LER-1979-027, /03L-0 on 790216:absolute Position Indication Amplifer for Rod 9 of Group 5 Was Inoperable.Caused by Failure of Integrated Circuit Chip in Amplifier.Integrated Circuit Chip Replaced |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3461979027R03 - NRC Website |
|
text
U. S. NUCLEAR REGULATORY COMMISSION NRC F ORM 36G 0411 LICENSEE EVENT REPORT
l l
l l
l (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION)
I 6
@l0l0l-l0l0lNlP]Fl-l0l3l@l4l1l1l1l1 @l l
l@
lo lt l l 0 l H DlBlS 1
7 8 9 LICENSEE COGE 14 15 LICENSE NUVBER 25 a t>
LLCENSE TY PE JO SI C A r 58
((g] l L )@l 0 l 5 l 0 l - l 0 l 314 l 6 @l 0 l 2 l 1 l 6 I 719 ]@l 0 ] 3 l 1l 5 l 7 l 9 l@
COWT o
1 i
8 60 61 DOCKET NUYBER 68 63 EVENT DATE I4 15 REPORT C ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h At 2233 hours0.0258 days <br />0.62 hours <br />0.00369 weeks <br />8.496565e-4 months <br /> on 2/15/79, an asymmetry alarm was received on all rods in Group 5.
l lo12]
The absolute and relative position indications indicated all rods 100% withdrawn. At ;
l o 131 i hours on 2/16/79, technicians found the absolute position indication (API) ampli7 0730 o
4 fier for Rod 9 of Group 5 to be inoperable. This placed the unit in Action Statement o
s I (a) of Technical Specification 3.1. 3.3.
There vas no danger to the health and safety [
10161 [
O 7
l of the public or unit personnel. The control rod was verified aligned with the group l by zone reference location and API-the relative indication was operable. (NP-33-79-3 )
g g
7 8 9 COVP.
VALVE SYSTEY
CAUSE
CAUSE CODE CODE SU8 CODE COUPONENT CODE SU8 CODE SUSCODE l0l91 l R l B l@ IMh lG l@ l Il Nl Sl Tl Rl Ul@ l E l@ ]@
7 8
9 TO 11 12 13 18 19 20 REVISION SE QUE NTI AL OCCURRENCE REPORT LER 90 EVENT YE AR REPORT NO.
CODE TYPE NO.
O,agg 1719 l-1012l7l l-l j ol3 jt l l_l lcj
_ 21 21 23 24 26 27 28 29 20 31 32 KE4 C
C PLA T ET O HOURS S 8 T FOP t 8.
S PL E MAN FACTO ER l A]Ql Zl@
l Zig lZ l@
l Dj 0l 0l 0l l Yl@
[ N]@
[ N Q lD lj 5l Og 33 J4 h
Jo 31 40 41 42 43 44 47 cAUSE DESCRIPTION AND CORRECTIVE AFilONS l Upon investination, technicians found that an integrated circuit chip in the API *.am-l i
o i
i i plifier for Rod 9 of Group 5 had failed. The integrated circuit chip was replaced, J
l i 1,1 l returning operability to the API for Rod 9 of Group 5.
At 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br /> on 2/16/79, fron l i 3 l all of Group 5 API amplifiers were returned to normal status, removing the unit 1 Action Statement (a) of Technical Specification 3.1.3.3.
l i
4 80 7
e 9 ST S
N PonER OTHER ST ATUS D SCO RY DISCOVERY DESCRIPTION l E @ l 0l 8l 8l@l NA l
l Al@l operator observation l
i 5 A TIVITY CC TENT RELE ASED CF H6LE ASE AMOUNT OF ACTIVITY LOCATION oF RELE ASE NA l
l NA l
[Z)@ [Zj@l i
6 60 7
8 9 10 11 44 45 PERSONNEL E XPOSURES NUY8 E R TYPE CE SCR6P TION -
101010 l@l Z l@l NA I
i 7
PE RSON N E IN1b ES NUYMER CESCRIPTION l
l0lNl l NA 1 a 80 7
8 9 11 12 LOSS OF OR D AY AGE TO FACILITY TYFE DE SCniP TION l
li l o l Lzj@
NA 80 7
8
'l 10 LN_j81NA 79032003%
i i iiiii'ii i i l:
squrn DESCR'PTION 2 o 68 69 80-5 7
8 9 19 036 C. Mdens 419-259-5dC0, Ext. 231 PHONE:
NAME OF PREPARER
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-31 DATE OF EVENT:
February 16, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: The Absolute Position Indication (API) for Control Rod 9 of Group 5 was inoperable.
Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2440, and Load (Gross MC) = 805.
Description of Occurrence: At 2233 hours0.0258 days <br />0.62 hours <br />0.00369 weeks <br />8.496565e-4 months <br /> on February 15, 1979, an asymmetry alarm was received on all rods in Group 5.
However, all rods indicated 100% withdrawn both on the absolute and relative position indications. At 2252 hours0.0261 days <br />0.626 hours <br />0.00372 weeks <br />8.56886e-4 months <br />, the API for each rod in Group 5 was placed in BYPASS, as it appeared that the asymmetric rod fault circuitry for Group 5 was inoperable. At 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br /> and 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br /> on Febru-ary 16,1979, all rods in Group 5 were verified as being 100% withdrawn on the absolute position indication, the relative position indication, and the 100% zone reference indication. At 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br /> on February 16, 1979, the Instrument and Control technicians found the API amplifier for Rod 9 of Group 5 to be inoperable.
This placed the unit in Action Statement (a) of Technical Specification 3.1.3.3, which permits continued operation provided all relative position indication is operable.
Designation of Apparent Cause of Occurrence: Upon investigation, Instrument and Control technicians found that an integrated circuit chip in the API amplifier f or Rod 9 of Group 5 had f ailed high. This caused the group average amplifier to go high and this in turn caused asymmetry alarms on all rods (Rod 9 looked high, and all other rods in Group 5 looked low). The failure of this component caused the API for Rod 9 of Group 5 to be inoperable.
Analysis of Occurrence: There was no danger to the health and safety of the public cr to unit personnel. The control rod was actually aligned with the group, and the relative indication was operable. The control rod was operating properly.
Corrective Action
On February 16, 1979, the integrated circuit chip was replaced, returning operability to the API for Rod 9 of Group 5.
At 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br /> on February 16, 1979, all of Group 5 API amplifiers were returned to normal status, which removed the unit from Action Statement (a) of Technical Specification 3.1.3.3.
Failure Data: There have been no previous API failures caused by API amplifier failures.
LER #79-027
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000346/LER-1979-001-03, /03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator | /03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator | | | 05000346/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000346/LER-1979-002-03, /03L-1 on 790102:main Steam Valves 106 & 106A Failed to Open,Resulting in Auxiliary Feed Pump Afp 1-1 Being Taken Out of Operation.Caused by Dirt Buildup on Valve Stems as Result of New Const | /03L-1 on 790102:main Steam Valves 106 & 106A Failed to Open,Resulting in Auxiliary Feed Pump Afp 1-1 Being Taken Out of Operation.Caused by Dirt Buildup on Valve Stems as Result of New Const | | | 05000346/LER-1979-002, Forwards LER 79-002/03L-1 | Forwards LER 79-002/03L-1 | | | 05000346/LER-1979-003-03, /03L-0 on 790104:control Room Emergency Ventilation Sys Damper HV5311E Inoperable.Caused by Leaking Pneumatic Operator.New Operator Installed.Damper Operated & Tested for Response Time & Declared Operable | /03L-0 on 790104:control Room Emergency Ventilation Sys Damper HV5311E Inoperable.Caused by Leaking Pneumatic Operator.New Operator Installed.Damper Operated & Tested for Response Time & Declared Operable | | | 05000346/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000346/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000346/LER-1979-004-03, /03L-0 on 790105:failure to Post Guards at Entrance to Containment During Periods of Free Access. Caused by Personnel Error.Special Order 84 Revised to Require Posting of Guards | /03L-0 on 790105:failure to Post Guards at Entrance to Containment During Periods of Free Access. Caused by Personnel Error.Special Order 84 Revised to Require Posting of Guards | | | 05000346/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000346/LER-1979-005-03, /03L-0 on 790106:during Surveillance Testing, Borated Water Storage Tank Level Bistable Was Tripped;Valves DH9A Opened & DH7A Closed.Caused by Component Failure of Output Relay K51A & Instrument Drift | /03L-0 on 790106:during Surveillance Testing, Borated Water Storage Tank Level Bistable Was Tripped;Valves DH9A Opened & DH7A Closed.Caused by Component Failure of Output Relay K51A & Instrument Drift | | | 05000346/LER-1979-006-03, /03L-0:on 790105,reviewer Noted 781228 Record of Continuous Alarm at Contact Data Record Point F018.Panel C4705 Not Reset.Caused by Failure of Indicator Lights on Panel C4705.Panel Reset,Clearing F018.Surveillance Modified | /03L-0:on 790105,reviewer Noted 781228 Record of Continuous Alarm at Contact Data Record Point F018.Panel C4705 Not Reset.Caused by Failure of Indicator Lights on Panel C4705.Panel Reset,Clearing F018.Surveillance Modified | | | 05000346/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000346/LER-1979-007-03, /03L-0 on 790110:during Performance of Surveillance Test,Channel 2 of Containment Hydrogen Analyzer Was Found Inoperable.Caused by Defective Zener Diode in Millivolt Converter | /03L-0 on 790110:during Performance of Surveillance Test,Channel 2 of Containment Hydrogen Analyzer Was Found Inoperable.Caused by Defective Zener Diode in Millivolt Converter | | | 05000346/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000346/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000346/LER-1979-008-03, /03L-0 on 790109:during Surveillance Testing, Containment Recirculation Fan 1-1 Failed to Run.Cause Attributed to Buildup of non-conductive Film on Auxiliary Controller Contacts | /03L-0 on 790109:during Surveillance Testing, Containment Recirculation Fan 1-1 Failed to Run.Cause Attributed to Buildup of non-conductive Film on Auxiliary Controller Contacts | | | 05000346/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000346/LER-1979-009-03, /03L-0:on 790112,power to Vital Bus Y2 Lost. False Integrated Control Sys Signal Resulted in Reactor & Full Steam & Feedwater Rupture Control Sys Trip.Caused by Blown 125 Volt DC Fuse to Inverter | /03L-0:on 790112,power to Vital Bus Y2 Lost. False Integrated Control Sys Signal Resulted in Reactor & Full Steam & Feedwater Rupture Control Sys Trip.Caused by Blown 125 Volt DC Fuse to Inverter | | | 05000346/LER-1979-010-03, /03L-0:on 790112,Sys 7 Data Logger Experienced Core Dump,Voiding Computer Memory Bank Which Rendered Remote Monitoring of Fire Detection Sys Inoperable & Placed Unit in Action Statement of Tech Spec 3.3.3.8.Cause Unknown | /03L-0:on 790112,Sys 7 Data Logger Experienced Core Dump,Voiding Computer Memory Bank Which Rendered Remote Monitoring of Fire Detection Sys Inoperable & Placed Unit in Action Statement of Tech Spec 3.3.3.8.Cause Unknown | | | 05000346/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000346/LER-1979-011-03, /03L-0:on 790115,reactor Coolant Pump 1-2-2 Started W/Incorrect Breaker Alignment,Causing Low Voltage Relays to Trip Which de-energized Both 4.16 Kv Essential Buses C1 & D1.Caused by Personnel Error | /03L-0:on 790115,reactor Coolant Pump 1-2-2 Started W/Incorrect Breaker Alignment,Causing Low Voltage Relays to Trip Which de-energized Both 4.16 Kv Essential Buses C1 & D1.Caused by Personnel Error | | | 05000346/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000346/LER-1979-012-03, /03L-0:on 790116,during Surveillance Testing,Heat Traced Line Temp Measurement Points Below 105 F Limit.Caused by Injection of Makeup (Flush) Water After Boron Injection at Temp Lower than 105 F.Tests Rerun Satisfactorily | /03L-0:on 790116,during Surveillance Testing,Heat Traced Line Temp Measurement Points Below 105 F Limit.Caused by Injection of Makeup (Flush) Water After Boron Injection at Temp Lower than 105 F.Tests Rerun Satisfactorily | | | 05000346/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000346/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000346/LER-1979-013-03, /03L-0:on 790116,when Makeup Pump 1 Started for Surveillance testing,1/2 Inch Nipple at Discharge of Attached Gear Driven Lube Oil Pump Failed,Resulting in Oil Spray Which Required Pump Shutdown | /03L-0:on 790116,when Makeup Pump 1 Started for Surveillance testing,1/2 Inch Nipple at Discharge of Attached Gear Driven Lube Oil Pump Failed,Resulting in Oil Spray Which Required Pump Shutdown | | | 05000346/LER-1979-014-03, /03L-0:on 790116,during Shutdown,Boric Acid Addition Tanks (Baat) Total Vol 3-1/3% Below Tech Spec 3.1.2.9 Requirements.Caused by Reduced Baat Vol After Completion of Required Testing Followed by RCS Boration | /03L-0:on 790116,during Shutdown,Boric Acid Addition Tanks (Baat) Total Vol 3-1/3% Below Tech Spec 3.1.2.9 Requirements.Caused by Reduced Baat Vol After Completion of Required Testing Followed by RCS Boration | | | 05000346/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000346/LER-1979-015-03, /03L-0:on 790117,core Flood Tank 1-2 Isolation Valve CF1A Would Not Close by Remote Operation.Caused by Loose Set Screw.Cracked Pinion Gear & Associated Key Replaced Per Maint Work Order 78-2928 | /03L-0:on 790117,core Flood Tank 1-2 Isolation Valve CF1A Would Not Close by Remote Operation.Caused by Loose Set Screw.Cracked Pinion Gear & Associated Key Replaced Per Maint Work Order 78-2928 | | | 05000346/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000346/LER-1979-016-03, /03L-0:on 790124,emergency Lock Failed Leak Rate Test While Unit in Mode 5.Caused by Loosening of Shaft Seal (Teflon Packing) Due to Routine Use of Escape Lock.Packing Will Be Replaced During Next Convenient Outage | /03L-0:on 790124,emergency Lock Failed Leak Rate Test While Unit in Mode 5.Caused by Loosening of Shaft Seal (Teflon Packing) Due to Routine Use of Escape Lock.Packing Will Be Replaced During Next Convenient Outage | | | 05000346/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000346/LER-1979-017-03, /03L-0:on 790130,photoelectric Smoke Detector Ds 8605-E in Emergency Diesel Generator 1-1 Area Not Functional.Caused by Failure of Detector.New Detector Ordered & Fire Watch Patrol Established in Area | /03L-0:on 790130,photoelectric Smoke Detector Ds 8605-E in Emergency Diesel Generator 1-1 Area Not Functional.Caused by Failure of Detector.New Detector Ordered & Fire Watch Patrol Established in Area | | | 05000346/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000346/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000346/LER-1979-018-03, /03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily | /03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily | | | 05000346/LER-1979-019-03, /03L-0 on 790129:suction & Discharge Valves on Containment Spray Pump Were Closed.Caused by Personnel Error | /03L-0 on 790129:suction & Discharge Valves on Containment Spray Pump Were Closed.Caused by Personnel Error | | | 05000346/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000346/LER-1979-020-03, /03L-0 on 790205:10 of 18 Main Steam Safety Valves Found Outside Setpoint Range.Believed Caused by Changing Ambient Conditions at Valve Locations.Valves Adjusted & Retested Satisfactorily | /03L-0 on 790205:10 of 18 Main Steam Safety Valves Found Outside Setpoint Range.Believed Caused by Changing Ambient Conditions at Valve Locations.Valves Adjusted & Retested Satisfactorily | | | 05000346/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000346/LER-1979-021-03, /03L-0 on 790205:containment High Pressure Alarms Were Received & Safety Features Actuation Sys Channel 2 Erroneously Tripped.Cause Unknown.No Deficiencies Found from Surveillance Tests.Channel Returned to Operation | /03L-0 on 790205:containment High Pressure Alarms Were Received & Safety Features Actuation Sys Channel 2 Erroneously Tripped.Cause Unknown.No Deficiencies Found from Surveillance Tests.Channel Returned to Operation | | | 05000346/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000346/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000346/LER-1979-022-03, /03L-0 on 790208:diesel Fire Pump Battery Electrolyte Level in Four Cells Was Below Top of Cell Plates.Caused by Procedural Error.Levels Restored,Pump Declared Operable & Unit Removed from Action Statement | /03L-0 on 790208:diesel Fire Pump Battery Electrolyte Level in Four Cells Was Below Top of Cell Plates.Caused by Procedural Error.Levels Restored,Pump Declared Operable & Unit Removed from Action Statement | | | 05000346/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000346/LER-1979-023-01, /01T-0 on 790228:Startup Transformer 01 Taken Out of Svc;Surveillance Tests Not Performed within One Hour, Contrary to Tech Spec Requirements.Caused by Personnel Error.Testing Completed as Soon as Error Realized | /01T-0 on 790228:Startup Transformer 01 Taken Out of Svc;Surveillance Tests Not Performed within One Hour, Contrary to Tech Spec Requirements.Caused by Personnel Error.Testing Completed as Soon as Error Realized | | | 05000346/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000346/LER-1979-024-03, /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust | /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust | | | 05000346/LER-1979-025-03, /03L-0 on 790213:Ohio Edison Relay Testing Actuated Transfer Trip Receiving Relay & Tripped Switchyard Breakers.Caused by Failure of Util to Notify Toledo Edison Before Performing Relay Testing | /03L-0 on 790213:Ohio Edison Relay Testing Actuated Transfer Trip Receiving Relay & Tripped Switchyard Breakers.Caused by Failure of Util to Notify Toledo Edison Before Performing Relay Testing | | | 05000346/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | |
|