ML19276G612

From kanterella
Jump to navigation Jump to search
Forwards IE Info Notice 79-15, Deficient Procedures. No Action Required
ML19276G612
Person / Time
Site: Big Rock Point, Palisades  File:Consumers Energy icon.png
Issue date: 06/07/1979
From: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Dewitt R
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
References
NUDOCS 7907240252
Download: ML19276G612 (1)


Text

PDR g** "8 Gg UNITED STATES f(

NUCLEAR REGULATORY COMMIS510N i ~ 'r(i 3 nEcloN lli f

% k' Q,,h[f E

799 ROOSEVELT RO AD s,,9 cLEN ELLyN. stunOis not 27 v.....f JUN 7 1979 Docket No. 50-155 Docket No. 50-255 Consumers Power Company 2

ATTN:

Mr. R. B. DeWitt Manager of Nuclear Plant Operations 212 West Michigan Avenue Jackson, MI 49201 Gentlemen:

This Information Notice

, provided as an early notification of a possibly significant matter.

It is expected that recipients will review the infor-mation for possible applicability to their facilities. No specific action or response is requested at this time.

If further NRC evaluations so indi-cate, an IE Circular, Bulletin, or NRR Generic Letter will be issued to recommend or request specific licensee actions.

If you have questions regarding the matter, please contact the Director of the apnropriate NRC Regional Office.

Sincerely,

/

x.~

ames G. Keppler /k Director

Enclosure:

IE Information Notice No. 79-15 cc w/ enc 1:

Mr. C. J. Hartman, Plant Superintendent Mr. J. G. Lewis, Plant Superintendent Central Files Director. NRR/DPM Director, NRR/ DOR PDR Local PDR NSIC TIC Ronald Callen, Michigan Public Service Commission Anthony Roisman, Esq., Attorney Myron M. Cherry, Chicago 7 00724 0 A 62.

U.S. NUCLEAR REGULATORY COMMISSION OFFICr. OF INSPECTION AND ENFORCEMENT REGION III June 7, 1979 '

IE Information Notice No. 79-15 DEFICIENT PROCEDURES Summary On June 2,1979, at Arkansas Nuclear One - Unit 1, while observing conditions in the control room, an NRC inspector discovered an operational deficiency that could have resulted in the emergency feedwater system remaiaing isolated during subsequent power operation.

Description of Circumstances On June 2 while Arkansas Nuclear One - Unit I was preparing for startup, an NRC inspector in the control room found that during a surveillance test of the main feedwater check valves, the controls of the emergency feed-water system were positioned so that the system could not automatically respond if needed. The NRC inspector found that the test procedure being used by the licensed operators did not include, as it should have, instruc-tions either to bypass the emergency feedwater system or to return it to normal. The plant operators, without approved procedures covering this aspect of the test, bypassed the controls that would have started the feedwater system automatically. Lacking a procedural requirement to re-turn the system to normal, there was no assurance that emergency feedwater would be provided automatically if needed.

Following the Three Mile Island accident, the NRC required that operators be trained to initiate promptly the emergency feedwater system manually if it does not come on automatically. Thus, while no immediate safety hazard existed at the Arkansas Unit 1 plant because of the improper action, the NRC staff is concerned about the potential safety hazard of leaving the emergency feedwater system in the bypassed condition, about the possibility that other procedures at the Arkansas plant may be deficient and about the fact that the operators deviated from procedures in performing the surveillance test.

Arkansas Power and Light Cotpany h h j The June 2,1979, NRC Order con until the Com=ission staff is a DUPLICATE DOCUMENT trolling the development of ope procedures, and until there is Entire doctunent previously from those procedures, entered into system under:

ANO No. of pages:

.