ML19291B934

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Monthly Operating Rept for Nov 1979
ML19291B934
Person / Time
Site: Cooper Entergy icon.png
Issue date: 12/07/1979
From: Ballinger P
NEBRASKA PUBLIC POWER DISTRICT
To:
Shared Package
ML19291B932 List:
References
NUDOCS 7912140399
Download: ML19291B934 (4)


Text

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OPERATING DATA REPORT DOCKET NO. 050-0298 DATE 12-7-79 COMPLETED BY P. L. En111nger TELEPHONE 402-825-3811 OPERATING STATUS .

Cooper Nuclear Station Notes

1. Unit Name:
2. Reporting Period: November 1979 2381
3. Licensed Thermal Power (MWt):
4. Nameplate Rating (Gross MWe): 836
5. Design Electrical Rating (Net MWe): 778
6. Maximum Dependable Capacity (Gross MWe): 787
7. Maximum Dependable Capacity (Net MWe): 764
8. If Changes Occur in Capacity Ratings (Items Number .1 Through 7) Since Last Report. Give Reasons:
9. Power Level To which Restricted,if Any (Net MWe): None
10. Reasons For Restrictions. If Any: N0ne This Month Yr. to.Date Cumulative
11. Hours in Reportin; Period 720.0 9d16.0 47.407.0 _
12. Number Of Hours Reactor Was Critical 581.1 7038.4 40.441.1
13. Reactor Reserve Shutdown Hours 0.0 0.0 0.0
14. Hours Generator On.Line 571.2 6928.4 39,731.6
15. Unit Reserve Shutdown Hours nn nn nn
16. Gross Thermal Energy Generated (MWH) 1.126.128 14.117.784 74.541.942
17. Gross Electrical Energy Generated (MWH) 375,084 ,

4.633,548 23.991.434

18. Net Electrical Energy Generated (MWH) 361,521 4,466,581 23,129,920
19. Unit Service Factor 79.3 86.4 83.7
20. Unit Availability Factor 79.3 86.4 83.7
21. Unit Capacity Factor (Using MDC Net) 65.7 72.0 61.7
22. Unit Capacity Factor (Using DER Net) 6Q 71.6 62.6
23. Unit Forced Outage Rate 20.7 4.2 4.7
24. Shutdowns Scheduled Over Next 6 Months (Type. Date,and Duration of Each1:

Re fnpling and M14ntennnce. Mnrch 15. 1980. 8 weeks

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units in Test Status iPrior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 1579 356 7912140.3 7 7 rum

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 050-0298 UNIT Cooper Nuclear Stat.

DATE 12-7-79 COMPLETED BY P. L. Ballinger TELEPHONE 402-825-3811 MONTH November DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) g 737 j7 0 2 727 ig o 3 727 g9 0 4 713 20 3 5 739 21 383 6 771 22 544 7 722 611 23 8 722 24 601 9 722 25 569 10 713 26 705 419 27 692 12 522 ;g 697 13 434 697 29 14 261 30 694 15 0 31 16 0 INSTRUCTIONS On this format.!ist the average daily unit power levelin MWe Net for each day in the reporting month. Compute to the nearest whole megawatt.

(9/77) 1579 357

DOCKET NO.

050-0298 UNIT SilUTDOWNS AND POWER REDUC 110NS UNIT N AME Cooper Nuclear Stat.* '

DATE 12-7-79 COMPLETED BY P. L. Ballinger REPORT MON 111 November 1ELEPil0NE 402-825-1R11 e.

- E c 5; *

'E Licensee Et E"1. Cause & Corrective No. Date F

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~$ Event Report #

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u Action to Prevent Recurrence 6

79-12 791111 S 0 H 4 N/A N/A N/A Power was reduced to allow the ex-change of control rod patterns and to test the turbine control system.

79-13 791113 F 5 H 4 50-298-79-37 Diesel generator #1 & #2 were inoper-able at the same time. Power was re-duced for a normal station shutdcwn as required by Tech. Specs. Diesel gen-erator #1 was subsequently repaired and shutdown terminated. The reactor was returned to a reduced power oper-ation pending repair and inspection of the #2 diesel generator.

79-14 791114 F 148.8 A 2 50-298-79-36 Reactor was shutdown because the re-pair and annual inspection of the #2 diesel generator was not completed in seven days as required by the Tech.

snnce. nfocoi gonor,en. M7 ugg .g_

m paired, inspected and tested and the reactor M F: Forced Reason: Method: " 0 E Nt d M fruEOS Is" I "'

N S: Scheduled A Equipment F .ilure(Explain) 1 -Manual for Preparation of Data d B Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee C. Refueling 3 Automatic Saam. Event Report (LER) File (NURI.G-4 D-Regulatory Restriction 4-Other (Explain) 0161)

. .J1 E-Operator Training & Ucense Examination m F-Administrative 5 Eshibit I - Same Source G-Operational Error (Explain)

(9/77) Il-OLher (Explain)

COOPER NUCLEAR STATION OPERATIONS NARRATIVE November 1979 Power was reduced on November 11, 1979 to allow the exchange of control rod patterns (Sequence A-2 to Sequence B-2) and to test the turbine control system.

On November 13, 1979, diesel generator #1 would not start during per-formance of a surveillance procedure and was declared inoperable.

Diesel generator #2 was undergoing its annual inspection and thus was also inoperable. Power was reduced for a normal station shutdown as required by Technical Specifications. Diesel generator #1 was sub-sequently repaired, tested, and declared operable and the shutdown terminated. The reactor returned to reduced power operation pending completion of repair and annual inspection of the #2 diesel generator.

Reactor was shutdown on November 14, 1979 because the repair and annual inspection of the #2 diesel generator was not completed in seven days as required by Technical Specifications. The diesel generator #2 was repaired, tested, and declared operable and the reactor returned to normal operation after a 148.8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> outage.

Reactor operated with no additional unscheduled power reductions or outages for the balance of the month.

1579 359

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