ML19296B947

From kanterella
Jump to navigation Jump to search
/03L-0:on 800108,while Performing Relief Valve Setpoint Check,Reactor Vessel 1105A Actuated at 1,600 Psig & Reactor Vessel 1105B Actuated at 1,500 Psig.Possibly Caused by Setpoint Drift.Valves Will Be Repaired
ML19296B947
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 02/07/1980
From: Vahrenwald J
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19296B938 List:
References
80-001-03L, 80-1-3L, NUDOCS 8002220404
Download: ML19296B947 (1)


Text

NRC FOPM 366 U.S. NUCLEAR REGULATORY COMMISSION (7 77)

~

LICENSEE EVENT REPORT CONTROL BLOCK: l l

l l

l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6

@ ll l L l Q l A l D l 2 l@l0 l0 l 0 l - l 0 l 0 l 0 l - l 0 l 0 l 0 l@l 4 l 1 l I l1l1l@l l

l@

7 8 9 LICENSEE CODE 14 15 LICENSE NUMSER 25 26 LICENSE TYPE J0 5 7 CAT 58 CON'T

" C] l L @! ') l 51 0l 0 l 0 l 2 l 6 l 5 l@l 0 l 1 l 0 l 8 l 8 l 0 l@l 0 210 l7 l8 l0 l@

g, O

i 7

8 60 61 DOCKET NUM8ER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBAJLE CONSEQUENCES h

[OTTl While performing SBLC Relief Valve Setpoint Check, procedure QOS 1100-4, Relief f0TTlI valve RV 1105A actuated at 1600 psig and relief. valve RV 1105B actuated at 1500 psig. l The Technical Specification 4.4.A.2 limits for SBLC relief valves is 1400-1490 psig. l 0

4 gl The increased setpoints of the relief valves were still within the design pressure g

101s 1 l rating of the SBLC piping.

Subsequently the SBLC system was operable and would have l (O l 7 l l performed had the need arose.

l 0

s i I

80 7

8 9 E

C00 SUSCO E COMPONENT CODE Sub OD'E SU E

E lSlH h {h l Bl@ lV l A lL lV E lX l@ W@ W @

7 8

9 10 11 12 f3 18 19 20 SEQUENTIAL OCCUR RE NCE REPORT REVISION EVENT YE AR REPORT NO.

CODE TYPE NO.

h g"LER.ROl21dl 0l l-l l0l0l1l y

l0 l3 l W

[--.]

l 0l Ug E

22 23 24 26 27 28 29 30 31 32 N A O

O PL NT MET HOURS 22 S8 IT POR 8.

SUPPLI MA UFACTURER l x [gl34B l g l5 Z lg

[36Zl@ l0l0l0l l

lN g Ylg N[g lC l 7l ll 5lg 33 3

37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O I The apparent cause of this occurrance is setpoint drif t.

Unit Two is presently l

i i l

shut dOwn for refueling and the valves will be repaired or replaced, and satisfactorily m

tested before starting up.

A supplemental report will be issued when all l

l corrective actions have been completed.

l i

4 I

i 7

8 9 80 ST

% POWER '

OTHE R STATUS IS O P DISCOVERY DESCRIPTION NA l

W @l Survei11ance Test l

W lHlh l0l0l0lhl ACTIVITY CONTENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RE 8

NA l

l NA l

l.,Ll6.J [_Z,,j h l Zl@l 7

6 3 10 11 44 45 80 PERSONNEL EXPOSURES l 0 l 0 l O lhl TYPE @l DESCRIPTION NUMBER Zl NA l

i 7

PERSONNE L INJURIES NUMBER DESCRIPTION NA l

l 0l 0 0l@l i

a 7

8 9 11 12 80 LOSS OF OR DAMAGE TO FACIL TY 80 % 220

  1. 6Y-l TYPE DESCRIPTION W l Zlgl NA 7

8 9 10 80 Lus I I N hl DESCRIPTION ISSUE NA l

lllllllllllll1 7

8 9 10 68 69 W. :ll NAME OF PREPARER PHONE: