05000366/LER-1980-026-03, /03L-0:on 800314 During Local Leak Rate Testing, Hydrogen Recombiner Return Isolation Valve 2T49-F005B Had Unacceptable Test Results.Caused by Scratch on Seat Apparently Due to Valve Closing on Piece of Debris

From kanterella
(Redirected from ML19305C952)
Jump to navigation Jump to search
/03L-0:on 800314 During Local Leak Rate Testing, Hydrogen Recombiner Return Isolation Valve 2T49-F005B Had Unacceptable Test Results.Caused by Scratch on Seat Apparently Due to Valve Closing on Piece of Debris
ML19305C952
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 04/02/1980
From: Coggin C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19305C951 List:
References
LER-80-026-03L-01, LER-80-26-3L-1, NUDOCS 8004110476
Download: ML19305C952 (2)


LER-1980-026, /03L-0:on 800314 During Local Leak Rate Testing, Hydrogen Recombiner Return Isolation Valve 2T49-F005B Had Unacceptable Test Results.Caused by Scratch on Seat Apparently Due to Valve Closing on Piece of Debris
Event date:
Report date:
3661980026R03 - NRC Website

text

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (7 77)

LICENSEE EVENT REPORT -

CONTROL BLOCK: l l

l l

l l

lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) l 6

lC lA lE lI lH l2 l@l0 l 0 l -l 0 l 0 l 0 l 0 l 0 l - l 010 l@l 4 l 1 l 1 l 1 l 1 l@l l

l@

7 9

LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 40 57 CAT $8 c

p 10111d % "c' l Ll@l 0l Sl 0l 010 l 316 ] 6 l@l 0 l 3111418 l 0 l@l 014 l 01218 l 0 l@

7 8

60 61 OOCKET NUMBER 66 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEoVENCES h 10 I21 puring the performance of LLRTs while shutdown for a surveillance / vent i

10 : 3 l header deflector installation outage, hydrogen recombiner return isola-l [O l4 l $ ion valve 2T49-F005B did not have acceptable results ~ during its initial l lOls] gest.

There were no effects upon public health or safety due to this l

0 s pvent.

This is a repetitive event - see LER #50-366/1980-021.

I 10171I I

O s l I

80 7

8 9 DE CODE SUBC E COMPONENT CODE SUBCODE SU E

l0l9l l S l El@ [E_j@ l X l@ l V l Al Ll V [E l X l@ [E j@ lD l @

7 8

9 10 13 12 13 18 19 20 SEQUENTIAL OCCUR RE NCE REPORT r1EVISION LER EVENT YEAR REPORT NO.

CODE TYPE N O.

O ajg/RO l810l l-l l0l2l6l W

l0 l3 l lLl

[---j l0 l y

_ 21 22 23 24 26 27 28 29 30 31 32 [D

K N AC ON PL NT ET HOURS 22 SB IT FOR 8.

SU PLIE MANUFACTURER V l B l@LZj@

LZj@

lZl@

l0l0l0l0l

[_Y_J @

[N_j@

l A [@

l P l 3 l1 l2 l@

33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS lThe cause of the unacceptable leakage rate for this valve was a scratch 1 i O 11 111 I on the seat (apperently due to valve closing on piece of debris.)

Cor-1 i rective valve maintenance- (valv seat was lapped) was performed such I

i 2 til3i lthat the overall leakage rate for all Type B and C LLRTs will meet the l

FFTTlI.60La limit of Tech Specs section 3.6.1.2.b.1.

I 80 7

8 9 S

S

% POWER OTHER STATUS ISCO RY DISCOVERY DESCRIPTION li15I [G_j @ l 0l 01 0l @l NA l

l B l@l Local Leak Rate Test l

A TiVITY CO TENT RELE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE [Z_j @ [Z_J@l NA l

l NA l

i e 7

8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE

DESCRIPTION

1010 l0 l@lZ l@l NA l

i 7 PERSONN E L INJURt ES DESCRiPriON@

NuMsER 10 l 0 l0 l@l NA l

i a 7

9 11 12 80

'2*E "fS^"^? TION

'^c'"" @

[Z_j@l NA l

80 7

8 9 10 i[ssuE @oESCRiPTiON@

'8 0 0 4110 Nhll l l l l l l l l l l l l :;

"" C 'S't

"'Y l

NA l

2 o 68 69 80 5 I 7 8 9 to C. L. Coquin. Suot. Plt. Eng. Serv. psons: 912-367-7781 I,

NAME OF PREPARER

LER F:

90 ~466/1080-026 Licensee:

Georgia Powe" Compan y Facility Nane:

Edwin I.

Hatch Docket A:

50 166

Narrative

Report for LER 50-366/1080-026,

On 3-13-80, with the unit in cold shutdown for a

surveillance / vent header deflector installation outage, local leak rate testing being performed per H ?!P-2-? Q 9 2, PRI'4 A R Y CONT AI'IMENT PERIODIC TYPE B AND TYPE C LEAKAGE TESTS, showed that hydrogen recombiner "eturn isolation valve 2Tho-F0n9B was leaking in excess of specified criteria

("As Found" leakage was greater than 2200 actual cubic centimeters oer minutel.

Valve 2T4o-F004B is actually the isolation valve being tested;

however, 2Tho-F0053 is the " blocking valve" used as part of the boundary in order to test the F004B valve.
Thus, the Icakage must be attributed to both valves.

i The Icakage of valves 2T4Q-F004B and F005B is included as part of the.60La limit of Tech Specs section 3.6.1.2.b.1 This is a repetitive occurrence - see LER #go-966/1080-021 There was no effect upon public health or safety as a result of this event.

The cause of the unaccentable leakage rate for the valve was a scratch on the seat (apoarently due to valve closing on piece of debris).

Corrective maintenance consisted of lapping the valve seat.

The after-maintenance leakage was 20 actual cubic centimeters per minute.

This is not gen e r i,c a l t h ois::,h valve leakage during LLRTs is common to both units.

O D**D D 'T YM A $lnLa oo e

O i