ML19259A878

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Monthly Operating Rept for Dec 1978
ML19259A878
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 01/02/1979
From: Connell C
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
Shared Package
ML19259A876 List:
References
NUDOCS 7901110113
Download: ML19259A878 (7)


Text

V OPElt AllNG DATA Hl.PoltT DOCKET NO. 50-7ff 6 DA1E l-2-79 COMPl.ETEl) ItY C. tonne 1I TELEPilONE (9l 1) 7 W-0200 OPER AYING STA7115 Notes ,

1. Unit Name: ?"'H an poi nt f!o. 3 Muc3 car Power Plant rsn ane 107o
2. Reportin;: Period:
3. Licensed 1 hennal Power (MWI): - )025
4. Nameplate Itating (Gross MWe): 1013
5. Design Eh ctries!ItatingINet MWel: ^66
6. Maximum Dependable Capacity (Cross MWe): 1000
7. hicximum Dependable Capacity (Nc MWe): 965
8. If Changes Occurin Capacity itatings(It;ms Number 3 Through 7) Siace Last Report. Give Reasons:

None None

9. Power Level To Which Restricted. lf Any (Net MWel:
10. Reasons For Restrictions,if Any: "y TIJs Month Yr.-to-Date Cumulative 744 8760 20497
11. Ilours in P porting Period -

477 6679.32 _ 1R660_94

12. Numbu Of flours Reactor Was Crities! 0 o 0 -
13. Reactor Resene Shutdownllours . 562.95 6366.97 15207.7 I4. Ilours Generator On-Line 0 0 0
15. Un 'teserve Shutdown 11ours 16,976,609 40.251.169 1,603,787
16. Cross Thernui Energy Generated (MWil) 5.670.'11 11 7q'_771
17. Gross Electrical Energy Generated (MWill 536.480__.

416 n'1 s as7 n1 12.84A.810-

18. Net Electrical Energy Gencrated (MWil) 75 -7 7' 7 74 '

^19. Unit Senice Isetor . .

'20. Unit Availabi!'ty Factor . 74 7 7' 7 :_' .,

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21. Unit Capacity Factor (U>ing MDC Net)

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22. Unit Cagurity Factor (Udng DER Net) 71 a' 'c4 e ec_c

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23. Unit Forced Out. ige 1: ate
24. Shutdowns Scheduled Oscr Nest 6 Months (Type.Date.and Duration of Each):

n,-,

25. If Shul Down A End Of Reguirt Period. Ihtimatest Date of Startup:
26. Units in les: Status tPrior to Commercial Operatimii:  ::arceast Aehlesed A

INilu t. CHil tral.11 Y .

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- iun ni. nre nacity couui ucni.on na nos .. . .-

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Summary of Operating Experience December 1978 Indian Point Unit 3 was synchronized to the bus for a total of 562.95 hour0.0011 days <br />0.0264 hours <br />1.570767e-4 weeks <br />3.61475e-5 months <br /> $ producing a gross generation of 536,480 mwe for this reporting period.

During the reporting period, the unit experienced a shutdown, load reduction and a trip.

The shutdown occurred on December 7 at 0915. Steam jet air ejector discharge and necondary water samples indicated a steam generator tube leak. Upon verification of activity levels, the operator immediately started a 150 mwe/hr load reduction. The unit was removed from service at 15:22. The problem was isolated to a single leaking tube in No. 33 steam generator. The tube was plugged and the unit returned to service at 20:50 on December 14, 1978. A delay was encountered unile bringing the unit up to full power. Main boiler feed pump #32 would not come up to speed due to problems in the control oil system. After the problems were solved the pump was returned to service and load was increased to full power at 03:30 on December 16.

On December 16 at 05:20 #32 main boiler feed pump tripped and load was reduced to 800 mwe. The cause of the boiler feedwater pump trip was attributed to dirt in the governor control system. The dirt was removed and the unit was returned to full load at 11:00 of the same day.

The unit experienced a reactor trip during this period. At 21:08 on December 18, the unit tripped on #33 low steam generator level. The cause of the problem 'ias the loss of #32 boiler feed pump. Subsequent investigation did not reveal any problems with the' feed pump. The unit was.rcturned to service at 04:43 on December 19, 1978. .

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A\ I:l( A(.1: IMil.Y UNII l'OWI.It 1.1.VI.I.

- DOCKET No. co-21'r.

l and s .in Po,i ni UNIT ilo 3 DATE Januarv 2, lo;

. COMPLETED BY C . _C onne l l TELEPil0NE 9Ih-739-82U '

&lONTil December 1978 ,

DAY AVER AGE DAILY POWER LEVEL DAY AVERAGE DAILY POWr:n LEVEL (MWe-Net) (MWe-Net) .

A9 17 o41 I -

964 842 2 18 64 19 s19 3

965 20 926 4 ._..

964 gg 953 5

^5 22 057 6

do' 23 ocA 7

0 24 a5A 8

0 25 957 9 _

0 26 960 10

^ 27 " P

0 28 960 32 29 **A 13 0 0 30 458 14 546 31 a60

. 15 16 927 1NSTRUCTIONS On this fornut.hs the sserage daily unit power levelin MWe Net for exh day in the reportmg month. Compute lo the nearest whole megawatt.

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DOCKET NO. 50 'q6 ,,,,

UNITSilUTDOWNS AND POWER REDUCTIONS ,

UNIT N VIE Indian Point rinit 3

% DATE Januarv 2, 1979 COMPLETED BY C- conn'll REPORTMONT11 December 1978 TELErl10NE N141 m  ?"

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- ,k? .$ llcenscc Eg, f% Cause & Currective No. Date l[- gg  ;; .855 Event g? g "'g ,

Action to oE 5 j;8g Report #. m L8 g -

Prevent Recurrence g

20 781207 F 179.58 A I NA CB HTEXCH F Primary to Secondary Leak in #33

. S. team Generator. Tube plugged Los's of #32 MBFP/Centrol Oil 21 781216 F *0-A 1 NA . HH pump.XX B

  • Blockage / Cleaned Orifices .

22 781118 F 2.17 A 3 NA HH Pump XX B Loss of #32 MBFP/ Control Oil Blockage / Cleaned Orifices

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I 3 . 4 F: Fcned 2- Reason: Method: Exhibit F Instructions S: Sceduled A. Equipment Failure (Explain) 1 Manual for Preparation of Dara B Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee C Refueling 3 Automatic Scram. Esent &;.orI (LER) Fi!c (SUREG-D.Repulatory Restriction 4 Other(Explain) 0161)

E Operator Training & License Examination F Administrative 5 G Operational Error (Explain) Exhibi H - Same Source -

Cal77) II.Other (Explain)

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DOCKET NO. 50-N UNIT SilUTDOWNS AND POWER REDUC 110NS UNIT N \\1E Indian Point Unit 3*

6 DATE Januarv 2, 1979 COMPLETED BY c. conr.all REPORTMONT11 Decembor 1978 TELEr!!ONE N141 m- C '

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3g 3;; )gye .E Licensee Event

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o-3 Cause & Currestive Action to H

$E $ ,~i ;g a Report #. N0 $U -

Prevent Recurrence e  ! U 20 781207 P 179.58 A ,

1 NA CB IITEXCII F Primary to Secondary Leak in #33 S. team Generator. Tube plugged Los's of #32 MBPP/Centrol Oil 21 781216 F *O.

A 1 NA , Illi pump XX'B

- Blockage / Cleaned Orifices .

22 781118 F 2.17 A 3 NA Illi Pump XX B Loss of 432 MBPP/ Control Oil Blocka.ge/ Cleaned Orifices e, , . .

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I 3 , 4 F: Ferced 2- Reason: Method: Exhibit F -Instructions S: Scheduled A Equipment Failure (Explain) 1.Manu:I for Preparation of Dara B. Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee C Refocling 3 Automatic Scram. Esent Report (LER1 Fue (NUREG-D Regulatory Restriction 4-Other(Explain) 0161)

E Operator Training & License Examination -

F Administrative 5 G Operational Error (Explain) Exhibi.H Same Souree .

(9/77) Il Other (Explain) ,

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MONTHLY I & C CATEGORY I REPORT .

December 1978 Month Date '

W.R. # Equipment Malfunction Corrective Action 12/1/78 ILC-I-00ll8-38 #31 S.I. Accum Drain Solenoid burned out Replaced solenoid

, valve 12/19/78 IC&-I-00035-5 TCV-130 Not controlling properly in Loose positioner on valve, auto. tightened screws 12/26/78 I&C-I-00234-2 R-20 Recorder Recorder does n,c respond to Replaced recorder pen source check motor 12/19/78 I&C-I-000242-3C #31 Battery charger Ground Cleared ground on D.C.

distribution system 12/28/78 I&C-I-00229-2 Channel III iodine Failure alarm activates with. Tightened detector cable monitor indicator reading zero connector 12/29/78 I&C-I-00235-2 Channel II nuclear power Drifting Replace unit, eerformad static gain unit calibration and check

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