05000269/LER-1977-029-03, /03L-0:on 771219,Keowee Hydro Unit 2 Failed to Start on Initiation from Oconee.Caused by Failure of Field Flashing Breaker to Close.Breaker Verified Operable by Subsequent Operation.Insp Showed No Abnormality

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/03L-0:on 771219,Keowee Hydro Unit 2 Failed to Start on Initiation from Oconee.Caused by Failure of Field Flashing Breaker to Close.Breaker Verified Operable by Subsequent Operation.Insp Showed No Abnormality
ML19308A785
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 01/18/1978
From: Ken Wilson
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19308A781 List:
References
LER-77-029-03L, LER-77-29-3L, NUDOCS 7912110766
Download: ML19308A785 (1)


LER-1977-029, /03L-0:on 771219,Keowee Hydro Unit 2 Failed to Start on Initiation from Oconee.Caused by Failure of Field Flashing Breaker to Close.Breaker Verified Operable by Subsequent Operation.Insp Showed No Abnormality
Event date:
Report date:
2691977029R03 - NRC Website

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.0 EVENT DESCRIPTION AND PROB A8LE CONSEQUENCES lo t:1 I Durint normal operation Keowee Hydro Unit 2 failed to start on initiation to43; l from Oconee control room.

Since Keowee 2 is a source of auxiliary power i

I o 141 i for the Oconee station (Units 1,2, and 3) this is reportable under io,si[

T.S. 6.6.2.1.b.(2).

The unit started normally on second and subsequent i

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u ey C4uSE DESCRIPDCN AND COARECOVE AC 3CNS h 1, # o t l The Field Flashine Breaker on the generator failed to close on first i

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The breaker was verified as operable by subsequent operation

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