Updated SAR for Prairie Island Nuclear Generating Plant ML20043F7341990-06-11011 June 1990 Responds to NRC 900420 Ltr Re Violations Noted in Insp Repts 50-282/90-04 & 50-306/90-04.Corrective Actions:Operations Procedure D61 Will Be Revised to More Clearly Identify Requirements for Logging Openings ML20043D5681990-06-0505 June 1990 Rev 23 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20043C7731990-05-25025 May 1990 Informs That on 900425,yard Fire Hydrant Hose House 7 Declared out-of-svc Due to Const in Area,Per Tech Spec 3.14.F.2.Const in Area Will Prevent Return to Svc of Hydrant Hose House 7 Until Approx 900630 ML20043A4451990-05-0909 May 1990 Responds to NRC 900319 Ltr Re Violations Noted in Insp Repts 50-282/89-29 & 50-306/89-29.Corrective Actions:Changes Will Be Made to Review & Approval Process for Work Packages ML20043A4531990-05-0202 May 1990 Responds to NRC 900319 Ltr Re Violations Noted in Insp Repts 50-282/89-29 & 50-306/89-29.Corrective Actions:Incoming Workers Will Be Specifically Trained in Fire Prevention Practices & Permanent Workers Will Be Reminded at Meetings ML20042F8681990-04-30030 April 1990 Submits Supplemental Info on Response Time Testing of Instrumentation,In Response to Concerns Raised in Insp Repts 50-282/88-12 & 50-306/88-12.No Addl Changes to Current Response Time Testing Program Necessary ML20042E8081990-04-27027 April 1990 Forwards Radiation Environ Monitoring Program Rept 1989. ML20012E4261990-03-28028 March 1990 Forwards Inservice Insp-Exam Summary 900103-0219 Refueling Outage 13,Insp Period 2,Second Interval. Exam Plan Focused on Pressure Retaining Components & Supports of RCS & Associated Sys,Fsar Augmented Exams & Eddy Current Exam ML20012D9131990-03-22022 March 1990 Forwards Rev 0 to Core Operating Limits Rept Unit 1 - Cycle 14 & Rev 0 to Core Operating Limits Rept Unit 2 - Cycle 13. ML20012E0091990-03-21021 March 1990 Forwards Completed Questionnaire in Response to Generic Ltr 90-01, Request for Voluntary Participation in NRC Regulatory Impact Survey. ML20006G1931990-02-26026 February 1990 Forwards Rev 22 to Security Plan & Advises That Changes Do Not Decrease Effectiveness of Plant Security Plan & May Be Implemented W/O Prior NRC Review & Approval.Rev Withheld (Ref 10CFR73.21) ML20012A3131990-02-26026 February 1990 Forwards Rev 0 to Effluent Semiannual Rept,Jul-Dec 1989, Supplemental Info, Amend to Effluent & Waste Disposal Semiannual Rept for First Half of 1989 & Rev 11 to Odcm. Analyses for Sr-89 & Sr-90 Will Be Included in Next Rept ML20006F8631990-02-22022 February 1990 Provides Steam Generator Tube Plugging & Sleeving Info,Per Tech Spec 4.12.E.1.Following Recent Inservice insp,15 Tubes Plugged for First Time & 37 Tubes W/New Indications Sleeved ML20042E1871990-02-19019 February 1990 Forwards Response to NRC 900118 Ltr Re Violations Noted in Insp Repts 50-282/89-30 & 50-306/89-30.Response Withheld (Ref 10CFR73) ML20006E8031990-02-16016 February 1990 Forwards Request for Relief from Schedule Requirements of NRC Bulletin 89-002, Stress Corrosion Cracking of High Hardness Type 410 Stainless Steel Internal Preloaded Bolting in Anchor/Darling Valves. ML20011E4991990-02-0606 February 1990 Discusses Liability & Funding Requirements Re NRC Decommissioning Funding Rules & Verifies Understanding of Rules.Ltr from NRC Explaining Liability & Requirements of Rule Requested ML20006B9291990-01-29029 January 1990 Responds to Generic Ltr 89-13, Svc Water Sys Problems Affecting Safety-Related Equipment. Procedure Will Be Developed to Periodically Inspect Emergency Intake Crib Located in River ML20006B9041990-01-29029 January 1990 Responds to NRC Bulletin 89-003, Potential Loss of Required Shutdown Margin During Refueling Operations. Refueling Boron Concentration Will Be Calculated W/Provisions for One Shuffle Alteration ML20006B9951990-01-0303 January 1990 Suppls Response to Violations Noted in Insp Repts 50-282/89-14 & 50-306/89-15 Re Containment Airlock Local Leak Rate Testing.Corrective Actions:Changes to Local Leak Rate Testing Procedures Approved on 891229 ML20005E4881989-12-28028 December 1989 Responds to Generic Ltr 89-10 Re motor-operated Valve Testing & Surveillance.Listed Actions Will Be Performed in Order to Meet Recommendations of Generic Ltr ML20011D6941989-12-15015 December 1989 Forwards Addendum 1 to Sacm Diesel Generator Qualification Rept & Diesel Generator Set Qualification Rept. ML19351A5281989-12-13013 December 1989 Forwards Supplemental Response to NRC Bulletin 88-009, Thimble Tube Thinning in Westinghouse Reactors. Thimble Tube Insp Program Will Be Formalized by 901231 ML20005G4861989-12-11011 December 1989 Updates Response to Insp Repts 50-282/86-07 & 50-306/86-07 Provided by 860819 Ltr.Listed Actions Taken as Result of Task Force Evaluation,Inlcluding Implementation of Work Control Process for Substation Maint ML19332F3621989-12-0101 December 1989 Responds to Generic Ltr 89-21 Re Implementation Status of USI Requirements at Facilities.Pra to Address USI A-17, Sys Interactions in Nuclear Power Plants Will Be Completed in Feb 1993 ML19332E9371989-12-0101 December 1989 Forwards Executed Amend 9 to Indemnity Agreement B-60, Reflecting Changes to 10CFR140 ML20006E3301989-11-20020 November 1989 Forwards Fee in Amount of $25,000,in Response to 891019 Notice of Violation & Civil Penalty Re Commercial Grade Procurement,Per Insp Repts 50-282/88-201 & 50-306/88-201. Responses to Violations Also Encl ML19332D1761989-11-17017 November 1989 Forwards Application for Amends to Licenses DPR-42 & DPR-60, Deleting cycle-specific Core Operating Limits from Tech Specs & Creating New Core Operating Limits Rept,Per Generic Ltr 88-16 ML19332C8341989-11-13013 November 1989 Responds to NRC 891012 Ltr Re Violations Noted in Insp Repts 50-282/89-23 & 50-306/89-23.Corrective Actions:Procedure Changes Implemented to Require Placement of Yellow Tags on Fire Detection Panel Bypass Switches in Bypass Position ML19324C4031989-11-0606 November 1989 Responds to NRC Bulletin 88-010,Suppl 1, Nonconforming Molded-Case Circuit Breakers. Supply Breaker to Unit 2 Feedwater Isolation Valve Replaced W/Qualified & Traceable Replacement Circuit Breaker ML19332B6131989-11-0606 November 1989 Forwards Rev 4 to Safeguards Contingency Plan & Implementing Procedures,Per Generic Ltr 89-07.Rev Withheld ML19324B3321989-10-13013 October 1989 Submits Supplemental Info in Response to Violations Noted in Insp Repts 50-282/88-16 & 50-306/88-16.Corrective Actions: Air Test Connections Will Be Added to Allow Pressurization of Containment Spray Piping Between Stated Motor Valves ML20246L5061989-08-31031 August 1989 Responds to Generic Ltr 89-12, Operator Licensing Exams ML20246K2361989-08-28028 August 1989 Forwards, Effluent & Waste Disposal Semiannual Rept for Jan-June 1989, Revised Repts for 1988,1987 & 1985 & Revised Offsite Dose Calculation Manual ML20246L3771989-08-23023 August 1989 Forwards Supplemental Response to NRC Re Violations Noted in Insp Repts 50-282/88-16 & 50-306/88-16. in Future,Outboard Check Valves Will Be Tested W/Upstream Vent & Motor Valves MV-32103 & 32105 Repositioned ML20245L1911989-08-14014 August 1989 Submits Supplemental Info Re NRC Audit of Westinghouse Median Signal Select Signal Validation.Operability of Median Signal Select Function Will Be Demonstrated by Verifying That Failed Channel Not Selected for Use in Level Control ML19332C8431989-08-11011 August 1989 Responds to NRC 890713 Ltr Re Violations Noted in Insp Repts 50-282/89-18 & 50-306/89-18.Corrective Actions:All Personnel Involved in Event Counseled on Importance of Following Procedures & Work Requests as Written ML20246F4341989-08-11011 August 1989 Forwards Comments on SALP 8 Repts 50-282/89-01 & 50-306/89-01 Per 890629 Request.Addl Room Adjacent to Emergency Offsite Facility Ctr Classroom to Be Designated ML20247Q8181989-07-31031 July 1989 Provides Supplemental Info in Response to 890612 Request Re NRC Bulletin 79-14, Consideration of Torsional Moments (Tms) Piping Mods. Future Mods Will Reflect Tms Where Calculations of Stresses Due to Occasional Loads Performed ML20247H9111989-07-24024 July 1989 Forwards Response to Generic Ltr 89-08, Erosion/Corrosion- Induced Pipe Wall Thinning. Administrative Procedure, Defining Erosion/Corrosion Monitoring Activities,Issued on 890220 & NUMARC Recommendations Adopted ML19332F3501989-07-20020 July 1989 Responds to NRC 890620 Ltr Re Violations Noted in Insp Repts 50-282/89-17 & 50-306/89-17.Corrective Actions:New Monthly Sampling Procedures Prepared Which Will Require Monthly Independent Samples Be Taken from Fuel Oil Storage Tank ML20247D1851989-07-12012 July 1989 Provides Addl Info Re Molded Case Circuit Breaker Replacement,Per Insp Repts 50-282/88-201 & 50-306/88-201. Util Has Concluded That Replacement Breakers from Bud Ferguson Co Suitable for safety-related Purposes 1990-09-06
[Table view] |
Text
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _
- "W.
O- - :
l
~
1
_ _ _ j NSF -
NORTHERN STATES POWER CO M PA NY M I N N E A PO L.I S. M I N N E S OTA 55400 June 3, 1980 i
R E Martin, Operating Reactors Branch #3 i
Subj: Response to EG&G Questions dtd May 13, 1980, J H Cooper, EG&G, to R E Martin, NRC
- 1. November 14, 1980 letter is attached
. LOCA dose calculations have not yet been completed
- 3. Attachment 1, item 1: '
Relay circuit. See drawings. X - H IA W 95 M'" A
- 4. Attachement 1, item 2:
y - H I A W - I - 99 't 1%c v A N E- f o o f f h.c e r 14 / ;
Monitors are redundant. Gas and particulate monitors i are provided. Each gives isolation signal. ,
- 5. Attachment 1, item 3:
No keylock switches or other physical features are used.
- 6. Attachment 1, item 4: !
Only SI reset is annunciated in the control room.
- 7. Attachment 1, item 5: ,
No justification. This is a feature of the original plant design. Modifications are being considered.
i
, [R . b yoricio6Q - -
F NORTHERN 5TATES POWER COMPANY u N N e A f8O U S. M I N N EC S OTA 55409 April 12, 1979 directorofNuclearReactorRegulation U S Nuclear Regulatory Commissiont '
Uashington, DC 230555 PRAIRIE ISLAND NUCLEAR GENERATING PLANT Docket No. 50-282 License No. DPR-42 50-306 DPR-60 Containment Purging During Normal Plant Oneration In a letter dated November 29, 1978 from Mr A Schwencer, Chief, Operating Reactors Branch #1, Division of Operating Reactors, USNRC, we were informed of a number of events occurring at other facilities which reduced the effectiveness of automatic isolation of containment purge valves. In our letter dated January 5, 1979 we provided a preliminary reply to Mr Schwencer's letter and stated that we would contact Westinghouse Electric Corporation to evaluate the impact of purgirig on ECCS performancs.
Attachment (1) contains the results of a Westinghouse calculation assessing the impact of containment purging at the time of a LOCA on calculated Prairie Island ECCS performance. As noted in this attachment, operation of the 18-inch inservice purge system during normal plant operation should have a negligible impact on ECCS performance in the event of a LOCA. Operation of the 36-inch purge system with the reactor shutdown also has a negligible impact on ECCS performance in the event of a LOCA.
Ihe radiological consequences of operation of either purge systems at the time of a LOCA are negligible. As demonstrated in the Prairie Island LOCA Analysis submitted to the Commission on Febraary 21, 1979, no clad failure will occur in the three seconds required to close the containment purge valves.
An evaluation of the containment purge isolation instrumentation and control circuitry is contained in Sections 5.3 and 7.5 of the Prairie Island FSAR. The design used is extremely reliable and will guarantee purge valve closure occurs in the event of a LOCA during containment purging.
Please contact us if you have additional questions related to this matter.
Yours very truly,
. d. 3y y-L 0 Mayer, PE Manager of Nuclear Support Services LOM/DMM/ak hk\
i I
cc: J G Kepple -
G Charnoff 790416 0 \ T1 Attachment l l
. o Attachment (1) "
NSP Letter dated April 12, 1979 Containment Purging During Normal Plant Operation According to Branch Technical Position CSB6-4, evaluation of a containment purge system design should include "an analysis of the reduction in con-tainment pressure resulting from the partial . loss of containment atmosphere during'the accident for ECCS backpressure determination". Such an analysis has been performed for the Prairie Island Plant based on the containment conditions defined in the limiting FAC analysis case (DEC1C break, CD = 0.4) obtained using the February 1978 Westinghouse Evaluation Model. The contain-ment isolation signal received in that analysis will initiate valve closure shortly af ter inception of the 10CA. The inservice purge system utilized during reactor operation consists of two 18-inch diameter lines. It is con-servatively represented in this computation as follows:
- 1. A 3 second isolation valve closure time is assumed. No credit is taken for the reduction in effective flow area which occurs while the valve is in the process of closing.
~
- 2. The frictional res1 stance association with duct entrance and exit losses, filters, ductwork bends and skin friction has not been considered.
- 3. No fan coastdewn effects are considered.
4 No inertia is considered. Steady state flow out the purge system ducts is established immediately at ene time of the LOCA.
A mixture of occam and air wLil be exhausted from the containment through the purge lines during the time that the isolation valves are assumed to remain open. The effect of the composition of the gas being exhausted on contains.ent pressure has been bounded by investigating the two extreme cases, air alone and steam alone. Within several seconds of the inception of the LOCA, containment pressure will have increased to the point that critical flow will occur in the purge lines. To conservatively bound the calculated containment gas mixture exhausted through the purge lines, critical flow rates of steam and air were calculated during the CD = 0.4 DECIG break transient. Using these flowrates, critical flow was conservatively assumed to be in effect from time zero.
Equation (4.18) in Reference (1), was employed to calculate the critical flow rate of air _through the Prairie Island purge lines. Figure 14 of Reference (2) was applied to compute the critical flow rate of steam through the purge lines. The total mass released during the time period that the valves are presumed open is calculated as 1553 lbs. air or 1123 lbs. steam. The impact on containment pressure resulting from this loss of air or of steam is less than 0.35 psi in either case. The effect of s containment pressure reduction of this magnitude on the calculated peak clad temperature (PCT) is expected to be minor (less than 200 F). Therefore, the results of this evaluation !
indicate that the Prairie Island Units should meet 10 CFR 50.46 requirements i even if the containment inservice purge system is operating at the ti=c of a LOCA event.
I 1
l
.~
i
.. , 1 Attachment (1)
NSP Letter dated April 12, 1979 Containment Purging During Normal Plant Operation When the reactor is shutdown, a containment purge system consisting of two 36 inch diameter lines is used for ventilation. A computation identical to that described above was performed for the 36 in. line size. Assuming only air is released, 6213 lbs. air are lost from the containment building while the isolation valves remain open; if only steam is released, 4492 lbs.
are lost. In either case the impact on the calculated containment pressure is less than 1.4 psi. The impact of a containment pressure reduction of this magnitude on the calculated PCT will be minor compared to the reduction in PCT associated with shutdown conditions. Therefore, use of the 36-inch diameter containment purge system while the reactor is shutdown would not violate 10 CFR 50.46 criteria.
i REFERENCES :
(1) Shapiro, A. H., The Dynamics and Thermodynamics of Compressible Fluid Flow, Volume 1, p. 85.
(2) 1967 ASME S t eam Tab les , p . 301.
',f %g .
, , _ ,,s ur: TED ::TATt::
f y,)y(q h NUCLEAR REGULATORY COMMISSION E WASHWGTON,0. C. 20555
,N<.JC.Agg/
October 29, 1979
% mf a s
Docket Nos. 50-282 and 50-306 Mr. L. O. Mayer, Manager
. Nuclear Support Services Northern States Power Ccx1pany 414 Nicollet Hall - 8th Floor ,
Minneapolis, Minnesota 55401
Dear Mr. Mayer:
RE: Containment Purging and Venting During Nomal Operation By letter dated November 28, l978, the Commission (NRC) requested all licensees of operating reactors to respond to generic concerns about
, containment purging or venting during nonnal plant operation. The generic concerns were twofold:
(1) Events had occurred where licensees overrode or bypassed the safety
, actuation isolation signals to the containment isolation valves.
These events were determined to be abnonnal occurrences and reported to C~ongress in January 1979.' .
(2) Recent licensing reviews have required tests or analyses to show that
. containment purge or vent valves would shut without degrading con- -
tainment integrity during the dynamic load t of a design basis loss of coolant accident (DBA-LOCA)
The NRC position of the November 1978 letter requested that licensees take the following positive actions pending complettort of the NRC review:
(1) prohibit the override or bypass of any safety actuation signal which wcuid affect another safety actuatfor signal; the NRC Office of Inspection and Enforcement would verify that administrative controls prevent improper manual defeat of safety actuation signals, and (2) cease purging (or '
venting) of containment or limit purging (or venting) to an absolute minimum, not to exceed 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per year. Licensees were requested to demonstrate 'by test or by test and analysis) that containment isolation valves would out under postulated DBA-LOCA condition. The NRC positions were amplified by citatiort (and an attached copy) of our Standarti Review '
Plarr (SRP) 6.2.4 Revision 1 and the associated Branch Technical Positiorr CSB 6-4, which have effectively classed the purge and vent valves as
" active." inycking. the ope ~~ -
,pf .z
,w .
n.
The- NRC staff has made si4' licensees at Bethuda, Ma DUPLICATE DOCUMENT many other licensees and discussions, the NRC sta Entire document previously as noted above to assure entered into system under:
in the event of a DSA-LOC ANO '79/20 4 o//Af 4% 7h( No. of pages: f
. _ ._ _ (. .f_)
4 W
am(
8T I NORTHCRN STATES POWER COMPANY-M f M N E A P C L,1 C. M f N N C S CTA 5540%
o November 14, 1979 Director of Nuclear Reactor Regulation U S Nuclear Regulatory Commission Washington, DC 20555 PRAIRIE ISLAND NUCLEAR GENERATING PLANT Docket No. 50-282 License No. DPR-42 50-306 DPR-60 Dettonstration of Containment
_ Purge Valve Operability In a letter dated September 27, 1979 from Mr Darrell Eisenhut, Acting Director, Division of Operating Reactors, USNRC, we were provided with a docu=ent entitled, " Guidelines for Demonstration of Operability of Purge and Vent Valves." We were requested to initiate action on an expedited basis to ensure that containment vent and purge valves at Prairie Island meet these guidelines.
In a letter dated October 29, 1979 from Mr A Schwencer, Chief, Operating Reactors Branch #1, Division of Operating Reactors, USNRC, se were provided with a document entitled, " Interim Position for Containment Purge and Vent Valve Operatiet. Pending Resolution of Isolation Valve Operability." We were requested to commit to operate in conformance with the interim position and provide information which demonstrates that we have initiated the purge and vent valve operability verification on an expedited basis. Our response was to be submitted in accordance with 10 CFR 50.54(f) . l l
The following action has been taken to resolve the containment purge and vent.
valve operability questions discussed in these two letters:
- a. As noted in our Licensee Event Report dated June 20, 1979 (79-019) and our letter dated July 10, 1979, we have placed administrative controls on our containment purge and vent valves. These valves will be closed whenever the reactor is above cold shutdown.
- b. We have requested a proposal from the valve manufacturer, the Henry Pratt Company, to perform tests or analyses which demonstrate that the valves are capable of closing in the event a loss of coolant accident occurs while the containment is being purged. Valve modifications, if required, would be g included in the scope of this work.
W 7 911210 +S 7
NORTHCCN OTATCG POWCR CO! hNY Director of Nuclear Reactor Regulation Page 2 November 14, 1979
- c. Westinghouse Electric Corporation has completed an analysis which shows that ECCS system performance will be satisfactory in the event a loss of coolant accident occurs while the con-tainment is being purged. This was submitted by NSP for NRC review on April 12, 1979.
In confor=ance with the NRC Staff's " Interim Position for Containment Purge and Vent Valve Operation Pending Resolution of Isolation Valve Operability", we will continue to keep purge and vent valves closed above cold shutdown.
When the test and analysis program in item (b) above has been satisfactorily completed, vc will resume purge and vent operations during normal plant operation, limiting all purging and venting times to as low as achievable in accordance with the NRC Staff's interim position. We will work with the valve manufacturer to assure that tests and analyses performed to assure adequacy of the valves will meet with NRC approval. This may require discussions with the Staf f and valve manufacturer to resolve potential difficulties with the Staff's guidelines for demonstration of valve operability.
Please contact us if you have any questions related to the information we have provided, h*
L 0 Mayer, PE Manager of Nuclear Support Services LOM/DMM/ak cc: J G Keppler G Charnoff l
l 4
-- w e
UNITED STATES NUCLEAR RE a t.uoxY C0;;CSSR.,
NORTHERN STATES POWER COMPANY
?".AIRIE ISLAND NUCLEAR CENERATING PLANT Docket No. 50-282 50-306
- License No. DPR-42 DPR-60 LETTER DATED NOVEMBER 14,- 1979 RESPONDING TO NRC REQUEST FOR INF010 TAT 20N ON THE DEMONSTRATION OF CONTAINMENT PURGE VALVE OPERABILITY Northern States Power Company, a Minnesot.a corporation, by this letter dated November 14, 1979 hereby submits a response to the NRC request dated October 29, 1979 for information on the demmistration of centainment purge valve operability.
This response contains no restricted or other' defense information.
NOP.THERN STATES POWER COMPANY By 6 ,8 M / d >
L J Wachter Vice President, Power Production
& System Operation l l
On this 14th day of November,1979, before me a notary public in and fot said County, personally appeared L J Wachter, Vice President, Power Production and System Operation, and being first duly sworn acknesledged that he is authorized I to execute this document on behalf of Northern St. :es Power Company, that he I knows the contents thereof and that to the best of his knowledge, information and belief, the statements made in it are r and that it is not interposed for l l
delay. l
'l 2asab h *
[ Jeanne NotaryMPublic Hacker - Minnesota Hennepin County My Commission Expires May 6,1986 I
h <&
< l JEANNE M. HACKER 4Cf AAv Pustic . utNNESof4 l
- l HENNEPIN COUNTY l i
- e ,co. % e. s,e.......,, ...e ;
': m .s yrs ..w