ML19274D683

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IE Insp Rept 50-338/78-42 on 781211-15.Noncompliance Noted: Turbine Generator Automatic Stop Oil Functional Test Not Performed Prior to Reactor Startup on 781025, & 23 Temporary Procedural Changes Not Reviewed
ML19274D683
Person / Time
Site: North Anna Dominion icon.png
Issue date: 01/05/1979
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML19274D679 List:
References
50-338-78-42, NUDOCS 7902220167
Download: ML19274D683 (7)


See also: IR 05000338/1978042

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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Report No.: 50-338/78 ,2

Docket No.: 50-338

License No.: NPF-4

Licensee: Virginia Electric and Power Company

P. O. Box 26666

Richmond, Virginia 23261

Facility Name: North Anna Power Station, Unit 1

Inspectio.) at: North Anna Power Station, Miieral, Virginia

Inspection conducted:

Dacember 11-15, 1978

Inspector:

T. J. McHenry

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Approved by:

H. C. Dance, Chief

Date

Reactor Projects Section No.1

Reactor Operations and Nuclear Support Branch

Inspectiin Summary

Inspection on December 11-15, 1978:

(Report No. 50-338/78-42)

  1. 1-eas Inspected:

Routine unannounced inspection of plant operations, limiting

conditions for operation, and plant tour. The inspection involved 31 inspector

-hours on site by one NRC inspector.

Results: Of the three areas inspected, two items of noncompliance were

ident.ified in two areas (Infraction:

Failure to perform surveillance test,

338/78-42-01; Infraction:

Failure to review and approve temporary procedure

changes with 14 days, 338/78-42-02).

7902220\\W

RII Rpt. No. 50-338/78-42

1-1

DETAILS I

Prepared by:

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T. J. McHeng, Heactoi Insppfor

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Reactor Pr6jects Section No. 1

Reactor Operations and Nuclear

Support Branch

Dates of Inspection:

ecember 11-15, 1978

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Reviewed by:

H. C. Dance, Chief

'Dat e

Reactor Projects Section No. 1

Reactor Operrtions and Nuclear

Support Branch

1.

Individuals Contacted

a.

Virginia Electric Power Company

W. R. Cartwright, Station Manager

>J. D. Kellams, Superintendent, Station Operations

  • S. L. Harvey, Operating Supervisor
  • E. R. Smith, Jr. , Supervisor, Engineering Services
  • D. M. Hopper, Health Physics Supervisor
  • S. Sarver, System Health Physicist
  • D. C. Woods, hTC Coordinator
  • D. L. Smith, Resident QC Inspector, Operations
  • M. D. Tower, Quality Assurance Supervisor, Maintenance and

Operation

Several Control Room Operators and Operating Personnel

b.

Nuclear Regulatory Commission

  • M. S. Kidd, Resident Inspector
  • G.

R. Jenkins, Radiation Specialist

  • Denotes those present at the Exit Interview.

2.

Licensee Action on Previous Inspection Findings

No previous items of noncompliance or deviations were reviewed during

this inspection.

3.

Unresolved Items

No new unresolved items were identified during this inspection.

.

RII Rpt. No. 50-338/78-42

I-2

4.

Exit Interview

A meeting was held on December 15, 1978, with Mr. W. R. Cartwright,

Station Manager, and his staff members denoted in paragraph 1.

The

scope and findings presented in these Details which related to the

inspection activities were di cussed.

Items of noncompliance were

discussed, including station management's response and planned actions.

Also, four open items identified in the Details were discussed,

including station management's response and planned actions.

5.

Review of Plant Operations

The inspector reviewed the following Unit 1 logs and records for

October through November 1978, to ascertain whether operation was in

conformance with the Technical Specifications and established

administrative requirements:

Log-11, Action Statement Status log

Log-6A, Control Room log

Log-6B, Emergency Diesel and Boiler log

Log-6C, Turbine Building log

Log-6D, Auxiliary Building log

Log-6E, Outside log

Log-1, Shift Supervisor log

Log-2, Control Room Operators' log

Log-4, Operators' Surveillance Sheet

Log-12, Diesel Generator Running log

Log-8A, Liquid Waste log

Log-8B, Boron Recovery log

Log-8C, Gaseous Waste log

Plant Jumper log

Deviation Reports

a.

Turbine Generator Auto Stop Oil Functional Test

Technical Specification 4.3.1.1.1, Table 4.3-1, Item 18.A requires

that a functional test of Auto Stop Oil be performed prior to

reactor startup if not performed within the previous seven days.

During the review of the Control Room Log for October 25, 1978, it

was determined that PT-34.1, Turbine Generator Auto Stop Oil

Functional Test, had been performed subsequent to reactor startup.

The inspector discussed the performance of this test with control

room personnel who indicated that this test was performed routinely

following reactor startup since it was performed as prescribed by

the turbine startup procedure which follows reactor startup.

The

performance of this functional test subsequent to reactor startup

was discussed with the Operations Supervisor, who acknowledged

that an oversight of the prior to reactor startup requirement had

occurred and corrective measures would be taken to correct this

.

.

RII Rpt. No. 50-338/78-42

I-3

item.

Licensee representatives stated at the exit interview that

even though PT-34.1 had not been performed, the functional opera-

bility of the Auto Stop Trip was available due to existance of

trip status light for Auto Stop Oil prior to reactor start.

The

inspector indicated that failure to perform Auto Stop Oil Functional

Test prior to reactor start was an apparent item of noncompliance

with Technical Specification 4.3.1.1.1, Table 4.3-1, Item 18.A and

is identified as an infraction (338/78-42-01).

b.

Review of Deviation Reports

The inspector reviewed Plant Deviation Reports for period October

through November 1978 to confirm there were no violation of Technical

Specification limiting conditions for operations and reporting

requirements. Several Plant Deviation Reports were caused by

exceeding Technical Specification 6.8.3.c requirement that the

Station Nuclear Safety and Operating Committee (SNSOC) review and

station manager approve temporary procedure changes within 14

days. The inspector determined that many failures to meet the 14

day review and approval requirement had been identified by the

licensee and noted by an NRC inspector during inspection 338/78-18

on June 13-16, 1978, and that the licensee had taken corrective

action to correct and prevent recurrence.

The inspector discussed

the apparent ineffectiveness of the licensee corrective action

with a licensee representative who stated that the problem had

been corrected, and felt that only a small percentage of isolated

items existed.

The inspector reviewed the SNSOC meeting minutes

for the period of September 8-November 7,1978 and determined that

15 temporary changes had been identified by the licensee in excess

of the 14 day requirement.

The inspector discussed this item with

licensee representatives at the exit interview.

Licensee repre-

sentative stated that the record of late 14 day reviews and approvals

should be reviewed as it was felt that the percentage of these

items had significantly improved since June 1978.

The inspector

left this item unresolved at the exit, pending a detailed review

of identified overdue 14 day reviews and approvals by the NRC

Resident Inspector. The Resident Inspector review of SNSOC meeting

minutes within the period of July 3 through November 27, 1978,

indicated that for that period, 23 of 290 temporary procedure

changes were identified by the licensee to have exceeded the 14

day requirement. Even though the failure to review these temporary

procedure changes had been identified by the licensee, the number

and percentage of the occurrences of this item indicates that

corrective actions to prevent recurrence have not been effective.

This matter was discussed with the Plant Manager by telephone on

December 21, 1978, at which time the inspector indicated that this

item is an apparent item of noncompliance with Technical Specifi-

cation 6.8.3.c and is identified as an infraction (338/78-42-02).

1

RII Rpt. No. 50-338/78-42

I-4

c.

Functional Tests with Inputs to Solid State Protection System

During the review of PT-34.1, Turbine-Generator Auto Stop Oil Trip

Functional Test (noted in paragraph 5.a), the inspectcr found that

PT-34.1 did not verify input trip functions to both Train A and B,

Solid State Protection Systems (SSPS). The inspector discussed

instrumentation functional tests with a licensee representa-

tive who indicated that the tripping of both Trains of SSPS was

verified in instrumentation group periodic tests in that both the

trip status light and computer outputs were verified.

Licensee

representatives question the inspectors' concern since SSPS is

functionally tested as required by Technical Specifications.

The

inspector stated that functional testing of SSPS functionally

tested input circuitry within the SSPS but did not functionally

test the input circuitry from the process instrumentation. There-

fore, functional testing which inputs to SSPS must include func-

tional operability of inputs to both Trains of Solid State

Protection. This matter was discussed at the exit interview.

The

licensee stated that PT's 34.1 and 34.3 would be revised to provide

required functional checking of inputs to both Trains of Solid

State Protection.

Further, the licensee stated that a review of

other functional tests which input SSPS would be conducted. The

inspector indicated this item would remain open pending licensec

corrective action and subsequent review by an inspector at a

future inspection (338/78-42-03).

6.

Review of Safety Limits, Limiting Safety System Settings and Limiting

Conditions for Operation

The inspector reviewed plant logs, startup procedures and observed

plant operations to assure reactor operations were in conformance with

Technical Specification requirements for safety limits, limiting safety

system settings and limiting conditions for operation.

a.

Plant Startup Procedure Review

The inspector reviewed OP-1.5, Unit Startup from Hot Standby

procedures which were completed between July through November

1978.

During this review, the inspector noted that there was a

wide variance in the method used for the inverse multiplication

approach to criticality plots. The inspector discussed the

inverse multiplication startup plots with control room operators,

who stated that no procedure for performing the inverse multipli-

cation plots existed and the guidance for such plots was obtained

via the training program. The inspector discussed the lack of

approved procedural guidance for inverse multiplication plots with

the Operations Supervisor. The inspector stated that since the

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RII Rpt. No. 50-338/78-42

I-5

use of an inverse multiplication plot is only required when uncer-

tainty exists about the calculated critical data, procedural

guidance should be provided to assure the startup does not result

in critical conditions outside the limits established by the

Technical Specifications. This item was discussed at the exit

interview and licensee representatives stated that the matter

would be reviewed and procedural guidance for the performance of

inverse multiplication plots would be developed.

The inspector

stated that this item would remain open pending licensee develop-

ment of approved procedural guidance for inverse multiplication

plots and subsequent review by an inspector during a future

inspection (338/78-42-04).

b.

Wind Direction Channel Check

The review of Log-6A, Unit One Control Room log, indicated that

wind directions were routinely logged with a 60 to 100 degree

difference in direction between the indicator at 35 feet and 150

feet elevations.

In addition, no notation had been made on the

log indicating that one indicator could be possibly malfunctioning

even though '-chnical Specification 4.3.3.4 requires a daily

channel checn,

The inspector observed the wind direction recorders

during a plant tour and discussed the logged data with control

room personnel. Observation of wind direction recorders indicated

that instantaneous wind direction does vary; however, observation

of the recorder for sufficient time to estimate the average wind

directions indicated the average directions being approximately

equal A control room operator also stated that when the wind speed

is low the wind direction tends to vary to higher degrees. The

inspector discussed the lack of explanation on log-6A, when wind

speed variance between the two channels was high, with the Opera-

tions Supervisor who stated that the log would be reviewed and

revised as necessary.

The inspector stated this item would remain

open pending a review during a future inspection of the licensee's

corrective action to ensure an adequate performance and record of

the wind direction channel check (338/78-42-05).

c.

Power Calorimetric Review

The inspector reviewed completed copies of PT-24, Calorimetric,

for period of September through November 1978 to ascertain that

reactor power levels were maintained within the limits of the

Technical Specifications. The inspector discussed the methods for

obtaining the calorimetric data necessary for the power calculation

with control room operators.

It was determined f rom control room

operators that feed flow data was obtained directly from the

i

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RII Rpt. No. 50-338/78-42

I-6

computer. The inspector ascertained from plant personnel that

feed flow output from the computer is routinely calibrated;

however, the accuracy of the computer output could not be

established. This item was discussed at the exit interview. The

inspector stated that the concern was whether the feed flow accuracy

from the computer was adequate to meet the r aumption that the

calorimetric was accurate to plus or minus :.o percent in the FSAR

accident analysis. The licensee stated tha.

.n engineering evalua-

tion of the accuracy of the computer feed flow channel would be

conducted. The inspector indicated that this item would remain

open pending the licensee review and subsequent NRC inspection of

review data

(338/78-42-06).

7.

Plant Tour

The inspector toured portions of the facility including the auxiliary

building, turbine building and control room to ascertain the general

state of cleanliness and housekeeping.

Control room operations, including

observation of operations following an unscheduled reactor trip were

observed and discussed with control room personnel to assure compliance

with Technical Specifications. No problems were identified.

.