ML19276F676
| ML19276F676 | |
| Person / Time | |
|---|---|
| Site: | Brunswick |
| Issue date: | 12/05/1977 |
| From: | Banks H CAROLINA POWER & LIGHT CO. |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| Shared Package | |
| ML19276F671 | List: |
| References | |
| LER-1-77-98, NUDOCS 7904060428 | |
| Download: ML19276F676 (2) | |
Text
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57
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- 0 VENT CESCOc?CN With the reactor at power, in the RUN mode, RHR snubber on the steam condencint line I
50 was found inoperative by an auxiliary operator.
(Technical Specification 3.5.J.2) c0 I
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60 RO l-77-98 i
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- AUSE CESCAi TCN The broken snubber was apparently caused by water hac
- mer.
Periodic Test 8.2.2, RHR l
60 pumo operability was being performed daily due to the HPCI system beine inoperative EC l
(R0 1-7 7-9 5).
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l This 15. %ing recorted under Technical Specification Section 6.11.2.b(2).
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LER CONTINUATION -- RO #1-77-98 Facility: BSEP #1 Event Date 11-4-77 Corrective Action:
The snubber was replaced.
Action to Prevent Recurrence:
The operators have been cautioned to ensure the RHR heat exchanger is isolated and the system is filled and vented prior to starting RHR pumps. Filling and venting the RHR steam cor.densing piping has been covered in operator training. Parts are on c-der to repair the stern condensing valves that leak through and, :.? ow ste am to collect in the RHR piping.