ML19274C910
| ML19274C910 | |
| Person / Time | |
|---|---|
| Site: | La Crosse File:Dairyland Power Cooperative icon.png |
| Issue date: | 11/30/1978 |
| From: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Linder F DAIRYLAND POWER COOPERATIVE |
| Shared Package | |
| ML19274C911 | List: |
| References | |
| NUDOCS 7901050331 | |
| Download: ML19274C910 (2) | |
See also: IR 05000409/1978014
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UNITED STATES
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NUCLEAR REGULATORY COMMISSION
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GLEN E LLYN, ILLINotS 60137
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Docket No. 50-409
Dairyland Power Cooperative
ATTN:
Mr. F. W. Linder
General Manager
2615 East Avenue - South
La Crosse, WI
54601
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Centlemen:
This refers to the inspection conducted by Mr. L. A. Reyes of
this office on October 27-30 and November 3-5, 1978, cf activities
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at LACBWR Nuclear Generating Plant authorized by NRC Operating
License No. DPR-45 and to the discussion of cur findings with
Mr. R. Shimshak at the conclusion of the inspection.
The enclosed copy of our inspection report identifies areas
exanined during the inspection. Within these areas, the
inspection consisted of a selective examination of procedures
and representative records, observations, and interviews with
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personnel.
No items of noncompliance with NRC requirements were identified
during the course of this inspection.
Your initial attempts at demonstrating that the containment leak rate
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at LACBWR was within allowable Technical Specification limits f ailed
on two consecutive occasions in 1975 and 1978.
Consequently, accord-
ing to 10 CFR 50 Appendix J, Section III A.6.b, a Type A test is
required to be performed at each plant shutdown for refueling or
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approximately every 18 months, whichever occurs first, until two
consecutive Type A tests meet acceptance criteria. The increased
surveillance frequency is required to commence during your next
refueling shutdown.
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7901050 %
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Dairyland Power
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NOV 30 378
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Cooperative
In accordance with Section 2.790 of the NRC's " Rules of
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Practice," Part 2, Title 10, Code of Federal Regulations, a
copy of this letter and the enclosed inspection report will
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be placed in the NRC's Public Document Room, except as follows.
If this report contains information that you or your contractors
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believe to be proprietary, you must apply in writing to this
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off2ce, within twenty days of your receipt of this letter, to
withhold such information from public disclosure.
The
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application must include a full statement of the reasons for
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which the information is considered proprietary, and should be
prepared so that proprietary information identified in the
application is contained in an enclosure to the application.
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We will gladly discuss any questions you have concerning this
inspection.
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Sincerely,
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James G. Keppler
Director
Enclosure:
IE Inspection
Rpt No. 50-409/78-14
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cc w/ encl:
Mr. R. E. Shimshak, Plant
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Superintendent
Central Files
Reproduction Unit NRC 20b
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Local PDR
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Anthony Roisman, Esq.,
Attorney
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