ML19294A369
| ML19294A369 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 10/05/1978 |
| From: | Zufelt E POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | |
| Shared Package | |
| ML19294A368 | List: |
| References | |
| NUDOCS 7810130132 | |
| Download: ML19294A369 (4) | |
Text
OPER \\ TING DATA REPORT DOCKET NO 50-333 DATE.Oct. L.J.978 COMPLETED llY E. Zufelt TELEPliONE (315TM-3840 OPER ATING STATUS i
FitzPatrick Note
- I
- 1. Unit Name:
- 2. Reporting Period:
780901-780930 2436
- 3. Licensed Thennal Power (MWt):
- 4. Nameplate Rating (Gross MWe):
883
- 5. Design Electrical Rating (Net MWe):
821 830
- 6. Maximum Dependable Capacity (Gross MWe):
800
- 7. Maximum Dependable Capacity (Net MWe):
- 8. If Changes occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report.Gise Reasons:
Ibne
' 9. Power Level To Which Restricted,if Any (Net MWe): 615 Nuclear Reactor Regul
' Pending resclution, with the USNRC Division o1
- 10. Reasons For Restrictions.lf An'a: tion, of Analyses relating to the possible effects of mitiple safety relief valve actuatinns follrwincr a roncent innlarinn ovone.
This Month Yr..to.Date Cumularise
- 11. Ilours in Reporting Period 720 6551 27864
- 12. Number Of !!ours Reactor Was Critical 360.9 5901.1 21482
- 13. Reactor Resene Shutdown llours 0
0 0
- 14. Ilours Generator On.Line 349.6 5818.1 20790.2
- 15. Unit Restne Shutdown flours 0
0 0
- 16. Gross Thermal Energy Cecerated (MWil) 555240 12288452 41550116 17 Gross Electrical Energy Genented (Mwil) 184600 4140250 14081300 lb. Net Electrical Energy Generated (Mw!!;
178150 3991615 13620270
- 19. Uait Senice Factor 48.6%
88.8%
74 g
- 20. Unit Asailability Factor 48.6%
88.8%
74.6%
30.9%
76.2%
70.5%
- 21. Ur:. 'amcity Far'or (Using MDC Net) 30.1%
74.2%
59.5%
- 22. L., t Ca,,acity Factor (Using DER Net)
- 23. Unit forced Catage Rate 4.2%
3.7%
10.5%
- 24. Shutdowns Scheduled Oser Nest 6 Months t ry pe. Date.and Duration of Each):
lbne November 13, 1978
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status t Prior to Commercial Operation)
Forecast Achiesed INill \\L CRillCAI.ll Y INillAL ELECTRICITY CO\\1\\lERCI \\L Ol'f R All0N 7 Fr to t 3 o f 3 2.
AYl:It AGE D \\fl Y UNII pow ((t g,0yLL DOCKET NO.
50-333 tJNIT JAFNPP D iIE Oct. 5, 1978 E. Zufelt CO\\lPLETED BY TELEPil0NE (315)342-3840
.\\f 0 Nill Septmter 1978 DAY AVEll AGE DTILY POWElt LEVEL DAY AVER AGE DTILY POWElt I.EVEL Dih e-Net )
O!We Net t i
562 17 0
564 18 0
3 563 19 0
4 563 20 0
5 561 0
21 6
365 o
7 561 0
23 179 g
24 0
9 349 25 0
10 468 26 0
11 480 27 0
497 12 2s 0
13 498 29 0
501 34 30 0
474 15 y
38 16 SGM1RY: The unit was operating in a derated condition until September 16 when it was shut down for the refueling outage.
% -333 DOGET NO.
UNIT SIIUTDOWNS AND POWER REDUCTIONS UNIT N AS!E JAFNPP DATE __Oct. 5, 1978 CostPLETED Ity
_E.
Zufelt REPORT Sf 0NTi{
Sect &ber T EI EPilONE (315)342-3840 r.
N
=_
ei
?w a 5
Er
(
,s4 Licensee 5-r Fu Cause & Correctne o
No.
Date g
3p
.j g 5 Event 3?
c1 '
Action tii 55 5
j5g Report 2 LA 0 Present Recurrence c5 15 780908 F
15.5 G
3 NA NA NA Inadvertent loss of sealing steam 16 780916 S
354.9 C
2 ra NA NA Refueling outage i
t 3
4 I
F: Forced Reason:
Method :
Estabit G - Instruttions S: St hed uled A Equipment Failure (Explain) 14f anual for Piccaraiion i,1 luta ll4taintenance of Test 24tanual Scram.
Entr.s sheets f oi 1.icensee C-Refueling 3 Automatic Scram.
Inent Report (1.1 R) File (NUREG-D Regulatory Restriction 4-Ot her ( Explain )
0161)
E-Operator 1 raining & Iicense Examir-F Administratne 5
G-Operational Er ror (Explain)
Inhibit 1 - San e Sonrce (9/77)
II Other (Explain)
POWER AUTIICRITY OF TIIE STATE OF IEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PIAVI' NARRATIVE SUBfGRY OF OPERATING EXPERIDK'E SEPIDEER 1978 During the period frcm September 1,1978 until September 15, 1978 the unit operated in a derated condition. On September 9, 1978 the reactor scramed due to iandvertent loss of sealing steam.
On Septerrber 15, 1978 started reactor shutdown for scheduled refueling outage.
PONER AUT110RITY OF Tl!E STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT Safety Related Electrical 6 Mechanical Maintenance Summary SEPTEMBER 1978 UORK REQUEST A REPAIR DATE SYSTE.At fl0W DETECTED CAUSE OF mal. FUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME COMPONENT g
!!0URS 9/7/78 02 11771 Remove old FN sparger Replace with improved design FW Spargers from vessel 9/26/78 03 11569 Ilearing End of normal life Replace coil 2
03-ilCU-06-11 9/20/78 08 10907-N/A N/A End of normal life Reverse reel windup direction a0 9/6/78 14 11735 14-MOV-12A Surveillance Valve disc stuck in seat liigh DP across the seat 2
9/12/78 17 11765 17-RM-453B Inspection Loss of oil New pump on order 1
9/14/78 27 10921-SOV 128B 27-SOV-123B Surveillance Shorted solenoid coil Not resolved 10 8/22/78 36 1391-TCil-6ASB N/A Megger intake DE-ice N/A 20 heaters (F-ST-81) 8/31/78 L
76 11724 Fire damper Surveillance Mechanism caught when Minor adjust operated 9/6/78 93 8941 Loose insulation on 93-EDG-A Inspection muffler due to wind Replaced insulation and covered 15 and rain 8/28/78 93 11666 Inspection-Pump out of alignment Realigned 93-P-2A Noisy
JAMES A. FITZPATRICK NUCLEAR PCWER PLANT Maintenance Sunn:ary I 6 C 1978 Work Request #
Cause of Results of Action taken to Repair Date Systen U"
Component #
Malfunction Malfunction Preclude Tice Recurrence (Hours) 9/25/78 02 ISP-42 Unknown liigh Contact p
02 -I,S-71 G Resistance 12021 9/25/78 02 OPS None 02 'IT-157 BSD No readings None 6
9/25/78 02-3 OPS Unknown 02 85A Downscale Recal 12 11993 9/25/78 02-3 OPS Age No response Replaced parts 8
02-3-CR-98 11750 9/11/78 02-3 F-ISP-3-1 Bad switch Incorrect 02-3-LIS-58A Replaced switch 40 Setpoint 11708 Cannot use 9/25/78 02-3 Testing Bad valve 02-3-PS-51B isolation valve Replaced valve 3
11934 9/25/78 02-3 OPS Age Bad indication IMP-2-3.4 10 02-3-LR-98 11991 liigh Contact 9/25/78 02 02-PS-71K ISP-42 Unknown Replaced 2
Resistance 9/25/78 02 11992 liigh Contact ISP-42 Unknown 02-PS-71b.
Resistance R@wd 2
9/12/78 07 PS Unknown Spiking IMP-7.16 4
LPRhl 6-05C 9/16/78 07 F-ISP-71 N/A No Comp Point N/A found ok 1
SRM Comp Pt.
11787 Oscillatind Replaced 9/20/78 07 F-ISP-71 Age dbofg!s SRM A Power Supply
JAMES A. FITZPATRICK NUCLEAR PCWER PLANT Flaintenance Sumary I 6 C 1978 il rk Reouest #
Cause of Results of Action taken to Repair Date System Ilow Detected Conponent n F!alfunction F!alfunction Preclude Time Recurrence (flours) 11968 9/25/78 07 07-R-45 OPS Dirt Sluggish Cleaned bearings 5
11767 9/14/78 08 Limit switches OPS N/A N/A Checked okay 3.5 11775 Reversed Polarit"y 48 9/14/78 08 Speed Cont.
OPS Inc rrect Polarit) No speed cont.
of turb gen 11777 Replaced limit 18 9/8/78 08 Slack cable LS OPS Bad limit switche Incorrect ind.
switch 11917 8
9/29/78 17 17-IB!-456A OPS Age /Use Erratic fl.V.
Replaced parts 11585 4
9/19/78 23 23-CT-207C OPS Unknown liigh Reading ISP-24-2 8/30/78 70 70-D1 1A/111B OPS
'E E" ng pr e r 1 >*
p nd.
4 8/30/78 70 Adjusted G cal.
70-FF1-18A OPS Lubrication incorrect 11709 8
9/1/78 76 Lo se screws Elect. Shock Tightened screws 76-SD-81 OPS 11717 16 9/12/78 l 76-SD-51 4 52 F-ST-76J18 Bad relay No alarm Replaced relay 76 6
@ d M ay 9/12/78 76-
)-
1 11769 9/12/78 76 F-ST-76J9 Bad relay No alarm Replaced relay 16 76-SD-29
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