LER-1979-024, /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3461979024R03 - NRC Website |
|
text
NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7 771 LICENSEE EVENT REPORT CONTFX)L BLOCK:
l l
l l
l lh (PLEASE PRINT OR TYPE alt REQUIRED INFORMATION) i 6
l 0 l H l D l B l S l 1 l@l 0 l 0 l-l 0 l 0 l N l P l F l-0 l 3 l@l 4 l 1 l 1 l 1 l 1 l@!
l l@
o 1 7
8 9 LICENSEE CODE 14 15 LICENSE NUMBEH 2h 26 LICENSE T YPE JJ 5 7 C A T b6 CON'T 10111 3$n"c l L l@l 0 l 5 -l 0 l - l 0 l 3 l 4 l 6 @l 0 8 2 11 l 4 l 7 l 9 @l 0 l 3 l 1 l2 7l9l@
7
?
8 60 61 DOCKET NUVBER 68 63 kVENT DATE 74 7b REPORT DATE 80 EVENT DESCRIPTIC,N ANC PROB ABLE CONSEQUENCES h l On 2/14/79, investigation of an alarm signal from fire alarm panel C4706 indicated thel o 2 j laundry room detector DS8630 as the source.
Continued investigation revealed no obscrt o 3 [o TTI Ivable cause for the alarm. Attempts to clear the alarm failed and at 2145 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.161725e-4 months <br /> on l
IbE I 2/14/79, the detector DS8630 and associated panel C4706 were declared inoperable, I
o e l Placind the unit in the Action Statement of T.S. 3.3.3.8.
At 2235 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.504175e-4 months <br /> on 2/14/79, l
l maintenance personnel successfully reset DS8630, rcsnoving the unit from the Action I
o 7 l Statement of T.S. 3.3.3.8.
There was no danger to the public or unit personnel.
o a
'#e' suaCO5E C
C0D COMPONENT CODE SUBC DE S
E g
lAlB @ ]@ W@ l Il Nl Sl Tl Rl Ul@ W@ ]@
7 8
9 10 11 12 13 la 19 20 SEQUENTI AL oCCURAENCE REPORT REVISION L E R. RO EVENTYEAR REPORT NO.
CODE TYPE NO.
@ REPgsT 7l 9l
[__. )
l 0l 2l 4l y
l0l3l l Ll l.--J 0l
_ 21 22 2J 24 26 27 28 29 Ju 31 32 K
ACT Of ON PL ANT Hb HOURS 22 5 8 IT D FOR b H.
SUPPLIE MAN FACTURER lA lg[34.Zl g l Zl g lZ [g l 0l 0l 0l l
C@
lN l g lA l@
l J l 0 l 7 l 3 l@
33 35 30 3/
40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lilol The exact cause of this occurrence is undetermined.
Investigation of the equipment and g,,, g jdetector by maintenance personnel f ailed to find any equipment malfunction.
It is I
j ossible that gases or dust given off during normal laundre operation may have caused l p
l the detector to alarm. Attempts to substantiate this have proven inconclusive.
l g,
3 jDetector DS8630 was replaced.
l i 4 7
8 9 80 STA S
'4 POWE R oTHE R STATUS ISC V HY DISCOVERY DESCRIPTION l1151 l El@ l 0l 8 l 6l@l NA l
lA l@l Operator observation l
ACTIVITY CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION oF l'.ELEASE l1 l61 b @ l Z lgl NA l
lNA l
7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMB E R TYPE
DESCRIPTION
101010 l@l Zl@l NA l
i 7
PE RSONNE L INJURIES N U"B E R CESCRtPTION l
l l
l NA l
1 H
7 8 9 11 12 80 LOSS OF OR DAVAGE TO FACILITY 43 TYPE D E SC RIP TION (Z l@l NA Ii 9
10 80 7
8 9 PUBLICITY NRC USE ONLY
,,,,, 'ggrescgI "
790316012o
,,,,,,,,,,,jg 7
8 9 10 68 69 80 = ;
M 79-032 km hh WGbM, M. M g
g,ggg,png, ggg pgggg i
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-28 DATE OF EVENT: February 14, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Fire alarm panci C4706 inoperable due to erroneous detector The unit was in Mode 1, with Power (MWT) = 2375, Conditions Prior to Occurrence:
and Load (Gross MUE) = 795.
At 2141 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.146505e-4 months <br /> on February 14, 1979, investigation of Description of Occurrence:
an alarm caused by a signal frem panci C4706 indicated detector DS8630 (laundry room detector) as the signal source.
Continued investigation revealed no observa-ble cause for the alarm condition. Several n':ccmpts to clear the apparently spuri-ous alarm f ailed, and at 2145 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.161725e-4 months <br /> on February 14, 1979, the detector DS8630 and associated panel C4706 were declared inoperable. Although DS8630 is not a required detector per Technical Specifications, the fact that it was continuously alarming through panel C4706 rendered the panel incapable of alarming from any of its other This some of which are required by Technical Specifications.
associated detectors, placed the unit in the Action Statement of Technical Specification 3.3.3.8.
At 2235 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.504175e-4 months <br /> on February 14, 1979, maintenance personnel successfully reset DS8630.
This removed the unit from the Action Statement of Technical Specification 3.3.3.8.
Designation of Apparent Cause of Occurrence:
The exact cause of this occurrence is undetermined. Investigation of the equipment and detector by maintenance personnel f ailed to find any equipment malfunction.
It is possible that gases or dust given of f during normal laundry operation may have caused the detector to alarm.
Attempts to substantiate this have proven inconclusive.
There was no danger to the health and safety of the public Analysis of Occurrence:
or to unit personnel. No fires occurred during this time.
Corrective Action
Upon declaring panel C4706 inoperable, an immediate search of all area monitored by the panel.was performed. Maintenance personnel were advised A fire of the probica, and the equipment was checked for possible malfunction.
watch was instituted 'n accordance with Technical Specification 3.3.3.8.
Detector DS8630 was replaced on February 22, 1979 under Maintenance Work Request URO 13-8-79.
There has been one previous reported occurrence of erroneous detector Failure Data:
operation, see Licensee Event Report NP-33-79-22.
LER #79-024
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000346/LER-1979-001-03, /03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator | /03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator | | | 05000346/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000346/LER-1979-002-03, /03L-1 on 790102:main Steam Valves 106 & 106A Failed to Open,Resulting in Auxiliary Feed Pump Afp 1-1 Being Taken Out of Operation.Caused by Dirt Buildup on Valve Stems as Result of New Const | /03L-1 on 790102:main Steam Valves 106 & 106A Failed to Open,Resulting in Auxiliary Feed Pump Afp 1-1 Being Taken Out of Operation.Caused by Dirt Buildup on Valve Stems as Result of New Const | | | 05000346/LER-1979-002, Forwards LER 79-002/03L-1 | Forwards LER 79-002/03L-1 | | | 05000346/LER-1979-003-03, /03L-0 on 790104:control Room Emergency Ventilation Sys Damper HV5311E Inoperable.Caused by Leaking Pneumatic Operator.New Operator Installed.Damper Operated & Tested for Response Time & Declared Operable | /03L-0 on 790104:control Room Emergency Ventilation Sys Damper HV5311E Inoperable.Caused by Leaking Pneumatic Operator.New Operator Installed.Damper Operated & Tested for Response Time & Declared Operable | | | 05000346/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000346/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000346/LER-1979-004-03, /03L-0 on 790105:failure to Post Guards at Entrance to Containment During Periods of Free Access. Caused by Personnel Error.Special Order 84 Revised to Require Posting of Guards | /03L-0 on 790105:failure to Post Guards at Entrance to Containment During Periods of Free Access. Caused by Personnel Error.Special Order 84 Revised to Require Posting of Guards | | | 05000346/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000346/LER-1979-005-03, /03L-0 on 790106:during Surveillance Testing, Borated Water Storage Tank Level Bistable Was Tripped;Valves DH9A Opened & DH7A Closed.Caused by Component Failure of Output Relay K51A & Instrument Drift | /03L-0 on 790106:during Surveillance Testing, Borated Water Storage Tank Level Bistable Was Tripped;Valves DH9A Opened & DH7A Closed.Caused by Component Failure of Output Relay K51A & Instrument Drift | | | 05000346/LER-1979-006-03, /03L-0:on 790105,reviewer Noted 781228 Record of Continuous Alarm at Contact Data Record Point F018.Panel C4705 Not Reset.Caused by Failure of Indicator Lights on Panel C4705.Panel Reset,Clearing F018.Surveillance Modified | /03L-0:on 790105,reviewer Noted 781228 Record of Continuous Alarm at Contact Data Record Point F018.Panel C4705 Not Reset.Caused by Failure of Indicator Lights on Panel C4705.Panel Reset,Clearing F018.Surveillance Modified | | | 05000346/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000346/LER-1979-007-03, /03L-0 on 790110:during Performance of Surveillance Test,Channel 2 of Containment Hydrogen Analyzer Was Found Inoperable.Caused by Defective Zener Diode in Millivolt Converter | /03L-0 on 790110:during Performance of Surveillance Test,Channel 2 of Containment Hydrogen Analyzer Was Found Inoperable.Caused by Defective Zener Diode in Millivolt Converter | | | 05000346/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000346/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000346/LER-1979-008-03, /03L-0 on 790109:during Surveillance Testing, Containment Recirculation Fan 1-1 Failed to Run.Cause Attributed to Buildup of non-conductive Film on Auxiliary Controller Contacts | /03L-0 on 790109:during Surveillance Testing, Containment Recirculation Fan 1-1 Failed to Run.Cause Attributed to Buildup of non-conductive Film on Auxiliary Controller Contacts | | | 05000346/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000346/LER-1979-009-03, /03L-0:on 790112,power to Vital Bus Y2 Lost. False Integrated Control Sys Signal Resulted in Reactor & Full Steam & Feedwater Rupture Control Sys Trip.Caused by Blown 125 Volt DC Fuse to Inverter | /03L-0:on 790112,power to Vital Bus Y2 Lost. False Integrated Control Sys Signal Resulted in Reactor & Full Steam & Feedwater Rupture Control Sys Trip.Caused by Blown 125 Volt DC Fuse to Inverter | | | 05000346/LER-1979-010-03, /03L-0:on 790112,Sys 7 Data Logger Experienced Core Dump,Voiding Computer Memory Bank Which Rendered Remote Monitoring of Fire Detection Sys Inoperable & Placed Unit in Action Statement of Tech Spec 3.3.3.8.Cause Unknown | /03L-0:on 790112,Sys 7 Data Logger Experienced Core Dump,Voiding Computer Memory Bank Which Rendered Remote Monitoring of Fire Detection Sys Inoperable & Placed Unit in Action Statement of Tech Spec 3.3.3.8.Cause Unknown | | | 05000346/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000346/LER-1979-011-03, /03L-0:on 790115,reactor Coolant Pump 1-2-2 Started W/Incorrect Breaker Alignment,Causing Low Voltage Relays to Trip Which de-energized Both 4.16 Kv Essential Buses C1 & D1.Caused by Personnel Error | /03L-0:on 790115,reactor Coolant Pump 1-2-2 Started W/Incorrect Breaker Alignment,Causing Low Voltage Relays to Trip Which de-energized Both 4.16 Kv Essential Buses C1 & D1.Caused by Personnel Error | | | 05000346/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000346/LER-1979-012-03, /03L-0:on 790116,during Surveillance Testing,Heat Traced Line Temp Measurement Points Below 105 F Limit.Caused by Injection of Makeup (Flush) Water After Boron Injection at Temp Lower than 105 F.Tests Rerun Satisfactorily | /03L-0:on 790116,during Surveillance Testing,Heat Traced Line Temp Measurement Points Below 105 F Limit.Caused by Injection of Makeup (Flush) Water After Boron Injection at Temp Lower than 105 F.Tests Rerun Satisfactorily | | | 05000346/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000346/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000346/LER-1979-013-03, /03L-0:on 790116,when Makeup Pump 1 Started for Surveillance testing,1/2 Inch Nipple at Discharge of Attached Gear Driven Lube Oil Pump Failed,Resulting in Oil Spray Which Required Pump Shutdown | /03L-0:on 790116,when Makeup Pump 1 Started for Surveillance testing,1/2 Inch Nipple at Discharge of Attached Gear Driven Lube Oil Pump Failed,Resulting in Oil Spray Which Required Pump Shutdown | | | 05000346/LER-1979-014-03, /03L-0:on 790116,during Shutdown,Boric Acid Addition Tanks (Baat) Total Vol 3-1/3% Below Tech Spec 3.1.2.9 Requirements.Caused by Reduced Baat Vol After Completion of Required Testing Followed by RCS Boration | /03L-0:on 790116,during Shutdown,Boric Acid Addition Tanks (Baat) Total Vol 3-1/3% Below Tech Spec 3.1.2.9 Requirements.Caused by Reduced Baat Vol After Completion of Required Testing Followed by RCS Boration | | | 05000346/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000346/LER-1979-015-03, /03L-0:on 790117,core Flood Tank 1-2 Isolation Valve CF1A Would Not Close by Remote Operation.Caused by Loose Set Screw.Cracked Pinion Gear & Associated Key Replaced Per Maint Work Order 78-2928 | /03L-0:on 790117,core Flood Tank 1-2 Isolation Valve CF1A Would Not Close by Remote Operation.Caused by Loose Set Screw.Cracked Pinion Gear & Associated Key Replaced Per Maint Work Order 78-2928 | | | 05000346/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000346/LER-1979-016-03, /03L-0:on 790124,emergency Lock Failed Leak Rate Test While Unit in Mode 5.Caused by Loosening of Shaft Seal (Teflon Packing) Due to Routine Use of Escape Lock.Packing Will Be Replaced During Next Convenient Outage | /03L-0:on 790124,emergency Lock Failed Leak Rate Test While Unit in Mode 5.Caused by Loosening of Shaft Seal (Teflon Packing) Due to Routine Use of Escape Lock.Packing Will Be Replaced During Next Convenient Outage | | | 05000346/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000346/LER-1979-017-03, /03L-0:on 790130,photoelectric Smoke Detector Ds 8605-E in Emergency Diesel Generator 1-1 Area Not Functional.Caused by Failure of Detector.New Detector Ordered & Fire Watch Patrol Established in Area | /03L-0:on 790130,photoelectric Smoke Detector Ds 8605-E in Emergency Diesel Generator 1-1 Area Not Functional.Caused by Failure of Detector.New Detector Ordered & Fire Watch Patrol Established in Area | | | 05000346/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000346/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000346/LER-1979-018-03, /03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily | /03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily | | | 05000346/LER-1979-019-03, /03L-0 on 790129:suction & Discharge Valves on Containment Spray Pump Were Closed.Caused by Personnel Error | /03L-0 on 790129:suction & Discharge Valves on Containment Spray Pump Were Closed.Caused by Personnel Error | | | 05000346/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000346/LER-1979-020-03, /03L-0 on 790205:10 of 18 Main Steam Safety Valves Found Outside Setpoint Range.Believed Caused by Changing Ambient Conditions at Valve Locations.Valves Adjusted & Retested Satisfactorily | /03L-0 on 790205:10 of 18 Main Steam Safety Valves Found Outside Setpoint Range.Believed Caused by Changing Ambient Conditions at Valve Locations.Valves Adjusted & Retested Satisfactorily | | | 05000346/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000346/LER-1979-021-03, /03L-0 on 790205:containment High Pressure Alarms Were Received & Safety Features Actuation Sys Channel 2 Erroneously Tripped.Cause Unknown.No Deficiencies Found from Surveillance Tests.Channel Returned to Operation | /03L-0 on 790205:containment High Pressure Alarms Were Received & Safety Features Actuation Sys Channel 2 Erroneously Tripped.Cause Unknown.No Deficiencies Found from Surveillance Tests.Channel Returned to Operation | | | 05000346/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000346/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000346/LER-1979-022-03, /03L-0 on 790208:diesel Fire Pump Battery Electrolyte Level in Four Cells Was Below Top of Cell Plates.Caused by Procedural Error.Levels Restored,Pump Declared Operable & Unit Removed from Action Statement | /03L-0 on 790208:diesel Fire Pump Battery Electrolyte Level in Four Cells Was Below Top of Cell Plates.Caused by Procedural Error.Levels Restored,Pump Declared Operable & Unit Removed from Action Statement | | | 05000346/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000346/LER-1979-023-01, /01T-0 on 790228:Startup Transformer 01 Taken Out of Svc;Surveillance Tests Not Performed within One Hour, Contrary to Tech Spec Requirements.Caused by Personnel Error.Testing Completed as Soon as Error Realized | /01T-0 on 790228:Startup Transformer 01 Taken Out of Svc;Surveillance Tests Not Performed within One Hour, Contrary to Tech Spec Requirements.Caused by Personnel Error.Testing Completed as Soon as Error Realized | | | 05000346/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000346/LER-1979-024-03, /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust | /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust | | | 05000346/LER-1979-025-03, /03L-0 on 790213:Ohio Edison Relay Testing Actuated Transfer Trip Receiving Relay & Tripped Switchyard Breakers.Caused by Failure of Util to Notify Toledo Edison Before Performing Relay Testing | /03L-0 on 790213:Ohio Edison Relay Testing Actuated Transfer Trip Receiving Relay & Tripped Switchyard Breakers.Caused by Failure of Util to Notify Toledo Edison Before Performing Relay Testing | | | 05000346/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | |
|