ML19263E590
| ML19263E590 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 05/29/1979 |
| From: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Jeffery Grant TOLEDO EDISON CO. |
| References | |
| NUDOCS 7906200137 | |
| Download: ML19263E590 (1) | |
Text
e
'I $th p nasop UNITED STATES
[
q(,
NUCLEAR REGULATORY COMMISSION l',o y
3e REGloN til 7.
s'-!
no noosevrty nono
.[
g
~
corn ettvn. itusois soin MAY Z 91979 Docket No. 50-346 Toledo Edison Company ATE:
Mr. James S. Grant Vice President - Energy Supply Edison Plaza 300 Madison Avenue Toledo, OH 43652 Gentlemen:
This Information Notice is provided as an early notification of a possibly significant matter.
It is expected that recipients will review the information for possible applicability to their facilities.
No specific action or response is requested at this time.
If further NRC evaluations so indicate, an IE Circular or Bulletin will be issued to recommend or request specific licensee actions.
If you have questions regarding this matter, please contact the Director of this office.
Sincerely, A
L ames G.
'ep er Director
Enclosure:
IE Information Notice No. 79-13 cc w/ enc 1:
Mr. T. Murray, Station Superintendent Central Files Director, NRR/DPM Director, HRR/ DOR PDRgg }}4 Local PDR NSIC TIC Harold W. Kohn, Power Siting Commission Helen W. Evans, State of Ohio 7906200137
U.S. ' NUCLEAR REGULATORY COMMISSION Y OFFICE OF INSPECTION AND ENFORCEMENT REGION III May 29, 1979 IE Information Notice No. 79-13 INDICATION OF LOW WATER LEVEL IN THF OYSTER CREEK REACTOR Su==ary A loss of feedwater transient at the Oyster Creek facility on May 2, 1979, resulted in a significant reduction in water inventory within the reactor core shroud area as measured by one set of water level instruments (triple low level), while the remaining level instruments, sensing from the reactor annulus area indicated water levels above any protective feature setpoint (Figure 1). The water level within the core shroud area was reduced below the " triple low level" setpoint of 4-feet, 8-inches above the top of the fuel. Subsequent analysis by the licensee has determined that the minimum collapsed water level (solid, without steam voids) over the top of the fuel was 1 to 1-1/2 feet. Coolant sa=ple analyses and offgas release rates do not indicate any fuel damage occurred. General Oyster Creek is a non-jet pump BWR with licensed power of 1930 MWt. The plant was first made critical May 3, 1969. Status Before Transient Operating at near full power with the main parameters at levels as follows: 1895 MWt power level 79" Yarway (13'4" over top of fuel) reactor water level 1020 psig reactor pressure 7.1x106 f /hr feedflow 2288 195 14.8x104 gpm recirculation flow rate (4 pumps) 12 paid core Ap Equipment Out of Service (DOS DUPLICATE DOCUMENT "D" recire pump 00S due to se "B" startup transformer 00S f Entire document previously entered into system under. ANO / r, No. of Pages: .}}