ML19308A996

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Abnormal Occurrence AO-269/74-08:on 740507,reactor Coolant Pressure Transmitters RC3A-PT1,RC3A-PT2,RC3B-PT1 & RC3B-PT2 Found Out of Calibr.Caused by Instrument Drift.Transmitters Recalibr & Calibr Frequency Increased
ML19308A996
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 05/17/1974
From:
DUKE POWER CO.
To:
Shared Package
ML19308A991 List:
References
NUDOCS 7912120754
Download: ML19308A996 (2)


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DUKE POWER COMPANY OCONEE UNIT 1 Report No. : AD-269/74-8 Report Date: May 17, 1974 Occurrence Date:

May 7, 1974 Facility: Oconee Unit 1, Seneca, South Carolina Identification of Occurrence:

Reactor coolant pressure transmitters out of calibration Conditions Prior to Occurrence:

Cold shutdown Description of Occurrence:

On May 7, 1974, pressure transmitters RC3A-PT1, RC3A-PT2, RC3B-PT1, and RC3B-PT2 were found to be out of calibration by -1.9 percent, -2.1 percent, -3.8 percent, and -3.2 percent respectively.

These pressure transmitters provide reactor coolant pressure information to the Reactor Protective System.

The full-scale error measured as a result of transmitter drift was:

Channel A RC3A-PT1 - 15.2 psi Channel B RC3A-PT2 - 16.8 psi Channel C RC3B-PTl - 25.6 psi channel D RC3B-PT2 - 30.4 psi All four transmitters drifted in the negative direction and were within 2 percent of each other.

The transmitters were last calibrated on February 8-9, 1973, and there has been no indication of problems since the last calibration.

Analysis of Occurrence:

The Reactor Protective System high and low pressure trips are accuated by signals from the affected pressure transmitters.

The low pressure trip setpoint drifted in a conservative direction, and the high pressure trip setpoint drifted such that the high pressure trip setpoint exceeded the maximum RPS trip setting (2355 psig) by 24.4 psi.

However, the high pressure trip setpoint had been set at 2349 psig to allow for instrument drift, and a total reactor coolant pressure measurement error of -30 psi had been assumed in the safety analysis.

Therefore, the pressure transmitter drift would not have resulted in a high pressure trip at a pressure higher than that assumed in the safety analysis.

Furthermore, the safety limit of 2790 psig was not approached.This incident did not affect the health and safety of the public.

Corrective Action:

Immediate corrective action was to recalibrate the pressure transmitters.

This was completed on May 8, 1974.

To prevent similar occurrences, the frequency of calibration will be increased until there is assurance that the transmitters will not drift out of tolerance between calibrations.

Initially, calibration will be performed during outages for repatching control rods, approximately 1912120ISf'

4 v.

  • ary 100 affective full power days.

1 Failure Data:

The RPS pressure transmitters are Motorola Type 56PM-56PL'. The last calibration of these instruments was performed on February 8-9, 1973.

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