05000306/LER-1979-029-03, /03L-0:on 791102,during Surveillance Test,Turbine Driven Auxiliary Feedwater Pump Did Not Start.Cause Unknown. Valves Being Checked for Proper Position Every 4-h & Design Change Initiated

From kanterella
(Redirected from ML19260A756)
Jump to navigation Jump to search
/03L-0:on 791102,during Surveillance Test,Turbine Driven Auxiliary Feedwater Pump Did Not Start.Cause Unknown. Valves Being Checked for Proper Position Every 4-h & Design Change Initiated
ML19260A756
Person / Time
Site: Prairie Island Xcel Energy icon.png
Issue date: 11/30/1979
From: Hunstad A
NORTHERN STATES POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19260A752 List:
References
LER-79-029-03L, LER-79-29-3L, NUDOCS 7912030202
Download: ML19260A756 (1)


LER-1979-029, /03L-0:on 791102,during Surveillance Test,Turbine Driven Auxiliary Feedwater Pump Did Not Start.Cause Unknown. Valves Being Checked for Proper Position Every 4-h & Design Change Initiated
Event date:
Report date:
3061979029R03 - NRC Website

text

'

NOV 27 1979 Rcroo. -

(7-77) 1 C C, OCbI LJL UJF6 LICENSEE EVENT REPORT CONTROL BLOCK: l l

l l l

l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

- l 0 l0 l0 l0 l 0l -l0 l 0 l@ 4 l1 l1 l1 l 1 l@l l

l@

M ! N l P l I l N l 2 l@15 0

0 o i LICENSEE CODE 14 LICENSE NUMBER 26 26 LICENSE TYPE Jo 67 CAT 58 7

8 9 CON'T [0] Q 0l5 0 l0 l0 3l0l6 @l11110 217 l9 hl l l 1 l 3 l 0 l 7 l g l@

o i 8

60 61 DOCKET NUM8ER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h ITTT1 1 During surveillance test, No. 22 Turbine-Driven Auxiliary Feedwater Pump did not I

o 3 istart. Overspeed trip valve was found tripped. An inspection of Unit 1 revealed l

the overspeed trip valve for No. 11 Pump was also tripped. Redundant pumps were l

o 4 0 6 l operable. No ef fect on public health and safety.

l 10 is l l l

0 7 l l

10isI l

80 7

8 9 SYSTEM

CAUSE

CAUSE COMP.

VALVE CODE CODE SUSCODE COMPONENT CODE SU8 CODE SUSCODE h Wh Wh V lA lL lV lE X lh Wh W h O 9 lC H

7 8

9 10 11 12 13 18 19 20 SEQUE NTI AL OCCURRENCE REPORT REVISION LE RrRO EVENT YEAR REPORT NO.

CODE T'PE NO.

h,Rg l21 7 9l

[-j l 0l2 9l y

10 l 3l W

[.-j y

22 23 24 26 27 N

N 30 41 32 K N AC ON P NT ME HOURS S

IT FOR 8.

SUPPL M AN UF ACTU R E R Ql]@

W@

W@

l 0l0 0

0l y@

{g Al@

l G l1 l 5 l 3 l@

33 34 35 M

37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 i o l Cause unknown. Valves are being checked for proper position every four hours. A I

Design Change has been initiated to provide " valve tripped" annunciation in the 1

i i l control room.

EI I

i 4 l

l 7

8 9 80

$A S

% POWE R OTHER STATUS Dis OV RY DISCOVERY DESCRIPTION

(_QJh 0l 0 0lh!

NA l

b h! Surveillance Test and insoection 1 5 ACitVITY CO TENT RELE ASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE NA l

NA l

I 6 7

8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUM8ER TYPE DE SCRIPTION l 0 l 0 l 0 l@l Z l@l NA l

i 7 PERSONNE L INJURIES NUM8En

DESCRIPTION

l0 0 0l@l NA l

i a 7

8 9 11 12 80 LOSS OF OR OAMAGE TO FACILITY OO O

D D

9-i TYPE DESCRIPTIO~

y y@l NA

[\\

g T]

' * ' ~

"'"*U'

'kUUD 80 7

8 9 to ISSUE JESCRIPTION hl NA l llllllllll l l *g 2 o 7

8 9 10 68 69 80 g A. A. Hunstad P P R

PHON E:

7 912 0 3 0 E_ o 7_,