05000346/LER-1978-066-99, /99X-1:on 780429,during Operation at 20% Power, RCS Pressure Dropped to Approx 1620 Psig & Safety Features Actuation Sys Channels 1 & 3 Tripped on RCS Low Pressure, Initiating Incident Levels 1 & 2

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/99X-1:on 780429,during Operation at 20% Power, RCS Pressure Dropped to Approx 1620 Psig & Safety Features Actuation Sys Channels 1 & 3 Tripped on RCS Low Pressure, Initiating Incident Levels 1 & 2
ML19289D334
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 07/28/1978
From: Batch S
TOLEDO EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19289D331 List:
References
LER-78-066-99X, LER-78-66-99X, NUDOCS 7903050342
Download: ML19289D334 (1)


LER-1978-066, /99X-1:on 780429,during Operation at 20% Power, RCS Pressure Dropped to Approx 1620 Psig & Safety Features Actuation Sys Channels 1 & 3 Tripped on RCS Low Pressure, Initiating Incident Levels 1 & 2
Event date:
Report date:
3461978066R99 - NRC Website

text

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8 l During a transient on 4/29/78 while the unit was in the process of shutting down o 2 System l

10131 I maintenance outage and was operating at 20% reactor power, Reactor Coolant j

I o la 1 L(RCS) pressure dropped to approximately 1620 psig and Safety Features Ac This initiated j

I (SFAS) Channels 1 and 3 tripped at 0553 hours0.0064 days <br />0.154 hours <br />9.143518e-4 weeks <br />2.104165e-4 months <br /> on RCS low pressure.

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incident levels 1 and 2.

There was no danger to the health and safety 1o is 1 I No actual loss of coolant accident occurred.

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40 41 CAUSE DESCRIPTION AND CCRRECTIVE ACTIONS h Systen j l The cause of this high pressure iniection actuation was a low Reactor Coolant i o [i li l l pressure trip resulting from the opening of feedwater valves. The enusa of the food-of the feedwater system while i

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