ML19276F682

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LER 1-77-111 on 771210:while Securing Diesel Generator 3 from Control room,32D Relay & Diesel Lockout Relay Caught on Fire.Cause Undetermined.Relay Replaced,Recalibrated & Checked.Relay Circuits Trip Checked
ML19276F682
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/09/1978
From: Banks H
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19276F678 List:
References
LER-1-77-111, NUDOCS 7904060444
Download: ML19276F682 (2)


Text

M 366 LICENSEE EVENT REPORT a

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9 LICENSEE CODE 14 16 LICENSE NuvBEM 25 26 LicENSt YvrE Jo 57 L A T $8 ERCE d l0l5l0l-10131215 @l1 12 11 lo 17 17 @l0l1l019l7b l@

60 61 DOCKET NUMBE R 68 69 EVENT DATE 74 7b REPORf DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h M eu hvin-lAfter performine an E.C.C.S. load secuencing ence-diennt gnnnenent received.

The 1

1remotelv secured from the control room when a reverse power alarm wac l diesel generator output breaker was tripped by the control operator and em ke vu 1

Iobserved to be coming from 32D relay. When the cover for the 32D. Directional Power I 1

IRelay, was removed, the relay started to flane and was cytingefehoA bv n roch-icene.

lWhen the diesel generator output breaker door was opened. the diesel lockour enlov l

l l86DB, was also found flaming and was extinguished.

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VALVE SYSTEM CAUSE CAUSE CODE CODE SUBOODE COMPONENT CODE SV8 CODE SUBCODE AIYIXl@ W h (J_jh IElE h (h l Zlh I RI EI L I

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33 34 3b 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 'ufring was checked and l

INo cause for the f ailure was dere-innd All enlmv enveral laced. recalibrated. and checked.

Tha PAnF l lfound to be correct. The 32D relay was r The 86DBl l relay coil was replaced, the contacts cleaned, and the relay action checked.

l relay was then installed and recalibrated. The relay circuits were then visually l checked and trip checked.

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LER CONTINUATION -- RO# 1-77-111 Facility:

_BSEP Unit #1 Event Date:

12-10-77 CAUSE DESCRIPTION CON'T.:

A followup check will be made with the relay manufacturer to ensure that this type of relay does not have a history of failures.

If any problems are uncovered, an additional report will be submitted.