ML19263C979

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LER 79-004/03L-0 on 790214:during Routine Calibr of Torus Level Transmitter Lt 16-19-38A,instrument Could Not Be Calibr to Limits Specified.Caused by Buildup of Rust & Crud in Transmitter Capsule Cavity.Transmitter Was Replaced
ML19263C979
Person / Time
Site: Vermont Yankee Entergy icon.png
Issue date: 03/16/1979
From: Conway W
VERMONT YANKEE NUCLEAR POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19263C973 List:
References
LER-79-004-03L, LER-79-4-3L, NUDOCS 7903200391
Download: ML19263C979 (2)


Text

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Nave or enEPARER

VTVYS1 05000271 LER 79-4/3L EVENT DESCRIPTION AND PROBABLE CONSEOUENCES During routine calibration of the torus level trausmitter LT 16-19-38A, it was determined that the instrument could not be calibrated to the speci-fied limits of Tech. Spec. Table 3.2.1. The EPCI System was declared in-operable and alternate testing in accordance with Tech. Spec. 3.5.E.2 was initiated.

Within approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> from the time of discovery, the trans-mitter was returned to ser/ ice and alternate testing was secured.

Based on the fact that the redundant torus water level instrumenta-tion channel was operable, it was concluded that there were no adverse consequences to the public health or safety as a result of this event.

There were no previous reportable occurrences of this type.

CAUSE DESCRIPTION AND CORRECTIVE ACTION The apparent cause of this event appears to be an accumulation of rust and crud buildup in the transmitter capsule cavity.

Corrective action was to replace the transmitter with a spare of like kind.