05000193/LER-1978-004-03, /03L-0 on 780109:main Steam Line Low Pressure Switches Found to Actuate at Approx 35 Psig Below Tech Spec Requirements.Caused by Limited Setpoint Drift.Existing Surveillance Program Considered Adequate

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/03L-0 on 780109:main Steam Line Low Pressure Switches Found to Actuate at Approx 35 Psig Below Tech Spec Requirements.Caused by Limited Setpoint Drift.Existing Surveillance Program Considered Adequate
ML19269D538
Person / Time
Site: Rhode Island Atomic Energy Commission
Issue date: 02/16/1978
From: Mathis C
BOSTON EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19269D536 List:
References
LER-78-004-03L, LER-78-4-3L, NUDOCS 7906040217
Download: ML19269D538 (1)


LER-1978-004, /03L-0 on 780109:main Steam Line Low Pressure Switches Found to Actuate at Approx 35 Psig Below Tech Spec Requirements.Caused by Limited Setpoint Drift.Existing Surveillance Program Considered Adequate
Event date:
Report date:
1931978004R03 - NRC Website

text

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I 30 A,c&D were found to actuate at approxiEtely 35 psig below the requirements of i

fBT 1 1 ITTTll Table 3.2. A of the Technical Spuifications. These instruments initiate a contain-l isolation signal to the Main Steam isolation valves if the Reactor Mode Switch l [TTT1 I ment lo ls ] l 1s in the RUN position. These instruments were immediately recalibrated and l

lol7]l satisfactorily tested.

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o l This occurrence was caused by limited setpoint drift.

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