ML19282A961
| ML19282A961 | |
| Person / Time | |
|---|---|
| Site: | Zimmer |
| Issue date: | 02/16/1979 |
| From: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Borgmann E CINCINNATI GAS & ELECTRIC CO. |
| References | |
| NUDOCS 7903080429 | |
| Download: ML19282A961 (1) | |
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NUCLEAR REGULATORY COMMISSION f I D T'( l j REGloN 111 j
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GLEN E LLYN, lLLINoIS 60137 Docket No. 50-358 Cincinnati Gas and Electric Company ATTN:
Mr. Earl A. Borgmann Vice President Engineering Services and Electric Production 139 East 4th Street Cincinnati, OH 45201 Gentlemen:
This Information Notice is provided as an early notification of a possibly significant mitter.
It is expected that recipients will review the information for possible applicability to their facilities. No specific action or response is requested at this time.
If further NRC evaluations so indicate, an IE Circular, Bulletin or NRR Generic Letter will be issued to recommend or request specific licensee actions.
If you have questions regarding the matter, please contact the Director of the appropriate NRC Regional Office.
Sincerely, g g - On.
James G. Keppler Director
Enclosures:
1.
IE Information Notice No. 79-04 2.
List of IE Information Notice Issued in 1979 cc w/encls:
Mr. J. R. Schott, Plant Superintendent Central Files Director, NRR/DPM Director, NRR/ DOR PDR Local PDR NSIC TIC U. Young Park, Power Siting Commission 7 9 o 3 o 8 099
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U.S. NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT REGION III February 16, 1979 IE Information Notice No. 79-n4 DEGRADATION OF ENGINEERED SAFETY FEATURES Su=nsry On September 16, 1978, an unusual sequence of events occurred at Arkansas Nuclear One, Units 1 and 2.
The events involved the electrical power sources and culminated in the spurious activation and degraded operation of Unit 2 Engineered Safety Features (ESF). Analysis of the course of the incident has identified three safety concerns in the electrical distribution system operation and design.
(1) The offsite power supply for ANO Unit 1 Engineered Safety Feature loads was deficient in that degraded voltage could have resulted in the unavailability of ESF equipment, if it were to be needed.
(2) The design of the ANO site electrical system that provides offsite power to Units 1 and 2 did not fully meet the Co= mission's Regu'.a-tions, 10 CFR 50, Appendix A, General Design Criterion 17, because in certain circumstances a loss of one of the two offsite power circuits would also result in a loss of the other such circuit.
(3) Deficiencies existed in the operation of the Unit 2 inverters that convert DC to AC power for the uninterruptable 120 volt vital AC buses.
Description of Circumstances Initially Unit I was operating at 100 percent power; Unit 2 was in hot standby performing hot functional testing in preparation for initial criticality and power operation.1 Unit 1 auxiliary electrical loads were being supplied from the Unit I main generator via the unit auxiliary transformer. Unit 2 auxiliary electrical loads were being fed from the offsite grid through Startup Transformer No. 3.
The normal operating status was interrupted by the failure of the Unit 1 Loop "A" hain Steam Line Isolation Valve (MSIV) air operator solenoid causing the MSIV to close as designed. The Unit 1 Reactor Protection System sensed conditions requiring reactor shutdown and tripped the reactor. The 1 The Unit 2 Operating License did not permit criticality power operation at the time of the incident.
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