ML19309B782
| ML19309B782 | |
| Person / Time | |
|---|---|
| Site: | Callaway |
| Issue date: | 02/11/1980 |
| From: | Cordero Z, Danielson D, Lee E K NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML19309B776 | List: |
| References | |
| 50-483-80-02, 50-483-80-2, NUDOCS 8004070173 | |
| Download: ML19309B782 (5) | |
See also: IR 05000483/1980002
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U.S. NUCLEAR REGULATORY COMMISSION
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0FFICE OF INSPECTION AND ENFORCEMENT
REGION III
Report No. 50-483/60-02
Docket No. 50-483
License No. CPPR-139
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Licensee: Union Electric Company
P.O. Box 149-
St. Louis, MO 63166
Facility Name:
Callaway, Unit 1
Inspection At: Callaway Site, Callaway County, M0
Inspection Conducted: January 23-25, 1980
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Inspectors:
E. W. K. Lde
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Z. Cordero
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Approved By:
D. H. Danielson, Chief
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Engineering Support Section 2
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Inspection Summary
Inspection on-January 23-25, 1980 (Report No. 50-483/80-02)
Areas-Inspected: Reactor Coolant Pressure Boundary Piping welding activi-
ties, records, and procedures; safety related piping work activities. The
inspection involved a total of 38. inspector-hours'onsite by two NRC. inspect-
ors.
-Results: Of the four areas inspected, no items of noncompliance or deviation
were identified in three arear,.
One item of noncompliance was identified
in one area (infraction - failure to follow procedure paragraph 2).
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DETAILS
Persons Contacted-
Principal Licensee Employee
- G. N. Belchik,' Construction Engineer
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- J. R. Cook,-QC Manager
- M. I. Doyne, . General . Superintendent , Callaway Construction
- *J. V. Laux,. Assistant-QA Engineer
- R. L. Powers,' Supervising Engineer,.QA
- R. Veatch, Assistant QA Engineer
Other Personnel
- J. A. Holland, Project QA Manager, Daniel International Corporation (DIC)
- E. D. McFarland, Construction Engineering Manager, DIC
- H. J. Potter, Authorized Nuc! .ar Inspector, Hartford Steam Boiler Inspection
and Insurance Company
- M. K. Smith, Audit Responri-ility Coordinator, DIC
- H. J. Stan, Project Mana;;ei , DIC
The inspector also talked with and interviewed several other contractor
employees, including members of the quality, craftsmen, and foremen.
- D notes those attending the exit interview.
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Functional or Program Areas Inapected
1.
Reactor Coolant Pressure Boundary Piping - Welding Material Control
a.
Review of Document
The inspector reviewed the following documents:
(1) Daniel International Corporation (DIC) Procedure No. AP-VIII-02,
Revision 7, " Requisitioning Materials, Equipment, and Services."
(2) DIC Procedure No. AP-VIII-05, Revision 4, " Issuing Purchase
Orders and Change Orders."
(3) DIC Procedure No. AP-VII-03, Revision 4, " Material and
Equipment Receiving and Inspection."
(4) DIC Procedure No. WP-503, Revision 9, " Control of Welding
Consumables."
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.'(5) LPurchase' Order, Receiving Inspection Report, and' Material
Certification for E7018 welding rods with lot No. 02-1-D902R
and heat No. 402H9361, lot No. 02-2-C802P and heat No.
432B5961,. lot No. 02-2-B827P and heat No. 53119, E70S-2
welding rods with heats No. 065304, No. 065150, and No. 065163.
It.was determined that the above documents met the PSAR, 10 CFR
'50, Appendix B, and the applicable code requirements.
b.
Control of Materials
The inspector toured the weld rod issuing station located at the
Turbine Room and the trailer.
It was determined that (1) the
welding materials are properly identified and segregated; (2)
- the temperature of the rod ovens is maintained; (3) records are
-properly kept and (4) issuance and return of welding materials
are controlled in accordance with the approved procedure.
No items of noncompliance or deviations were identified.
2.
Reactor Coolant Pressure Boundary Piping - Observation of Welding
Activities
The inspector observed the following welding activities:
Reactor Coolant System Weld No. 2-BB-01-F204 on drawing No.
a.
M-03-BB01.
b.
Reactor Coolant System Weld No. 2-BB-01-F404 on drawing No.
M-03-BB01.
Reactor Coolant System Weld No. 2-BB-01-F302 on drawing No.
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c.
M-03-BB01.
It was determined that (1) work was conducted in accordance with
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traveler- (2) proper welding materials were used; (3) welding pro-
cedure requirements were met;-(4) work area was' free of weld rod-stubs;
(5) physical appearance was acceptable and (6) the welder welding on
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weld No. 2-BB-01-F404 had some of the welding rod in a welding rod
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pouch. .The condition is an item of noncompliance identified in
Appendix A.
(483/80-02-01)
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Except as_noted, no items of noncompliance or deviations were
identified.
3.
Reactor Coolant Pressure Boundary Piping - Observation of Work and
Work Activities
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The-inspector observed ti.e fitting up and alignment of Reactor Coolant
System Weld No. 2-BB-01-F305 on drawing No. M-03-BB01.
It was deter--
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mined that work activities were performed in accordance with the.
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applicable procedures and good construction practices were adhered
to.
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No items of noncompliance or deviations were identified.
4.
Reactor Coolant Pressure Boundary Piping - Visual Examination of Welds
a.
. Visual Examination
The inspector visually examined the following completed welds:
(1) The outside surface of the Reactor Coolant System Welds
-No. 2-BB-01-F202, No. 2-BB-01-F203 and No. 2-BB-01-F303 on
drawing No. M-03-BB01.
(2) The inside surface of the Reactor Coolant System loop 4,
weld No. 2 on drawing No. 26215-SCP, sheet 10.
It was detetmined that (1) weld surface finish and appearance
were acceptable and there was no evidence of wall thinning d.ae
to grinding; (2) are strikes and weld spatter were not evidence
and (3) there is some form of a linear indication on the inside
surface of loop 4, weld No. 2.
The indication is located at
approximately 9 o' clock to 1 o' clock when looking out from the
inside of the Reactor Vessel. The inspector also reviewed the
radiographic films and the liquid penetrant report but neither
the films nor the report showed the indication. The inspector
stated that this matter is considered unresolved pending a
review of a disposition report from Westinghouse and a written
acceptance of Westinghouse's disposition from the licensee.
(483/80-02-02)
b.
Review of Records
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The inspector reviewed Weld Control Record of the Reactor
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Coolant System Welds No. 2-BB-01-F202, No. 2-BB-01-F203 and
No. 2-BB-01-F303 on drawing No. M-03-BB01.
It was determined that (1)-the records indicated specified inspec-
tions were completed; (2) records are clear and legible and (3) purge
' dam removal, visual examination, and NDE have not been performed.
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No items of noncompliance or deviations were identified.
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15.
. Reactor Coolant' Pressure Boundary Piping - Weld Heat Treatment
a.
Review of Preheating Procedure-
The inspector reviewed DIC procedure No. N-8-8, Revision 16,
" Welding of Stainless Steel" and determined that preheating and
monitoring methods are specified and acceptable.
b.
Observation of Preheating
While observing welding activities for items stated in Paragraph
2 of this report,.the inspector determined that preheat met the
procedure requirements.
No items of noncompliance or deviations were identified.
6.
Reactor Coolant Pressure Boundary Piping - Welder Qualification
The inspector reviewed the following documents:
a.
DIC Procedure No. WP-502,. Revision 8, " Qualification of Welders."
b.
Randomly selected the qualification record of six welders who
performed welding on welds stated in paragraph 2 of this report.
No items of noncompliance or deviations were identified.
7.
Safety Related Piping - Observation of Work and Activities
The inspector observed the installed High Pressure Coolant Injection
System between Safety Injection Pump No. PEM01B and Valve No. 8926A.
It was determined that the pipe rum was installed in accordance with
the drawing.
No items of noncompliance or deviations were identified.
Unresolved Items
Unresolved items are matters about which more information is required in
order to ascertain whether they are acceptable items, items of noncompliance,
or diviation.
Unresolved item disclosed.during the inspection is discussed
in paragraph 4.
Exit Interview
-The inspector met with licensee representatives (denoted under Persons
Contacted) at the conclusion of the inspection on January 25, 1980. The
inspector summarized the purpose and findings of the inspection. The
licensee acknowledged the findings reported herein.
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