05000318/LER-1978-051-03, /03L-0 on 781212:during Normal Operation,The Containment Atmosphere Sampling Pump Tripped,Rendering Both Particulate & Gaseous Radioactivity Monitors Inoperable. Caused by Failed Pump Bearing

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/03L-0 on 781212:during Normal Operation,The Containment Atmosphere Sampling Pump Tripped,Rendering Both Particulate & Gaseous Radioactivity Monitors Inoperable. Caused by Failed Pump Bearing
ML19274D218
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 01/11/1979
From: Carroll J, Miernicki M
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19274D217 List:
References
LER-78-051-03L-01, LER-78-51-3L-1, NUDOCS 7901160287
Download: ML19274D218 (1)


LER-1978-051, /03L-0 on 781212:during Normal Operation,The Containment Atmosphere Sampling Pump Tripped,Rendering Both Particulate & Gaseous Radioactivity Monitors Inoperable. Caused by Failed Pump Bearing
Event date:
Report date:
3181978051R03 - NRC Website

text

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