ML19290E994
| ML19290E994 | |
| Person / Time | |
|---|---|
| Site: | Yankee Rowe |
| Issue date: | 03/12/1980 |
| From: | Beers F YANKEE ATOMIC ELECTRIC CO. |
| To: | |
| Shared Package | |
| ML19290E993 | List: |
| References | |
| NUDOCS 8003170425 | |
| Download: ML19290E994 (5) | |
Text
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YANKEE ATOMIC NUCLEAR POWER STATION MONTHLY STATISTICAL REPORT 80-02 FOR THE MONTH OF FEBRUARY,1980
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l L.a OPERATING DATA REPORT 0-29 DOCKET NO.
DATE 800312 CO31PLETED BY v.
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Beers TELEPHONE A17 16 A-9011 X2215 OPERATING STATUS Yankee Rowe Notes
- 1. Unit Name:
February, 1980
- 2. Reporting Period:
600
- 3. Licensed Thermal Power (31Wt):
185
- 4. Nameplate Rating (Gross 31We):
175 S. Design Electrics! Rating (Net 31We):
180
- 6. Sis.timum Dependable Capacity (Gross StWe):
175
- 7. 31s.ximum Dependsb!e Capscity (Net 31We):
- 8. If Changes Occur in Capacity P stings (Items Number 3 Through 7) Since Last Report. Gise Reasons:
- 9. Power Level To Which Restricted. If Any (Net 31We):
- 10. Reasons For Restrictions.If Any:
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This alonth Yr..to Date Cumulatiye i
t 696 1,440 I1. Hours In Reportin2 eriod P
6.07 445.77 138,810.42
- 12. Number Of Hours Resctor Was Critics!
0.0 0.0 0.0
- 13. Resctor Reserve Shutdown Hours 14, Hours Generator On Line 0.0 439.7 134',467.31
- 15. Unit Reserve Shutdown Hours 0.0 0.0 0.0
- 16. Gross Thermal Energy Genersted (31WH) 0.0 213.769 72.002,091.11 1
0.0 80,635 22,152,788.2
- 17. Gross Electries! Energy Genented (31WH) 0.0 75,748.88 20,741,892.21
- 18. Net Electrical Energy Generated (31WH)
- 19. Unit Service Factor 0.0 30.5 79.5 0.0 30.5 79.5
- 20. Unit Availability Factor 0
30 72.4
- 21. Unit Capscity Factor (Using SIDC Net) 0 30 72.4.
- 22. Unit Capacity Factor (Using DER Net) 100 61.3 2.1
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- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Over Next 6 Slonths (Type. Date.snd Durstion of Each1:
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- 25. If Shur Down At End Of Report Period. Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercist Operation):
Forecast Achieved INITIA L CRITICA LITY INITIA L ELECTRICITY CO3131ERCIAL OPERATION
'(9/77)
AVERAGE DAILY UNIT POWER LEVEL [
g DOCKET NO.
50-29 UNIT Yankee Rowe DATE 800312 COMPLETED BY F. C. Beers 617-366-9011 X2215 TELEPHONE MONTH February, 1980 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net)
(MWe. Net) 1 0.0 37 0.0 0.0 0.0 2
33 0.0 3
0.0 39 0.0 0.0 4
20 5
0.0 21 0.0 0.0 0.0 6
22 0.0 0.0 7
23 0.0 0.0 3
9 0.0 25 0.0 0.0 10 0.0 26 0.0 11 0,0 27 12 0.0 0.0 28 13 0.0 0.0 29 0.0 14 30 15 0.0 3,
0.0 16 INSTRUCTIONS On this format. list the average daily unit power levelin MWe. Net for each day in the reporting month. Compute to the nearest whole megawatt.
v-(9/77)
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UNITSituTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-29 UNIT NAME Y:mkee Roug, DATE 800312 COMPLETED liY F.
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Beers REPORT MONTII _ Fohru,ry. 1980 TELEP1 TONE 617-166-9011 X2215 "i
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Event u?
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Psevent Itecursence 6
1 1/19/80 F
696 D&A 1
N/A N/A N/A The plant was shut down to install voltage regulators and make TMI re-lated changes until 2/5/80. Remained shut down until 2/12/80 to repair main coolant pump flange leak.
Re-mained shut down the rest of the month due to turbine rotor failure.
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Method:
Exhibit G -Insieuctions S: Schedialed A Eipiipment Failure (Explain) 1 Manual fo. Picparation of Data B-Maintenance of Test 7-Manual Sesam.
Entry Shecis fos I.icensee C.Itefueling 3 Aufomatic Scram.
Event ;tepml (Llilt! File INult!'.G-5D D.Itegulaimy Restriction 4 Other (Explain) 0161) p, E-Opesator Training & License Examination F Aihniniusative 5
G Operational Iuser (limplain)
Exhibit I Same Sonice l'8/31) 11 Othes Ilixplain)
DOCKET NO.
50-29 UNIT Yankee Rowe DATE 800312 COMPLETED BY F. C.
Beers TELEPHONE 617-366-9011 X2215 REPORT MONTH February, 1980 SU' NARY OF OPERATING EXPERIENCES 2/1 At 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> commenced a plant startup from cold shutdown (Mode 5) per OP-2100.
2/5 At 1332 hours0.0154 days <br />0.37 hours <br />0.0022 weeks <br />5.06826e-4 months <br /> commenced a plant cooldown to make repairs on a flange leak on No. 3 Main Coolant Pump.
(PIR 80-4) 2/6 At 0410 hours0.00475 days <br />0.114 hours <br />6.779101e-4 weeks <br />1.56005e-4 months <br /> the plant was in cold shutdown (Mode 5).
2/12 At 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> commenced a plant startup from cold shutdown (Mode 5) per OP-2100.
2/14 At 1135 hours0.0131 days <br />0.315 hours <br />0.00188 weeks <br />4.318675e-4 months <br /> the plant experienced a turbine trip during startup.
Began cooldown to investigate turbine damage.
(PIR 80-5) 2/16 At 1155 hours0.0134 days <br />0.321 hours <br />0.00191 weeks <br />4.394775e-4 months <br /> the plant was in a cold shutdown condition (Mode 5).
Subsequent investigation revealed exter. iive damage to first six rows of blades on both sides of L.P. turbine rotor.
2/29 Plant remained shut down in Mode 5 at the end of the report period.
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